Event Notification Report for November 20, 2023
U.S. Nuclear Regulatory Commission
Operations Center
EVENT REPORTS FOR
11/19/2023 - 11/20/2023
Part 21
Event Number: 56764
Rep Org: Flowserve
Licensee: Flowserve
Region: 1
City: Lynchburg State: VA
County:
License #:
Agreement: Y
Docket:
NRC Notified By: Christopher Shaffer
HQ OPS Officer: Lawrence Criscione
Licensee: Flowserve
Region: 1
City: Lynchburg State: VA
County:
License #:
Agreement: Y
Docket:
NRC Notified By: Christopher Shaffer
HQ OPS Officer: Lawrence Criscione
Notification Date: 09/29/2023
Notification Time: 08:36 [ET]
Event Date: 09/29/2023
Event Time: 00:00 [EDT]
Last Update Date: 11/17/2023
Notification Time: 08:36 [ET]
Event Date: 09/29/2023
Event Time: 00:00 [EDT]
Last Update Date: 11/17/2023
Emergency Class: Non Emergency
10 CFR Section:
21.21(a)(2) - Interim Eval Of Deviation
10 CFR Section:
21.21(a)(2) - Interim Eval Of Deviation
Person (Organization):
Lally, Christopher (R1DO)
Miller, Mark (R2DO)
Orlikowski, Robert (R3DO)
Young, Cale (R4DO)
Part 21/50.55 Reactors, - (EMAIL)
Lally, Christopher (R1DO)
Miller, Mark (R2DO)
Orlikowski, Robert (R3DO)
Young, Cale (R4DO)
Part 21/50.55 Reactors, - (EMAIL)
EN Revision Imported Date: 11/20/2023
EN Revision Text: PART 21 INTERIM REPORT - DEVIATION ASSOCIATED WITH AN SMB-1 GEARED LIMIT SWITCH ASSEMBLY
The following information was provided by Flowserve via phone and email:
"The purpose of this letter is to provide written notification of an evaluation of a deviation in a basic component in accordance with 10 CFR21.21(a)(2). This interim report pertains to actuator geared limit switch assemblies contained in SMB-1 actuators supplied to Bopp & Reuther Valves for use in safety related applications at Bruce Nuclear Generating Station.
"Flowserve - Limitorque was contacted by Bruce Power who reported a malfunction of an actuator geared limit switch (GLS) assembly which occurred while attempting to set the valve travel position limits prior to placing the actuator into service. Site inspections of the GLS assembly revealed damage to the GLS drive pinion which engages with the actuator drive train. Site photos and dimensional measurements of the drive pinion requested by Flowserve indicate that the GLS was assembled with an incorrect drive pinion resulting in the malfunction. Use of an incorrect subcomponent in the assembly constitutes the deviation to the design being evaluated. The actuator GLS assembly is a safety related component. A malfunction of the GLS in service has the potential to affect the safety function of the actuator.
"The assembly containing the deviation is a 4-train geared limit switch (GLS) assembly part number 10168 supplied in SMB-1 actuators manufactured on Flowserve order 175377.001 Three actuators (serial numbers L1226986, L1226987, & L1226988) were shipped to Bopp & Reuther Valves on 2/4/2020.
"Flowserve's evaluation of this issue is ongoing and will not be completed within 60 days. The evaluation is expected to be completed by 11/17/2023 pending return of the affected components to Flowserve for inspection. Questions concerning this notification can be directed to Chris Shaffer, Quality Manager."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
This issue was identified at a Canadian reactor plant owned by Bruce Power. The Quality Manager at Flowserve is not currently aware of any affected US reactor plants.
* * * UPDATE ON 11/17/2023 AT 0914 EST FROM CHRISTOPHER SHAFFER TO ERIC SIMPSON * * *
Flowserve Quality Assurance Manager submitted the Final Part 21 Report pertaining to a deviation in a basic component in accordance with 10 CFR 21.21(a)(2). The report concluded that the evaluated deviation constitutes a reportable defect affecting three actuators listed in the final report.
Notified R1DO (Defrancisco), R2DO (Miller), R3DO (Feliz-Adorno), R4DO (Vossmar), and Part 21 Reactors (email).
EN Revision Text: PART 21 INTERIM REPORT - DEVIATION ASSOCIATED WITH AN SMB-1 GEARED LIMIT SWITCH ASSEMBLY
The following information was provided by Flowserve via phone and email:
"The purpose of this letter is to provide written notification of an evaluation of a deviation in a basic component in accordance with 10 CFR21.21(a)(2). This interim report pertains to actuator geared limit switch assemblies contained in SMB-1 actuators supplied to Bopp & Reuther Valves for use in safety related applications at Bruce Nuclear Generating Station.
