Information Notice No. 84-76: Loss of All AC Power
SSINS No.: 6835 IN 84-76 UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF INSPECTION AND ENFORCEMENT WASHINGTON, D.C. 20555 October 19, 1984 Information Notice No. 84-76: LOSS OF ALL AC POWER Addressees: All nuclear power reactor facilities holding an operating license (OL) or construction permit (CP). Purpose: This notice is provided to alert recipients of a significant degradation in the level of safety caused by loss of all ac power. It is expected that recipients will review this information for applicability to their facilities and consider actions, if appropriate, to preclude similar problems occurring at their facilities. However, suggestions contained in this notice do not constitute NRC requirements and, therefore, no specific action or written response is required. Description of Circumstances: On July 26, 1984, Susquehanna Steam Electric Station Unit 2 was operating at 30% power and Unit 1 was operating at 100% power when the licensee began preparations for a "Loss of Turbine Generator and Offsite Power" startup test on Unit 2. Test conditions required that the electrical supplies to the units be separated so that all Unit 1 engineered safety system buses were to be fed from the Unit 1 startup transformer, all Unit 2 engineered safety system buses were to be fed from the Unit 2 startup transformer, and all feeder breakers from the Unit 1 startup transformer to the Unit 2 engineered safety system buses were to be racked out. The tie breaker between Unit 1 and Unit 2 auxiliary buses also was required to be racked out. All loads common to both units were to be placed on Unit 1 supplies. After establishing the required test configurations and prerequisites, the startup test was initiated by simultaneously opening the Unit 2 main generator output breakers and the Unit 2 startup transformer feeder breaker. As expected, the reactor tripped, turbine bypass valves opened and containment isolation occurred. However, the four emergency diesel generators did not start and all four feeder breakers to the Unit 2 engineered safety system buses remained closed. The breakers should have opened and the diesel generators should have started automatically when the startup transformer feeder breaker opened. The operator opened these breakers from the control room. When the diesels still did not start, the operator manually started all four diesels from the control room. Diesel generator D tripped on overvoltage, and B tripped on overvoltage and underfrequency. Diesel generators A and C idled but did not close onto their associated buses. Diesel generator A exhibited large frequency 8410180185 . IN 84-76 October 19, 1984 Page 2 of 3 oscillations and was manually tripped by the operator. The operator tried to manually close diesel generator C breaker to the associated bus, but the breaker would not close. The operator then closed the startup transformer breaker and attempted to close the feeder breakers to the engineered safety system buses, but they would not close. At this point, operators were instructed to rack in the feeder breakers from the Unit 1 startup transformer to the four Unit 2 engineered safety system buses. As each breaker was restored to operability, the related engineered safety system bus preferred feeder breaker closed and the related tripped diesel generator (A, B, and D) automatically started. Power was restored to the first engineered safety system bus in approximately 11 minutes and the last bus in approximately 18 minutes. After restoring power, diesel generators A, B, and D were shut down manually from the control room as they had high priority alarms. During the loss of all ac power to Unit 2, a significant portion of the instrumentation in the control room failed downscale. The dc powered instrumentation available to the operator included two narrow range level instruments for monitoring reactor water level, high pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) supply pressure indicators for monitoring reactor pressure, and a source range monitor. The full core display provided erroneous indication that a significant number of rods had not inserted into the core, which initially confused the operators. The shutdown was confirmed, based on the indication from source range monitor instrumentation and the reactor pressure trend. The control room had no indication of suppression pool temperature and no indication of reactor water level below zero on the narrow range instrument. Personnel stationed at the local instrument racks were able to provide reactor water level information to the control room. Discussion: The causes of the event include operator error, inadequate operator training, imprecise procedures, ineffective independent verification, and inadequate implementation of corrective actions for previously identified problems. NRC and licensee investigations have revealed that the event was initiated as a result of incorrect performance of the process utilized to rack out the feeder breakers from the Unit 1 startup transformer to the Unit 2 engineered safety system buses. The normal practice for racking out a breaker is to ensure the breaker is open, enter the breaker cubicle, and open the knife switch supplying dc power for breaker control. The breaker is then racked out. When the operator went to rack out a breaker, he was confronted with two dc knife switches and opened the wrong switch, thereby removing dc power to the engineered safety system logic circuitry for each bus rather than the dc control power to the breaker. The error was repeated on all four buses. The consequences of the error were as follows: - no automatic transfer capability of engineered safety buses to alternate power sources . IN 84-76 October 19, 1984 Page 3 of 3 - no automatic diesel generator start on loss of bus voltage - no ability to re-energize the buses from an offsite source from the control room - no bus load shedding capability - no degraded grid protection - no breaker overcurrent or differential current protection - no core spray or residual heat removal pump automatic or manual start capability even with power available, hence, disabling the low pressure emergency core cooling systems The investigation further revealed that the knife switch for dc control power to the breaker was labeled "BREAKER CONTROL SWITCH AND TRIP CIRCUIT FUSES" and the one for dc power to the engineered safety system logic circuitry was labeled "DC CONTROL." It was the "DC CONTROL" knife switch that the operator opened, and the error was not detected by the startup engineer assigned to verify the operator actions. During the investigation of the event, it was learned that on two previous occasions during the preoperational testing, the "DC CONTROL" switch was improperly operated. The licensee corrective action following these events was to provide operator training; however, the operator who racked out the breakers for the startup testing had not received that training. Following the event, the licensee initiated immediate and long-term corrective action programs. Immediate actions, which included revising labeling and painting of knife switches and providing training and revising procedures to preclude similar events, were completed prior to the unit restart. The longterm corrective actions include: improvement of the independent verification program; upgrading of existing electrical operating procedures and developing new ones, as required; determination of the adequacy of instrumentation available on loss of ac power; and evaluation of the present design for compliance with Regulatory Guide 1.47, Bypass and Inoperable Status Indication for Nuclear Power Plant Safety Systems. Although the diesel generator problems which occurred during the event added to the complexity of the event, licensee actions to resolve these problems are beyond the scope of this notice. No specific action or written response is required by this information notice. If you have any questions regarding this matter, please contact the Regional Administrator of the appropriate regional office or this office. Edward L. Jordan, Director Division of Emergency Preparedness and Engineering Response Office of Inspection and Enforcement Technical Contact: R. N. Singh, IE (301) 492-8985 Attachment: List of Recently Issued IE Information Notices
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Page Last Reviewed/Updated Tuesday, March 09, 2021