Information Notice No. 92-39: Unplanned Return to Criticality During Reactor Shutdown
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF NUCLEAR REACTOR REGULATION
WASHINGTON, D.C. 20555
May 13, 1992
NRC INFORMATION NOTICE 92-39: UNPLANNED RETURN TO CRITICALITY DURING
REACTOR SHUTDOWN
Addressees
All holders of operating licenses or construction permits for nuclear power
reactors.
Purpose
The U.S. Nuclear Regulatory Commission (NRC) is issuing this information
notice to alert addressees to recent events involving unplanned returns to
criticality caused by the cooldown of the reactor coolant system during
reactor shutdowns. It is expected that recipients will review the
information for applicability to their facilities and consider actions, as
appropriate, to avoid similar problems. However, suggestions contained in
this information notice are not NRC requirements; therefore, no specific
action or written response is required.
Description of Circumstances
The licensees for the following plants recently experienced unplanned
criticalities during reactor shutdowns: the Monticello Nuclear Generating
Plant, the Big Rock Point Nuclear Plant, and the Grand Gulf Nuclear Station.
Monticello
On June 6, 1991, an unplanned criticality occurred at the Monticello Nuclear
Generating Plant during a reactor shutdown when an unanticipated cooldown
occurred in conjunction with rod insertion. The licensee initiated this
shutdown to repair a leaking safety-relief valve shortly after the plant was
returning to power following a refueling outage.
Since this shutdown occurred shortly after the cycle startup, the reactor
did not generate sufficient decay heat to produce the steam needed to supply
the normal steam system loads and still maintain pressure in the reactor.
As control rods were being inserted using notch insertion, the reactor
coolant system pressure and temperature began to decrease. As long as the
operator continued to insert control rods, the reactor remained subcritical.
However, when the operator stopped inserting control rods to review and
evaluate plant conditions, the cooldown continued, adding sufficient
reactivity to overcome the negative reactivity from the insertion of control
rods and causing the reactor power to increase. The reactor power continued
to
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increase until an intermediate-range monitor (IRM) tripped on a high-high
flux setpoint, causing a reactor scram.
Further details of the event may be found in Licensee Event Report
50-263/91-15 or NRC Inspection Report 50-263/91-13.
Big Rock Point
On November 30, 1991, an unplanned criticality occurred at the Big Rock
Point Nuclear Plant during a reactor shutdown when a cooldown occurred in
conjunction with a rod insertion. The event occurred during a scheduled
shutdown for a refueling outage.
After taking the main turbine off line and bringing the reactor to a
subcritical condition, the licensee delayed actions to continue inserting
control rods while changing shifts. However, the reactor coolant system
continued to cool down because the normal steam system loads were removing
heat. The cooldown added sufficient reactivity to eventually overcome the
effects of the control rods, and the reactor returned critical. The
operators noticed the condition in approximately 2 minutes and took the
appropriate actions to return the reactor subcritical.
Further details of the event may be found in Licensee Event Report
50-155/91-009 or NRC Inspection Report 50-155/91-25.
Grand Gulf
On December 30, 1991, an unplanned criticality occurred at the Grand Gulf
Nuclear Station during a reactor shutdown when a cooldown occurred in
conjunction with a rod insertion. The event occurred during a scheduled
shutdown for a maintenance outage to replace a recirculation pump shaft. To
minimize the release of plated-out radioactive material from the fuel
cladding and channels to the reactor coolant system, a slow power reduction
and a slow cooldown were prescribed for this shutdown.
The slow power reduction and the effects of an earlier outage minimized
reactor decay heat and xenon peaking. The operators were driving rods into
the core individually because gang drive for the control rods was
unavailable. This made the reactivity insertion slower than normal. The
operators inserted rods to reduce flux to range 3 on the IRMs and stopped
rod insertion in order to perform a source range monitor surveillance.
Indicated power reached IRM range 1. However, the reactor coolant system
continued to cool down because the normal steam system loads were removing
heat. In order not to affect the source range monitor surveillance, the
shift supervisor elected to not insert control rods and alerted the
operators to the possibility of a return to criticality as the cooldown
continued. The reactivity added by the cooldown eventually overcame the
effects of the control rods. The reactor returned to a critical condition,
and reactor power increased on a reactor period between 300 to 800 seconds.
The operators, having been trained on a similar event at another BWR, were
monitoring the condition and expected the power to increase to the point of
adding heat, where the fuel and moderator temperature coefficients would
halt the reactor power increase. As the power increased, the
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reactor operator ranged the IRMs to prevent a reactor scram. Power level
remained on scale. The power increase was terminated with the IRMs reading
on range 7 and 8. The operators completed the source range monitor
surveillance, then resumed inserting rods and successfully completed the
shutdown.
Further details of the event may be found in NRC Inspection Report
50-416/92-04 and Licensee Event Report 50-416/91-16.
Discussion
The underlying principle of reactivity management is to maintain the reactor
in the desired condition by properly anticipating, controlling, and
responding to the plant's changing parameters. The experience at
Monticello, Big Rock Point, and Grand Gulf indicates that shutdowns in
situations with low decay heat present a unique challenge to reactivity
control if inadvertent recriticality is to be prevented. These events
emphasize the importance of the operator giving continuous attention to
plant parameters during a shutdown. Further, accepting recriticality
without prior management approval and procedures, i.e., an ad-hoc approach,
raises concerns due to the lack of opportunity for contingency planning.
This information notice requires no specific action or written response. If
you have any questions about the information in this notice, please contact
one of the technical contacts listed below or the appropriate Office of
Nuclear Reactor Regulation (NRR) project manager.
Charles E. Rossi, Director
Division of Operational Events Assessment
Office of Nuclear Reactor Regulation
Technical contacts: Melvyn Leach, RIII
(708) 790-5559
Geoffrey Wright, RIII
(708) 790-5695
Paul O'Connor, NRR
(301) 504-1307
Attachment: List of Recently Issued NRC Information Notices
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