"Flowserve - Limitorque was contacted by Bruce Power who reported a malfunction of an actuator geared limit switch (GLS) assembly which occurred while attempting to set the valve travel position limits prior to placing the actuator into service. Site inspections of the GLS assembly revealed damage to the GLS drive pinion which engages with the actuator drive train. Site photos and dimensional measurements of the drive pinion requested by Flowserve indicate that the GLS was assembled with an incorrect drive pinion resulting in the malfunction. Use of an incorrect subcomponent in the assembly constitutes the deviation to the design being evaluated. The actuator GLS assembly is a safety related component. A malfunction of the GLS in service has the potential to affect the safety function of the actuator.
"The assembly containing the deviation is a 4-train geared limit switch (GLS) assembly part number 10168 supplied in SMB-1 actuators manufactured on Flowserve order 175377.001 Three actuators (serial numbers L1226986, L1226987, & L1226988) were shipped to Bopp & Reuther Valves on 2/4/2020.
"Flowserve's evaluation of this issue is ongoing and will not be completed within 60 days. The evaluation is expected to be completed by 11/17/2023 pending return of the affected components to Flowserve for inspection. Questions concerning this notification can be directed to Chris Shaffer, Quality Manager."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
This issue was identified at a Canadian reactor plant owned by Bruce Power. The Quality Manager at Flowserve is not currently aware of any affected US reactor plants.
* * * UPDATE ON 11/17/2023 AT 0914 EST FROM CHRISTOPHER SHAFFER TO ERIC SIMPSON * * *
Flowserve Quality Assurance Manager submitted the Final Part 21 Report pertaining to a deviation in a basic component in accordance with 10 CFR 21.21(a)(2). The report concluded that the evaluated deviation constitutes a reportable defect affecting three actuators listed in the final report.
Notified R1DO (Defrancisco), R2DO (Miller), R3DO (Feliz-Adorno), R4DO (Vossmar), and Part 21 Reactors (email).
Agreement State
Event Number: 56847
Rep Org: SC Dept of Health & Env Control
Licensee: Medical University Hospital
Region: 1
City: Charleston State: SC
County:
License #: 081
Agreement: Y
Docket:
NRC Notified By: Korina Koci
HQ OPS Officer: Eric Simpson
Licensee: Medical University Hospital
Region: 1
City: Charleston State: SC
County:
License #: 081
Agreement: Y
Docket:
NRC Notified By: Korina Koci
HQ OPS Officer: Eric Simpson
Notification Date: 11/10/2023
Notification Time: 10:02 [ET]
Event Date: 11/09/2023
Event Time: 17:00 [EST]
Last Update Date: 11/10/2023
Notification Time: 10:02 [ET]
Event Date: 11/09/2023
Event Time: 17:00 [EST]
Last Update Date: 11/10/2023
Emergency Class: Non Emergency
10 CFR Section:
Agreement State
10 CFR Section:
Agreement State
Person (Organization):
Eve, Elise (R1DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
Eve, Elise (R1DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
AGREEMENT STATE REPORT - PATIENT RECEIVED 45 PERCENT UNDERDOSE
The following was received from the South Carolina Department of Health and Environmental Control (Department) via phone and email:
"The South Carolina Department of Health and Environmental Control was notified via telephone at approximately 0930 EST on 11/10/23 that a medical event had been discovered by the licensee on 11/09/23 at approximately 1700 EST. The Medical University of South Carolina (MUSC) reported an underdose to a patient's liver during a Y-90 microsphere procedure by 45 percent of the prescribed 500 Gray (Gy) dose. MUSC estimates that the patient received 276 Gy of the intended 500 Gy dose. The licensee reported that the total dose or activity delivered differs from the prescribed dose or activity, as documented in the written directive, by 20 percent or more.
"The licensee reports no immediate or ongoing concerns to public health and safety. Department inspectors will be dispatched to the facility to investigate this event. This event is still under investigation by the South Carolina Department of Health and Environmental Control."
