Part 21 Report - 1995-080
ACCESSION #: 9501230060 LICENSEE EVENT REPORT (LER) FACILITY NAME: Perry Nuclear Power Plant, Unit 1 PAGE: 1 OF 9 DOCKET NUMBER: 05000440 TITLE: Slow Control Rod Scram Insertion Times Result in Technical Specification Violation EVENT DATE: 12/12/94 LER #: 94-023-00 REPORT DATE: 01/11/95 OTHER FACILITIES INVOLVED: N/A DOCKET NO: 05000 OPERATING MODE: 1 POWER LEVEL: 80 THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR SECTION: 50.73(a)(2)(i) LICENSEE CONTACT FOR THIS LER: NAME: Charles R. Elberfeld, Compliance Engineer TELEPHONE: (216) 280-5264 COMPONENT FAILURE DESCRIPTION: CAUSE: X SYSTEM: AA COMPONENT: PSV MANUFACTURER: A610 REPORTABLE NPRDS: Yes SUPPLEMENTAL REPORT EXPECTED: NO ABSTRACT: On December 11, 1994, at 2045, during Technical Specification (TS) Surveillance testing of control rod scram insertion times, TS Limiting Condition for Operation (LCO) 3.1.3.2 ACTION c.1 was entered due to the number of "slow" control rods exceeding twenty percent of a ten percent sample. Enforcement discretion was requested from the NRC and granted. On December 12, 1994, at 0845, the TS LCO ACTION was exceeded when the plant was not placed into HOT SHUTDOWN condition. The cause of this event is attributed to degradation of the batch 314 Viton seating material located in the disk holder sub-assembly used in some of the Scram Solenoid Pilot Valves (SSPVs) replaced during the last refuel outage. The degradation of the seating material causes it to stick to the seating surface after long periods of solenoid energization, resulting in a delay in the valve opening after solenoid de-energization. The delay, in turn, causes the subject control rod to exceed its TS Control Rod Scram Maximum Insertion Time requirement to notch position 43. The SSPVs containing batch 314 Viton seating material were replaced. Perry Nuclear Power Plant, General Electric, and the Automatic Switch Company are working to resolve the SSPV problem. Augmented Control Rod Scram Maximum Insertion Time testing will be performed to provide further confidence in the effectiveness of the corrective actions taken. END OF ABSTRACT TEXT PAGE 2 OF 9 I. Introduction On December 11, 1994, at 2045, during Technical Specification (TS) Surveillance testing of control rod scram insertion times, TS Limiting Condition for Operation (LCO) 3.1.3.2 ACTION c.1 was entered due to the number of "slow" control rods exceeding twenty percent of a ten percent sample of the control rods. This ACTION required the plant to be in at least HOT SHUTDOWN within twelve hours. Enforcement discretion was requested, and granted on December 11, 1994, at 2230, to allow continued testing to identify control rods that may have been subject to degraded insertion times and to provide for timely corrective action for identified rods. The initial duration of the enforcement discretion extended until December 16, 1994, at 2230. On December 12, 1994, at 0845, TS LCO 3.1.3.2 ACTION c.1 was exceeded when the plant was not placed into HOT SHUTDOWN condition. This event is being reported pursuant to 10CFR50.73(a)(2)(i)(B) as operation prohibited by the plant's Technical Specifications. At the time of the event, the plant was in Operational Condition 1 at 80 percent of rated thermal power. The reactor vessel pressure was approximately 1000 psig with reactor coolant at saturated conditions. II. Background Information Grand Gulf Nuclear Power Station Experience Perry Nuclear Power Plant became aware of potential problems with Scram Solenoid Pilot Valves [PSV] (SSPVs) due to difficulties at the Grand Gulf Nuclear Power Station (GGNS). Control rod scram time tests performed at the GGNS in May, 1994 identified that 25 of 191 control rod insertion times to notch position 43 were "slow" (0.320 to 0.390 seconds) and that an additional 8 insertion times failed to meet the TS limits for operable rods (greater than 0.390 seconds). GGNS root cause analysis endorsed a material problem with SSPV seating material located in the disk holder sub-assembly supplied in pre-assembled top head assemblies. The root cause analysis indicated that a problem may exist with seating materials (Viton manufactured post-1991). The failure mechanism is believed to be associated with degradation of the seating material which causes it to "stick" to the seating surface. This results in a delay in venting the air actuators on the inlet and outlet scram valves, and concurrent "slow" control rod scram time to notch position 43. Testing performed by General Electric (GE) indicates