Information Notice No. 83-77: Air/Gas Entrainment Events Resulting in System Failures
SSINS No.: 6835
IN 83-77
UNITED STATES
NUCLEAR REGULATORY COMMISSION
OFFICE OF INSPECTION AND ENFORCEMENT
WASHINGTON, D.C. 20555
November 14, 1983
Information Notice No. 83-77: AIR/GAS ENTRAINMENT EVENTS RESULTING IN
SYSTEM FAILURES
Addressees:
All holders of a nuclear power reactor operating license (OL) or
construction permit (CP).
Purpose:
This information notice is provided as notification of events that rendered
redundant safety systems inoperable because air or gas entrainment caused
pump cavitation. It is expected that recipients will review the information
herein for applicability to their facilities. No specific action or response
is required.
Description of Circumstances:
Calvert Cliffs
On May 20, 1980, Calvert Cliffs Unit 1 sustained a loss of both service
water system (SWS) redundant trains. The SWS became air bound after a
service water heat exchanger (SWHX) was returned to operation, following
routine maintenance.
During the time that the SWHX was not in operation, the heat exchanger
outlet valve was closed and air accumulated on the shell side of the heat
exchanger. The source of air was a failed tube in the instrument air
compressor (IAC) aftercooler. When the SWHX was brought back on line, the
trapped air was swept into the SWS. Shortly thereafter, high temperature
alarms for components cooled by service water (SW) were observed.
Simultaneously, low pressure was also observed in both SW headers and low
amperage was being drawn by the two SW pumps that were running. These
indications signaled that SW pumps were cavitating. The reactor was manually
tripped because of increasing main turbine and feed pump turbine bearing
temperatures. It was subsequently found that the air was swept into the
common inlet header for the SW pumps, causing pump cavitation and disabling
both safety-related subsystems.
Although the SWS is provided with a number of constant vent valves, their
relieving capacity was exceeded by the sudden influx of the large quantity
of air that had accumulated in the SWHX, while it was out of service. After
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IN 83-77
November 14, 1983
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the IAC aftercooler discharge valve was shut, open vents began discharging
solid streams of water and the two SW subsystems were both operating soon
thereafter.
McGuire
On February 12, 1982, McGuire Unit 1 experienced a loss of high head safety
injection emergency boration and reactor coolant makeup capability. Hydrogen
from the positive displacement pump (PDP) suction dampener entered the
common suction of the charging system, causing both centrifugal charging
pumps and the PDP to be inoperable. The system was restored within 30
minutes. The unit was in Mode 1, at 50% of full power at the time. This
event was described in more detail in Information Notice No. 82-19.
San Onofre
During preoperational testing on March 14, 1982 at the San Onofre Nuclear
Generating Station, Unit 2, the shutdown cooling system was inoperable for
90 minutes when the low pressure safety injection (LPSI) pumps became
nitrogen bound. The event resulted from an improper valve alignment during
nitrogen backflushing of a purification filter in the chemical and volume
control system.
Backflushing consists of passing nitrogen gas at 350 psig through the
isolated purification filter and discharging the gas and collected
contaminants into the filter backflush storage tank. In this instance, as a
result of either a system malfunction or operator error, the gaseous
nitrogen passed through the purification line into the suction of the LPSI
pumps which were being used for shutdown cooling. Flow from the operating
LPSI pump fell from 4000 gpm to zero as the pump became gas bound and
attempts to establish flow with this pump or the alternate LPSI pump were
unsuccessful. The pumps and piping high points were vented and shutdown
cooling flow was reestablished.
St. Lucie
On October 23, 1982, with St. Lucie Unit 1 in hot standby during recovery
from a reactor trip, the three operating positive displacement charging
pumps stopped injecting coolant to the reactor coolant system because the
volume control tank (VCT) was pumped dry. The reactor had tripped on a low
steam generator water level signal after a loss of feedwater flow to the
steam generator.
The VCT was empty although its two liquid level sensors indicated an
acceptable liquid inventory and hence an apparently acceptable
inflow/outflow balance from the VCT. The hydrogen cover-gas blanket of the
VCT entered the suction of each pump. The false liquid level indication was
caused by an empty reference leg that was shared by both liquid level
sensors. The pumps were restored to operation by repeated venting after
filling the VCT to a high level.
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IN 83-77
November 14, 1983
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The aforementioned events are intended to be illustrative. Hence, licensees
are cautioned that the types of system inoperability resulting from air or
gas entrainment vary. Moreover, redundant safety-related trains or
components can be affected as shown by the events cited above. The serious
consequences that may result from such system or component impairment cannot
be overemphasized. For example, although the actual consequences of the loss
of shutdown cooling flow at San Onofre-2 were minimal because the event
occurred prior to initial criticality, the event could have been more
serious if the plant had been operating at full power for an extended period
of time prior to the event.
If you have any questions regarding this matter, please contact the Regional
Administrator of the appropriate NRC Regional Office, or this office.
Edward L. Jordan Director
Division of Emergency Preparedness
and Engineering Response
Office of Inspection and Enforcement
Technical Contacts: R. M. Young, IE
49-27275
E. V. Imbro, AEOD
49-24495
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