A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
The following was received from the South Carolina Department of Health and Environmental Control (Department) via phone and email:
"The South Carolina Department of Health and Environmental Control was notified via telephone at approximately 0930 EST on 11/10/23 that a medical event had been discovered by the licensee on 11/09/23 at approximately 1700 EST. The Medical University of South Carolina (MUSC) reported an underdose to a patient's liver during a Y-90 microsphere procedure by 45 percent of the prescribed 500 Gray (Gy) dose. MUSC estimates that the patient received 276 Gy of the intended 500 Gy dose. The licensee reported that the total dose or activity delivered differs from the prescribed dose or activity, as documented in the written directive, by 20 percent or more.
"The licensee reports no immediate or ongoing concerns to public health and safety. Department inspectors will be dispatched to the facility to investigate this event. This event is still under investigation by the South Carolina Department of Health and Environmental Control."
A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
Fuel Cycle Facility
Event Number: 56851
Facility: Framatome ANP Richland
Region: 2 State: WA
Unit: [] [] []
RX Type: Uranium Fuel Fabrication
Comments: Leu Conversion
Fabrication & Scrap Recovery
Commercial Lwr Fuel
NRC Notified By: Calvin Manning
HQ OPS Officer: Ernest West
Region: 2 State: WA
Unit: [] [] []
RX Type: Uranium Fuel Fabrication
Comments: Leu Conversion
Fabrication & Scrap Recovery
Commercial Lwr Fuel
NRC Notified By: Calvin Manning
HQ OPS Officer: Ernest West
Notification Date: 11/13/2023
Notification Time: 15:13 [ET]
Event Date: 11/02/2023
Event Time: 10:45 [PST]
Last Update Date: 11/13/2023
Notification Time: 15:13 [ET]
Event Date: 11/02/2023
Event Time: 10:45 [PST]
Last Update Date: 11/13/2023
Emergency Class: Non Emergency
10 CFR Section:
PART 70 APP A (c) - Offsite Notification/News Rel
10 CFR Section:
PART 70 APP A (c) - Offsite Notification/News Rel
Person (Organization):
Miller, Mark (R2DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
Miller, Mark (R2DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
CONCURRENT REPORT FOR DEGRADED CONNECTOR
The following information was provided by the licensee via phone and email:
"Pursuant to 10 CFR 70 Appendix A (c), Framatome is making this concurrent report:
"On November 2, 2023, Framatome made a courtesy telephone call to the Washington Department of Health (WDOH) about a degraded flexible connector on an exhaust duct downstream of the final HEPA filter.
"On November 3, 2023, WDOH requested that Framatome submit a report within ten days regarding this notification. Framatome will be submitting the requested report today, [November 13, 2023]."
The following information was provided by the licensee via phone and email:
"Pursuant to 10 CFR 70 Appendix A (c), Framatome is making this concurrent report:
"On November 2, 2023, Framatome made a courtesy telephone call to the Washington Department of Health (WDOH) about a degraded flexible connector on an exhaust duct downstream of the final HEPA filter.
"On November 3, 2023, WDOH requested that Framatome submit a report within ten days regarding this notification. Framatome will be submitting the requested report today, [November 13, 2023]."
Power Reactor
Event Number: 56856
Facility: Calvert Cliffs
Region: 1 State: MD
Unit: [2] [] []
RX Type: [1] CE,[2] CE
NRC Notified By: Corey Donahoo
HQ OPS Officer: Adam Koziol
Region: 1 State: MD
Unit: [2] [] []
RX Type: [1] CE,[2] CE
NRC Notified By: Corey Donahoo
HQ OPS Officer: Adam Koziol
Notification Date: 11/16/2023
Notification Time: 05:15 [ET]
Event Date: 11/16/2023
Event Time: 02:27 [EST]
Last Update Date: 11/16/2023
Notification Time: 05:15 [ET]
Event Date: 11/16/2023
Event Time: 02:27 [EST]
Last Update Date: 11/16/2023
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
Defrancisco, Anne (R1DO)
Defrancisco, Anne (R1DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
2 | A/R | Y | 100 | Power Operation | 0 | Hot Standby |
AUTOMATIC REACTOR TRIP
The following information was provided by the licensee via email:
"At 0227 EST on 11/16/23, Calvert Cliffs Unit 2 experienced an automatic trip from the reactor protection system (RPS) based on reactor trip bus undervoltage (UV). At that time, a loss of U-4000-22 (13 kV to 4 kV transformer) caused a loss of 22, 23, and 24 4 kV busses. This resulted in a loss of both motor generator (MG) sets causing the reactor trip bus UV. The loss of 22 and 23 4 kV non-safety related busses resulted in a loss of main feedwater. Auxiliary feedwater (AFW) was manually initiated and is feeding both steam generators. The 2B diesel generator (DG) started and restored the 24 4 kV safety related bus. Heat removal is via the normal turbine bypass valves to the main condenser.