a relationship between degradation in SSPV response time and the cumulative solenoid energization time. TEXT PAGE 3 OF 9 Perry Nuclear Power Plant Experience The Perry Nuclear Power Plant (PNPP) SSPVs, Automatic Switch Company (ASCO) Model Number HVA1768161, were replaced during the most recent refuel outage in 1994 (RFO-4). Of the 177 SSPVs installed during the outage, 132 were confirmed to contain Viton batch 314 material which is known to have been manufactured post-1991. Scram time data was obtained during startup from RFO-4 on July 27 and August 2 - 4, 1994. The RFO-4 scram time data indicated that the PNPP control rods met the TS LCO 3/4.1.3.2 for maximum insertion times. However, statistical analysis of the RFO-4 scram time data supported a potential that a failure mechanism could exist which would result in "slow" actuation of SSPVs. An offset (approximately 0.01 second increase) was observed in scram time distribution from historical PNPP scram time data for control rods with certain lots of SSPVs using batch 314 Viton material. Control rods with non-batch 314 SSPVs exhibited a normal distribution. In addition, a relationship was observed between the cumulative energization time of the SSPVs and the scram time in that a statistically significant upward shift in the data mean values was noted at 195 hours energization time. Scram time data from RFO-4 was insufficient to project SSPV response time for longer term solenoid energization. TS Surveillance Requirement 4.1.3-2.c requires control rod scram time testing at least once per 120 days of power operation. This is significantly longer than the maximum energization time (23 days) for which PNPP test data was available. Because scram time offset appeared to change with SSPV energization time, additional testing to monitor this phenomenon, prior to the 120 day surveillance interval, was determined to be prudent. The SSPVs had been energized for 49 days on September 24, 1994. Although not required by TS Surveillance frequency, scram time testing was performed to determine if degradation was occurring in the response time of the PNPP SSPVs. An initial test sample of 20 control rods was selected to provide a statistical confidence level of 95% in SSPV performance. Data from the September 24 and 25, 1994 interim testing as a whole did not indicate degradation in performance of the suspect (Viton batch 314) SSPVs at 49 days of continuous energization. III. Event Description Control rod scram time testing commenced at 09:50 hours on December 10, 1994, in accordance with TS Surveillance Requirement 4.1.3.2.c, which requires control rod scram time testing at least once per 120 days of power operation. This testing consisted of a designated initial test sample of 18 control rods. TEXT PAGE 4 OF 9 On December 11, 1994, at 2045, testing had been completed for 12 of the initial test sample control rods, with the following initial results. - 8 acceptable rods (scram times to notch position 43 met TS 3.1.3.2 LCO), - 4 "slow" rods (scram times to notch position 43 greater than TS 3.1-3.2 LCO, but OPERABLE), - 0 inoperable rods. Results also showed that rods tested met TS 3.1.3.2 LCO times to notch positions 29 and 13. Upon identification of each "slow" rod, testing of adjacent rods began in accordance with TS requirements concurrent with replacement of the affected SSPV prior to additional sample testing. Testing of the adjacent rods identified additional control rods which were "slow" to notch position 43. Subsequent scram time test results for control rods with replaced SSPVs were acceptable. Specific test results were documented in Letter PY-CEI/NRR-1896L, "Request for Enforcement Discretion with Respect to Control Rod Insertion Times," dated December 12, 1994. On December 11, 1994, at 2045, the scram time for test sample rod 12 was identified as exceeding the maximum scram insertion time limits of TS 3.1.3.2. TS LCO 3.1.3.2 ACTION c.1 was entered due to the number of "slow" control rods exceeding 20% of a 10% sample of the control rods, thus requiring the plant to be in at least HOT SHUTDOWN within 12 hours. The plant was therefore required to be placed in HOT SHUTDOWN by December 12, 1994, at 0845. Enforcement discretion with respect to TS 3.1.3.2 LCO ACTIONS c.1, c.3, and c.4 was requested from the NRC and granted on December 11, 1994, at 2330, until December 16, 1994, at 2330, to allow continued scram time testing to identify control rods that may have been subject to degraded scram insertion times to notch position 