Information Notice No. 84-35: BWR Post-scram Drywell Pressurization
INS No.: 6835
84-35
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF INSPECTION AND ENFORCEMENT
WASHINGTON, D.C. 20555
April 23, 1984
Information Notice No. 84-35: BWR POST-SCRAM DRYWELL PRESSURIZATION
Addressees:
All boiling water power reactor facilities holding an operating license (OL)
or construction permit (CP).
Purpose:
This information notice is provided as a notification of events that
resulted in drywell pressure increases following a reactor scram and the
subsequent unavailability of systems that could be used to reduce drywell
pressure. We expect recipients of this notice will review the information
for applicability to their facilities and consider actions, if appropriate,
to preclude a similar problem occurring at their facilities. However,
suggestions contained in this information notice do not constitute NRC
requirements and, therefore, no specific action or response is required.
Description of Circumstances:
Edwin I. Hatch Plant Unit 2
In August 1982, Hatch Nuclear Plant Unit 2 sustained a reactor scram and
group 1 isolation from full power conditions when an inboard main steam
isolation valve (MSIV) failed closed. After resetting the scram, the opera-
tors controlled vessel level and pressure with the high pressure coolant
injection (HPCI) system and the safety relief valves (SRVs). On opening the
"A" SRV a second time the operators noticed that drywell pressure was in-
creasing rapidly. When the drywell pressure reached 2.0 psig a second
reactor scram and loss of coolant accident (LOCA) signal were initiated. The
scram signal reopened the scram inlet and outlet valves while the LOCA
signal initiated the emergency core cooling system and shut off the drywell
coolers. Drywell pressure continued to rise and peaked at about 4.0 psig.
Some time after the second scram signal was received, it was discovered that
the scram discharge volume (SDV) drain line isolation valve had not fully
closed. With the sustained reactor scram signal, the reactor water continued
to flow out of the open scram valves, through the SDV drain, and into the
reactor building equipment drain (RBED) sump where the hot pressurized
reactor water flashed to steam. The steam then flowed back through open
drains into the reactor building causing a high area temperature trip of the
reactor core isolation cooling (RCIC) system and elevated air temperatures
in other parts of the reactor building.
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IN 84-35
April 23, 1984
Page 2 of 3
The only immediate way of isolating the flow of reactor water through the
scram valves was by resetting the reactor scram signal, which would close
the scram valves. This could not be readily accomplished because the 2.0
psig drywell pressure scram signal was still present. The operator
unsuccessfully attempted to reduce the drywell pressure with the
ventilation, system and decided that personnel would have to restore the
drywell coolers to operation in order to rapidly reduce the drywell
pressure. To accomplish this, an electrical technician had to be sent to the
equipment cabinets to bypass the trip signal for the drywell coolers since
no control room trip override switch was provided on Unit 2. (Such a switch
does exist at Hatch Unit 1).
During this event it took nearly one hour and 45 minutes from the time the
coolers tripped to the time they could be restored. It took nearly another
hour before the coolers reduced the drywell pressure below 2 psig, at which
time the scram could finally be reset and the steam release to the reactor
building terminated.
Quad Cities Station Unit 2
In June 1982, the Unit 2 reactor scrammed from approximately 95 percent
power. The reactor scrammed from a low water level signal following the trip
of a reactor feed pump due to the loss of one of two major 4 kV buses. Prior
to the trip of the turbine generator, and the subsequent loss of the other
major 4 kV bus, the operator ran the vessel level up to the high level trip
point of the feedwater pumps. The operator then controlled reactor pressure
by intermittently opening main steam relief valves. Approximately 30 minutes
after the scram the drywell pressure exceeded 2 psig and a second scram sig-
nal was received along with an emergency core cooling system (ECCS) initia-
tion signal and the trip of the drywell coolers and the reactor building
closed cooling water (RBCCW) pumps.
Both 4 kV buses were returned to service 40 minutes after the trip and sup-
pression pool cooling was established 50 minutes after the trip. The trip
signal to the drywell coolers and RBCCW pumps was bypassed about l hour and
35 minutes after the trip and the drywell pressure was reduced to below 2
psig. Once the drywell pressure was reduced with the drywell coolers, the
second scram signal could be reset.
Discussion:
During the Hatch event it is believed that the high drywell pressure was
caused by the "A" SRV tailpipe vacuum breaker sticking in the open or par-
tially open position (see Information Notice No. 83-26, "Failure of Safe-
ty/Relief Valve Discharge Line Vacuum Breakers"). The high drywell pressure
experienced during the Quad Cities event was apparently caused by leaky gas-
kets on the flanged elbows in the relief valve discharge lines. Such
bypasses or leakage pathways in relief valve piping may reduce the
effectiveness of the pressure suppression system and are of themselves
significant events.
This Information Notice is focussed on the subsequent difficulties in making
equipment available to reduce drywell pressure to normal following leakage
.
IN 84-35
April 23, 1984
Page 3 of 3
from SRV piping. During both events, systems normally used to reduce drywell
pressure were tripped by a high drywell pressure condition and could not be
readily reset. Considerable time was spent before drywell pressure was re-
duced because electrical jumpers had to be installed in order to bypass the
trip signals.
At Hatch Unit 2, no design changes were made to the drywell chiller trip
logic to retain drywell cooling in the presence of a LOCA signal. Instead,
the licensee's corrective action included training of site personnel on
bypassing signals in general along with operator training on the functions
of systems that would allow signals to be bypassed, if needed, on an
emergency basis.
At Quad Cities Unit 2 the high drywell pressure trip logic has since been
modified to allow for continuous operation of the drywell coolers and the
RBCCW pumps when normal power is available to the emergency buses.
A more detailed description of the event and corrective actions taken after
the event at Hatch Unit 2 is discussed in Power Reactor Events, Volume 5,
No. 4, Nuclear Regulatory Commission, January, 1984.
Because of the potential seriousness of this type of event, licensees may
wish to consider design changes to the high drywell pressure logic to
prevent tripping the drywell coolers when offsite power is available, and/or
provide convenient override arrangements (e.g., switches) to permit rapid
restarting of drywell coolers when a high drywell pressure condition still
exists. Before making such design changes, appropriate analyses should be
performed in consultation with NRC.
No written response to this notice is required. If you have any questions
regarding this matter, please contact the Regional Administrator of the
appropriate NRC Regional Office or this office.
Edward L. Jordan, Director
Division of Emergency Preparedness
and Engineering Response
Office of Inspection and Enforcement
Technical Contact: Eric W. Weiss, IE
(301) 492-4973
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