"RPS actuation is reportable under 10 CFR 50.72(b)(2)(iv)(B) - 4 hour report
"ESFAS (engineering safety features actuation system) actuation (2B DG start on UV) is reportable under 10 CFR 50.72(b)(3)(iv)(A) - 8 hour report
"AFW operation is reportable under 10 CFR 50.73(a)(2)(iv)(A) - 60 day report
"The NRC Senior Resident Inspector has been notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
All rods fully inserted. There was no impact on Unit 1 operations. Unit 2 is stable in mode 3.
* * * UPDATE ON AT 0940 EST FROM KERRY HUMMER TO ADAM KOZIOL * * *
"ESFAS actuation (AFW manual initiation) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8 hour report"
Notified R1DO (Defrancisco).
The following information was provided by the licensee via email:
"At 0227 EST on 11/16/23, Calvert Cliffs Unit 2 experienced an automatic trip from the reactor protection system (RPS) based on reactor trip bus undervoltage (UV). At that time, a loss of U-4000-22 (13 kV to 4 kV transformer) caused a loss of 22, 23, and 24 4 kV busses. This resulted in a loss of both motor generator (MG) sets causing the reactor trip bus UV. The loss of 22 and 23 4 kV non-safety related busses resulted in a loss of main feedwater. Auxiliary feedwater (AFW) was manually initiated and is feeding both steam generators. The 2B diesel generator (DG) started and restored the 24 4 kV safety related bus. Heat removal is via the normal turbine bypass valves to the main condenser.
"RPS actuation is reportable under 10 CFR 50.72(b)(2)(iv)(B) - 4 hour report
"ESFAS (engineering safety features actuation system) actuation (2B DG start on UV) is reportable under 10 CFR 50.72(b)(3)(iv)(A) - 8 hour report
"AFW operation is reportable under 10 CFR 50.73(a)(2)(iv)(A) - 60 day report
"The NRC Senior Resident Inspector has been notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
All rods fully inserted. There was no impact on Unit 1 operations. Unit 2 is stable in mode 3.
* * * UPDATE ON AT 0940 EST FROM KERRY HUMMER TO ADAM KOZIOL * * *
"ESFAS actuation (AFW manual initiation) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8 hour report"
Notified R1DO (Defrancisco).
Power Reactor
Event Number: 56858
Facility: Brunswick
Region: 2 State: NC
Unit: [1] [2] []
RX Type: [1] GE-4,[2] GE-4
NRC Notified By: Jason Williamson
HQ OPS Officer: Ian Howard
Region: 2 State: NC
Unit: [1] [2] []
RX Type: [1] GE-4,[2] GE-4
NRC Notified By: Jason Williamson
HQ OPS Officer: Ian Howard
Notification Date: 11/16/2023
Notification Time: 12:12 [ET]
Event Date: 11/16/2023
Event Time: 09:06 [EST]
Last Update Date: 11/16/2023
Notification Time: 12:12 [ET]
Event Date: 11/16/2023
Event Time: 09:06 [EST]
Last Update Date: 11/16/2023
Emergency Class: Non Emergency
10 CFR Section:
26.719 - Fitness For Duty
10 CFR Section:
26.719 - Fitness For Duty
Person (Organization):
Miller, Mark (R2DO)
Miller, Mark (R2DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | N | Y | 100 | Power Operation | 100 | Power Operation |
2 | N | Y | 100 | Power Operation | 100 | Power Operation |
FAILED FITNESS FOR DUTY TEST
The following information was provided by the licensee via phone and email:
"At 0906 Eastern Standard Time (EST) on November 16, 2023, it was determined that a non-licensed employee supervisor failed a test specified by the Fitness for Duty (FFD) testing program. The individual's authorization for site access has been removed.
"The NRC Resident Inspector has been notified."
The following information was provided by the licensee via phone and email:
"At 0906 Eastern Standard Time (EST) on November 16, 2023, it was determined that a non-licensed employee supervisor failed a test specified by the Fitness for Duty (FFD) testing program. The individual's authorization for site access has been removed.
"The NRC Resident Inspector has been notified."