43, and to provide for timely corrective action for identified rods. Compensatory measures utilized for the duration of the enforcement discretion included: 1) implementation of corrective action to replace SSPVs for all control rods identified as having scram insertion times to notch position 43 exceeding the scram insertion time limits of TS LCO 3.1.3.2, and immediate corrective action implementation for control rods with scram insertion times identified in excess of TS LCO 3.1.3.2 ACTION a.1, 2) reactor power not to exceed 85% rated thermal power, and 3) administrative reduction of the Maximum Fraction of Limiting Critical Power Ratio (MFLCPR) acceptance criteria to 0.990 from 1.00 until repairs were completed on the rods which had been identified as "slow". TEXT PAGE 5 OF 9 On December 15, 1994, scram time testing was completed for the complete core population of 177 control rods with a total of four rods identified as "INOPERABLE" and 26 rods identified as "slow" per Technical Specifications. By that time, the four "INOPERABLE" control rods already had their SSPVs replaced and were restored to OPERABLE status. Corrective actions had been completed for eight of the "slow" control rods; however, additional enforcement discretion time was needed to complete corrective actions on remaining "slow" control rods to exit the HOT SHUTDOWN requirement of TS 3.1.3.2 LCO ACTIONs c.1, c.3, and c.4. On December 16, 1994, an extension of enforcement discretion was requested from the NRC for an additional seven days ending on December 23, 1994, at 2230 or until compliance with the Technical Specifications had been achieved, whichever occurred first. The requested extension and its justification was documented on Letter PY-CEI/NRR-1897L, "Request for Extension of Enforcement Discretion with Respect to Control Rod Insertion Times," dated December 16, 1994. This extension of enforcement discretion was granted on December 16, 1994, at 1515. On December 17, 1994, at 2206, NRC enforcement discretion with respect to TS 3.1.3.2 Control Rod Scram Maximum Insertion Times expired when compliance with Technical Specifications was achieved. IV. Cause of Event The cause of this event is attributed to the degradation, over time of solenoid energization, of the Viton batch 314 seating material located in the disk holder sub-assembly used in some of the Scram Solenoid Pilot Valves replaced during RFO-4. The degradation of the seating material causes it to stick to the seating surface resulting in a delay in the valve opening after solenoid de-energization. The delay, in turn, causes the subject control rod to exceed its TS Control Rod Scram Maximum Insertion Time requirement to notch position 43. GE and ASCO testing as well as PNPP diagnostic testing support this determination. V. Safety Analysis The control rod system is designed to bring the reactor subcritical at a rate fast enough to prevent the Minimum Critical Power Ratio (MCPR) from becoming less than 1.07 during the limiting power transient analyzed in Chapter 15 of the USAR. This USAR analysis shows that the negative reactivity rates resulting from the scram, with the average response of control rod drives as given in the specifications, provide the required protection and MCPR remains greater than 1.07. The occurrence of scram times longer than those specified should be viewed as an indication of a systematic problem with the rod drives. TEXT PAGE 6 OF 9 The Control Rod Drive Hydraulic [AA] (CRDH) system provides the hydraulic driving head for insertion, withdrawal, and scramming of control rods. Each control rod (drive) has a Hydraulic Control Unit (HCU) which provides the scram function. The CRDH system provides water at 1720 psig to the HCU. Each HCU contains a scram accumulator as well as several air operated valves to direct the water pressure to the control rod drive for insertion, withdrawal, and scramming of the control rod under various conditions. The Scram Solenoid Pilot Valve (SSPV) is a dual solenoid operated valve which, when de-energized, vents air from the actuators of both the scram inlet and outlet valves, allowing them to open and provide a flow path for CRDH system and accumulator pressure to scram the control rod. Each of the SSPV dual solenoids is energized from a separate Reactor Protection System bus (A or B) and both of the solenoids must be de-energized for the SSPV to perform its function. The control rod scram is designed to bring the reactor subcritical at a rate fast enough to prevent fuel damage. The accidents/transients