Power Reactor
Event Number: 56861
Facility: South Texas
Region: 4 State: TX
Unit: [2] [] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Neil Rocha
HQ OPS Officer: Ian Howard
Region: 4 State: TX
Unit: [2] [] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Neil Rocha
HQ OPS Officer: Ian Howard
Notification Date: 11/16/2023
Notification Time: 21:30 [ET]
Event Date: 11/16/2023
Event Time: 15:41 [CST]
Last Update Date: 11/16/2023
Notification Time: 21:30 [ET]
Event Date: 11/16/2023
Event Time: 15:41 [CST]
Last Update Date: 11/16/2023
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
Person (Organization):
Vossmar, Patricia (R4DO)
Vossmar, Patricia (R4DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
2 | N | Y | 100 | Power Operation | 100 | Power Operation |
ESSENTIAL CHILLER TRAINS INOPERABLE
The following information was provided by the licensee via phone and email:
"11/05/23, 2200 CST: Essential Chiller 'B' train and associated cascading equipment were declared INOPERABLE for planned maintenance. Unit 2 entered the Configuration Risk Management Program as required by Technical Specifications on 11/12/23 at 2200.
"11/16/23, 1541: Essential Chiller 'C' train and associated cascading equipment were declared INOPERABLE due to an unexpected material condition causing the Essential Chiller to trip. The most limiting [Limiting Condition of Operability] LCO is 3.7.7, Action c.
"This condition resulted in the INOPERABILITY of two of the three safety trains required for the accident mitigating function including: High Head Safety Injection, Low Head Safety Injection, Containment Spray, Electrical Auxiliary Building HVAC, Control Room Envelope HVAC, Essential Chilled Water.
"This is an 8 hour reportable condition per 10CFR50.72(b)(3)(v)(D) because it could affect the ability to mitigate the consequences of an accident.
"A risk analysis was performed for the equipment INOPERABILITY and mitigating actions have been taken per site procedures. All 'A' train equipment remains operable."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The 'B' train Emergency Diesel Generator was also inoperable due to planned maintenance and continues to be inoperable. It was considered in the Configuration Risk Management Program and it was determined this condition could be maintained. LCO 3.7.7, Action c requires reactor shutdown within 72 hours.
The following information was provided by the licensee via phone and email:
"11/05/23, 2200 CST: Essential Chiller 'B' train and associated cascading equipment were declared INOPERABLE for planned maintenance. Unit 2 entered the Configuration Risk Management Program as required by Technical Specifications on 11/12/23 at 2200.
"11/16/23, 1541: Essential Chiller 'C' train and associated cascading equipment were declared INOPERABLE due to an unexpected material condition causing the Essential Chiller to trip. The most limiting [Limiting Condition of Operability] LCO is 3.7.7, Action c.
"This condition resulted in the INOPERABILITY of two of the three safety trains required for the accident mitigating function including: High Head Safety Injection, Low Head Safety Injection, Containment Spray, Electrical Auxiliary Building HVAC, Control Room Envelope HVAC, Essential Chilled Water.
"This is an 8 hour reportable condition per 10CFR50.72(b)(3)(v)(D) because it could affect the ability to mitigate the consequences of an accident.
"A risk analysis was performed for the equipment INOPERABILITY and mitigating actions have been taken per site procedures. All 'A' train equipment remains operable."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The 'B' train Emergency Diesel Generator was also inoperable due to planned maintenance and continues to be inoperable. It was considered in the Configuration Risk Management Program and it was determined this condition could be maintained. LCO 3.7.7, Action c requires reactor shutdown within 72 hours.
Power Reactor
Event Number: 56863
Facility: River Bend
Region: 4 State: LA
Unit: [1] [] []
RX Type: [1] GE-6
NRC Notified By: Jason Shidaker
HQ OPS Officer: Sam Colvard
Region: 4 State: LA
Unit: [1] [] []
RX Type: [1] GE-6
NRC Notified By: Jason Shidaker
HQ OPS Officer: Sam Colvard
Notification Date: 11/18/2023
Notification Time: 02:51 [ET]
Event Date: 11/17/2023
Event Time: 23:55 [CST]
Last Update Date: 11/18/2023
Notification Time: 02:51 [ET]
Event Date: 11/17/2023
Event Time: 23:55 [CST]
Last Update Date: 11/18/2023
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
Vossmar, Patricia (R4DO)
Vossmar, Patricia (R4DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | M/R | Y | 24 | Power Operation | 0 | Hot Shutdown |
MANUAL REACTOR SCRAM
The following information was provided by the licensee via phone and email:
"On November 17, 2023, at 2215 CST, River Bend Station (RBS) was operating at 30 percent reactor power performing plant startup activities when an isolation of low-pressure feedwater string `A' occurred. The team entered applicable alternate operating procedures and inserted control rods to exit the restricted region of the power to flow map. Feedwater temperature continued to lower until it challenged the prohibited region of the AOP-0007 graph requiring a reactor scram. The team inserted a manual reactor scram at 2355 from 24 percent reactor power. All control rods fully inserted and there were no complications. All systems responded as designed. Currently RBS Unit 1 is stable with reactor level being maintained 10 to 51 inches with feed and condensate, and pressure being maintained 500 to 1090 psig using steam drains.
"This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the Reactor Protection System (RPS) when the reactor is critical and 10 CFR 50.72(b)(3)(iv)(A) Specified System Actuation as result of Group 3 isolations.
"The NRC Senior Resident inspector has been notified.
"No radiological releases have occurred due to this event from the unit."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The electric plant is in a normal lineup for current plant conditions with all emergency diesel generators available. The cause of the initial isolation of low-pressure feedwater string "A" is still under investigation.
The following information was provided by the licensee via phone and email:
"On November 17, 2023, at 2215 CST, River Bend Station (RBS) was operating at 30 percent reactor power performing plant startup activities when an isolation of low-pressure feedwater string `A' occurred. The team entered applicable alternate operating procedures and inserted control rods to exit the restricted region of the power to flow map. Feedwater temperature continued to lower until it challenged the prohibited region of the AOP-0007 graph requiring a reactor scram. The team inserted a manual reactor scram at 2355 from 24 percent reactor power. All control rods fully inserted and there were no complications. All systems responded as designed. Currently RBS Unit 1 is stable with reactor level being maintained 10 to 51 inches with feed and condensate, and pressure being maintained 500 to 1090 psig using steam drains.
"This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the Reactor Protection System (RPS) when the reactor is critical and 10 CFR 50.72(b)(3)(iv)(A) Specified System Actuation as result of Group 3 isolations.
"The NRC Senior Resident inspector has been notified.
"No radiological releases have occurred due to this event from the unit."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The electric plant is in a normal lineup for current plant conditions with all emergency diesel generators available. The cause of the initial isolation of low-pressure feedwater string "A" is still under investigation.
Power Reactor
Event Number: 56864
Facility: Harris
Region: 2 State: NC
Unit: [1] [] []
RX Type: [1] W-3-LP
NRC Notified By: Scott Faulkner
HQ OPS Officer: Sam Colvard
Region: 2 State: NC
Unit: [1] [] []
RX Type: [1] W-3-LP
NRC Notified By: Scott Faulkner
HQ OPS Officer: Sam Colvard
Notification Date: 11/19/2023
Notification Time: 00:53 [ET]
Event Date: 11/18/2023
Event Time: 21:38 [EST]
Last Update Date: 11/19/2023
Notification Time: 00:53 [ET]
Event Date: 11/18/2023
Event Time: 21:38 [EST]
Last Update Date: 11/19/2023
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(xi) - Offsite Notification
10 CFR Section:
50.72(b)(2)(xi) - Offsite Notification
Person (Organization):
Miller, Mark (R2DO)
Miller, Mark (R2DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | N | Y | 100 | Power Operation | 100 | Power Operation |
OFFSITE NOTIFICATION - REPORT TO ANOTHER GOVERNMENT AGENCY
The following information was provided by the licensee via phone and email:
"At 2138 EST on November 18, 2023, Harris Nuclear Plant notified the National Response Center of a biodegradable oil leak that entered the Harris Lake. The North Carolina Department of Environmental Quality will also be notified of this condition on November 19, 2023. The oil leak was less than one gallon and came from a temporary pump. The leak has stopped, and spill cleanup is underway. This condition did not violate any NRC regulations or reporting criteria. This notification is being made solely as a four-hour, non-emergency notification for a notification to another government agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi).
"There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."
The following information was provided by the licensee via phone and email:
"At 2138 EST on November 18, 2023, Harris Nuclear Plant notified the National Response Center of a biodegradable oil leak that entered the Harris Lake. The North Carolina Department of Environmental Quality will also be notified of this condition on November 19, 2023. The oil leak was less than one gallon and came from a temporary pump. The leak has stopped, and spill cleanup is underway. This condition did not violate any NRC regulations or reporting criteria. This notification is being made solely as a four-hour, non-emergency notification for a notification to another government agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi).
"There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."