that are "scram time sensitive" are those where the scram time can impact on the Minimum Critical Power Ratio (MCPR) or the vessel overpressurization limit. In the current fuel cycle, the limiting event for MCPR is the Load Reject with No By-Pass valve actuation (LRNBP), and for pressurization it is the Main Steamline Isolation Valve (MSIV) fast closure with a neutron flux scram (with no credit for the scram signal from MSIV position). Loss-of-Coolant Accidents do not set MCPR limits nor lead to overpressurization concerns, and other events such as Rod Withdrawal Errors or Rotated Fuel Bundles are not impacted by scram times. Therefore, the examination of the impact of a delayed scram initiation concentrated on two areas: a re-analysis of the limiting scram time sensitive events, and reviews of the assumptions of the original analyses which serve as the basis for the Control Rod Maximum Scram Insertion Time Specification. Re-analyses of the Load Reject with No By-Pass and MSIV Closure events was performed, which assumed the single failure of the highest worth rod to insert, and the remainder of the rods received the Reactor Protection System scram signal with an additional delay of 70 milliseconds from that assumed in the standard analysis. This 70 millisecond time delay corresponds to the time difference (for notch position 43) between the standard analysis assumption and the point at which the rod would be declared "inoperable" by the Technical Specifications. As an example, the standard analysis assumption for the time to notch position 43 at 1050 psig is 320 milliseconds (0.32 seconds), and the rod would be declared inoperable if its scram time exceeded 390 milliseconds (0.39 seconds). If any rod scram times to notch position 43 are measured during scram time testing at up to 70 milliseconds slower than the times assumed in the standard analysis, they are treated by Technical Specifications as "slow" rods, but not inoperable. The TEXT PAGE 7 OF 9 re-analysis assumption of a 70 millisecond delay simulates that every trippable rod in the core is held up by its scram solenoid to the point that they would all be as "slow" as allowed without being declared "inoperable". The results of the analyses of these two limiting events identified that the effects of the scram initiation delay were minimal. For MCPR, the change in Critical Power Ratio during the LRNBP event (the "delta CPR") was examined. In the original reload analysis for Cycle 5 (the current fuel cycle), the delta CPR was 0.15. In the re-analysis, the delta CPR was 0.16, a change of only 0.01 from the base case. The MCPR limit for each fuel bundle type in the PNPP core is determined based on performance of various limiting transients, and for six of the seven fuel bundle types, the current MCPR limits are set by the Rotated Bundle Analysis, which is not scram time sensitive. For the remaining fuel type (the 10 gad rod GE10 fuel), adding the additional 0.01 delta CPR makes the LRNBP the most limiting transient for that fuel type. This has been accounted for by implementing an administrative penalty on the parameter used during power operation to ensure the MCPR limits are met, i.e., the Maximum Fraction of Limiting Critical Power Ratio (MFLCPR). The MFLCPR acceptance criteria was administratively reduced to 0.990 from 1.00 until repairs were completed on the rods which were identified as "slow". Implementing the penalty in this manner applied the 0.01 delta CPR universally across the fuel types, although only the one fuel type was limited by the re-analysis. In practice this had limited impact, since the core was not currently being operated near the limits. The change in peak vessel pressure during the MSIV Closure event was also examined. In the original reload analysis for Cycle 5, the peak pressure was calculated to be 1294 psig, well below the TS 2.1.3 Safety Limit of 1325 psig. In the re-analysis, the peak pressure was calculated to be 1296 psig, also maintaining adequate margin to the 1325 psig limit. Reviews were performed of the assumptions in the original analyses that support TS LCO 3.1.3.2 "Control Rod Maximum Scram Insertion Times". The purpose of these reviews was to determine the significance of any rods which might experience scram times slower than those examined in the re-analysis of the LRNBP event discussed above; i.e., with times more than 70 milliseconds slower than the original analysis values. The Technical Specifications direct that these rods are to be declared inoperable. The