Power Reactor
Event Number: 56865
Facility: Quad Cities
Region: 3 State: IL
Unit: [1] [2] []
RX Type: [1] GE-3,[2] GE-3
NRC Notified By: Harrison Grimm
HQ OPS Officer: John Russell
Region: 3 State: IL
Unit: [1] [2] []
RX Type: [1] GE-3,[2] GE-3
NRC Notified By: Harrison Grimm
HQ OPS Officer: John Russell
Notification Date: 11/19/2023
Notification Time: 14:44 [ET]
Event Date: 11/18/2023
Event Time: 20:20 [CST]
Last Update Date: 11/19/2023
Notification Time: 14:44 [ET]
Event Date: 11/18/2023
Event Time: 20:20 [CST]
Last Update Date: 11/19/2023
Emergency Class: Non Emergency
10 CFR Section:
26.719 - Fitness For Duty
10 CFR Section:
26.719 - Fitness For Duty
Person (Organization):
Feliz-Adorno, Nestor (R3DO)
FFD Group, (EMAIL)
Feliz-Adorno, Nestor (R3DO)
FFD Group, (EMAIL)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | N | Y | 100 | Power Operation | 100 | Power Operation |
2 | N | Y | 100 | Power Operation | 100 | Power Operation |
FITNESS FOR DUTY REPORT
The following information was provided by the licensee via phone and fax:
"On November 18, 2023, the presence of alcohol was discovered inside the protected area. In accordance with the Constellation Fitness For Duty (FFD) Program, the individual has been escorted offsite and access to the plant denied pending the results of an investigation.
"This event is being reported under 10 CFR 26.719(b)(1) as it represents a significant FFD violation.
"The NRC Resident Inspector has been notified."
The following information was provided by the licensee via phone and fax:
"On November 18, 2023, the presence of alcohol was discovered inside the protected area. In accordance with the Constellation Fitness For Duty (FFD) Program, the individual has been escorted offsite and access to the plant denied pending the results of an investigation.
"This event is being reported under 10 CFR 26.719(b)(1) as it represents a significant FFD violation.
"The NRC Resident Inspector has been notified."
Agreement State
Event Number: 56853
Rep Org: Florida Bureau of Radiation Control
Licensee: Moffitt Cancer Center
Region: 1
City: Tampa State: FL
County:
License #: 1739-1
Agreement: Y
Docket:
NRC Notified By: Paul Norman
HQ OPS Officer: Ernest West
Licensee: Moffitt Cancer Center
Region: 1
City: Tampa State: FL
County:
License #: 1739-1
Agreement: Y
Docket:
NRC Notified By: Paul Norman
HQ OPS Officer: Ernest West
Notification Date: 11/14/2023
Notification Time: 16:54 [ET]
Event Date: 11/14/2023
Event Time: 12:11 [EST]
Last Update Date: 11/14/2023
Notification Time: 16:54 [ET]
Event Date: 11/14/2023
Event Time: 12:11 [EST]
Last Update Date: 11/14/2023
Emergency Class: Non Emergency
10 CFR Section:
Agreement State
10 CFR Section:
Agreement State
Person (Organization):
Defrancisco, Anne (R1DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
Defrancisco, Anne (R1DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
DOSE GREATER THAN PRESCRIBED
The following information was provided by the Florida Department of Health via email:
"On 11/14/2023, a patient arrived in the nuclear medicine department for administration of their fourth cycle of Lutathera, a Lu-177 labeled radiopharmaceutical. The standard prescription of Lutathera for patients is 200 mCi in accordance with manufacturer's instructions for use and industry standard. The technologist assayed the vial and went through pre-administration procedures including a pre-treatment time out. 202 mCi of Lutathera was administered via IV in the right upper forearm over the course of thirty minutes. Start time of 1211 [EST] with an end time of 1241.
"Upon completion of the procedure, the technologist noticed that the patient had been prescribed a reduced activity of 150 mCi as opposed to the standard prescription of 200 mCi. Realizing this was a medical event, the technologist notified the radiation safety officer (RSO) at approximately 1330. The technologist also informed the nuclear medicine department supervisor. The RSO proceeded to inform the Authorized User (AU)/prescribing physician.
"The AU spoke with the patient explaining that the activity administered exceeded the prescribed amount. The physician explained that he did not expect any adverse effects from the higher than prescribed activity as the patient had received the standard activity of 200 mCi. The reduced activity of 150 mCi had been decided by the prescribing physician due to borderline renal function and the patient had tolerated all previous three administrations. Since the patient's renal function was not affected by the three previous administrations, the prescribing physician explained that the patient could have received the 200 mCi. The patient did not express concern upon being informed of this event.
"The AU also informed the referring physician.
"An initial report was made to [Florida] via telephone at 1529 in accordance with 64E-5.345(4)(a)."
Florida Incident Number: FL23-164
A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
The following information was provided by the Florida Department of Health via email:
"On 11/14/2023, a patient arrived in the nuclear medicine department for administration of their fourth cycle of Lutathera, a Lu-177 labeled radiopharmaceutical. The standard prescription of Lutathera for patients is 200 mCi in accordance with manufacturer's instructions for use and industry standard. The technologist assayed the vial and went through pre-administration procedures including a pre-treatment time out. 202 mCi of Lutathera was administered via IV in the right upper forearm over the course of thirty minutes. Start time of 1211 [EST] with an end time of 1241.
"Upon completion of the procedure, the technologist noticed that the patient had been prescribed a reduced activity of 150 mCi as opposed to the standard prescription of 200 mCi. Realizing this was a medical event, the technologist notified the radiation safety officer (RSO) at approximately 1330. The technologist also informed the nuclear medicine department supervisor. The RSO proceeded to inform the Authorized User (AU)/prescribing physician.
"The AU spoke with the patient explaining that the activity administered exceeded the prescribed amount. The physician explained that he did not expect any adverse effects from the higher than prescribed activity as the patient had received the standard activity of 200 mCi. The reduced activity of 150 mCi had been decided by the prescribing physician due to borderline renal function and the patient had tolerated all previous three administrations. Since the patient's renal function was not affected by the three previous administrations, the prescribing physician explained that the patient could have received the 200 mCi. The patient did not express concern upon being informed of this event.
"The AU also informed the referring physician.
"An initial report was made to [Florida] via telephone at 1529 in accordance with 64E-5.345(4)(a)."
Florida Incident Number: FL23-164
A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
Power Reactor
Event Number: 56866
Facility: Dresden
Region: 3 State: IL
Unit: [2] [] []
RX Type: [2] GE-3,[3] GE-3
NRC Notified By: Edward Burns
HQ OPS Officer: Ernest West
Region: 3 State: IL
Unit: [2] [] []
RX Type: [2] GE-3,[3] GE-3
NRC Notified By: Edward Burns
HQ OPS Officer: Ernest West
Notification Date: 11/20/2023
Notification Time: 17:53 [ET]
Event Date: 11/20/2023
Event Time: 09:56 [CST]
Last Update Date: 11/20/2023
Notification Time: 17:53 [ET]
Event Date: 11/20/2023
Event Time: 09:56 [CST]
Last Update Date: 11/20/2023
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
Person (Organization):
Feliz-Adorno, Nestor (R3DO)
Feliz-Adorno, Nestor (R3DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
2 | N | Y | 100 | Power Operation | 100 | Power Operation |
HPCI DECLARED INOPERABLE
The following information was provided by the licensee via email:
"At 0956 [CST] on November 20, 2023, accumulated gas was identified in the Dresden Unit 2 high pressure coolant injection (HPCI) system discharge header. As a result, the HPCI system was declared inoperable. Since HPCI is a single-train system, this is a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The HPCI system was subsequently vented, and the accumulated gas has been removed, restoring the Dresden Unit 2 HPCI system to an operable status. All other emergency core cooling systems remained operable during this time period.
"There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The licensee administratively verified the isolation condenser was operable after declaring HPCI inoperable as required by technical specifications. The licensee stated there was no increase in plant risk. The cause of gas accumulating in the Dresden Unit 2 HPCI discharge header is under investigation, and this issue has been entered into the licensee's corrective action program.
The following information was provided by the licensee via email:
"At 0956 [CST] on November 20, 2023, accumulated gas was identified in the Dresden Unit 2 high pressure coolant injection (HPCI) system discharge header. As a result, the HPCI system was declared inoperable. Since HPCI is a single-train system, this is a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The HPCI system was subsequently vented, and the accumulated gas has been removed, restoring the Dresden Unit 2 HPCI system to an operable status. All other emergency core cooling systems remained operable during this time period.
"There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The licensee administratively verified the isolation condenser was operable after declaring HPCI inoperable as required by technical specifications. The licensee stated there was no increase in plant risk. The cause of gas accumulating in the Dresden Unit 2 HPCI discharge header is under investigation, and this issue has been entered into the licensee's corrective action program.