analyses that serve as the basis for the ACTIONs of LCO 3.1.3.2 assume that there are as many as nine control rods that are inoperable (one (1) "stuck" and eight (8) inoperable but trippable) in addition to seven (7) more "slow" rods. The eight inoperable rods were assumed to scram slowly enough that they do not contribute to meeting the scram reactivity curve. Although this analysis provides the basis for allowing up to 16 rods to be "slow" (in the above described combination of one stuck, eight "slow" to the point of being inoperable, TEXT PAGE 8 OF 9 and seven more "slow"), the current Technical Specification limits the total number of "slow" (including slow to the point of inoperability) rods in the core at any one time to seven. These seven can, therefore, be any combination of "slow" or inoperable rods, as long as no more than one is a "stuck" rod. This is reflected by ACTIONs a.1, a.3, b, c.2, and c.4. Therefore, during the discretionary enforcement period, from a safety analysis standpoint, there is no significance to rods found to be "slow", since every rod in the core could have been "slow" and the safety parameters of concern would have continued to be met. In addition, the situation where several rods are found to be slow to the point of inoperability is also bounded, from a safety analysis standpoint, in that the existing Technical Specification permits up to seven such rods to exist in the core at any one time. This event is not considered to be safety significant. VI. Similar Events A previous similar event was documented by LER 89-030. On November 25, 1989, the malfunction of two SSPVs due to improper seating material resulted in a violation of Technical Specifications. The causes for the November 1989 event were inadequate implementation of the Nonconformance Control Program and personnel error in the assessment of test results. An event that occurred on October 1, 1990, resulted in the discovery of malfunctioning SSPVs from a single lot installed in the plant during a refueling outage, and resulted in a 10CFR21 notification on December 11, 1990. Another previous similar event was documented by LER 91-018-01. On October 6, 1991, the plant was shut down in accordance with Technical Specifications as a result of two adjacent control rods exceeding maximum insertion scram time limits. The cause of the slow control rods was SSPV failure. A combination of contaminants found on the valve disk and seats was believed to have formed an adhesive which could have bound the valve seat. The suspect SSPVs were from the same lot remanufactured by ASCO in November 1990. The 49 valves from that suspect lot were removed and steps were taken to reduce the potential for introduction of contaminants into the valves. Because none of the previous similar events involved the use of post-1991 batch 314 Viton components within the SSPVs, it is not reasonable to expect that the corrective actions associated with these events could have precluded the December 1994 event. TEXT PAGE 9 OF 9 VII. Corrective Actions The SSPVs containing batch 314 Viton seating material were replaced by December 30, 1994. The replacement valves used were both new valves with post-1991 non-batch-314 Viton seating material and refurbished valves with pre-1991 Viton seating material. PNPP, GE, and ASCO are working to resolve the SSPV problem. Augmented Control Rod Scram Maximum Insertion Time testing will be performed to provide further confidence in the effectiveness of the corrective actions taken. Energy Industry Identification System (EIIS) codes are identified in the text as [XX] ATTACHMENT TO 9501230060 PAGE 1 OF 1 CENTERIOR ENERGY PERRY NUCLEAR POWER PLANT Mail Address: Robert A. Stratman P.O. BOX 97 VICE PRESIDENT - 10 CENTER ROAD PERRY, OHIO 44081 NUCLEAR PERRY, OHIO 44081 (216) 259-3737 January 11, 1995 PY-CEI/NRR-1901L United States Nuclear Regulatory Commission Document Control Desk Washington, D.C. 20555 Perry Nuclear Power Plant Docket No. 50-440 LER 94-023 Gentlemen: Enclosed is Licensee Event Report 94-023 concerning Slow Control Rod Insertion Times Result in Technical Specification Violation. If you have questions or require additional information, please contact Mr. James D. Kloosterman, Manager - Regulatory Affairs at (216) 280-5833. Very truly yours, CRE: sc Enclosure: LER 94-023 cc: NRC Project Manager NRC Resident Inspector Office NRC Region III Operating Companies Cleveland Electric Illuminating Toledo Edison *** END OF DOCUMENT ***
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