U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/27/2018 - 11/28/2018 ** EVENT NUMBERS ** |
Fuel Cycle Facility | Event Number: 53744 | Facility: GLOBAL NUCLEAR FUEL - AMERICAS RX Type: URANIUM FUEL FABRICATION Comments: LEU CONVERSION (UF6 TO UO2) LEU FABRICATION LWR COMMERICAL FUEL Region: 2 City: WILMINGTON State: NC County: NEW HANOVER License #: SNM-1097 Docket: 07001113 NRC Notified By: SCOTT MURRAY HQ OPS Officer: OSSY FONT | Notification Date: 11/19/2018 Notification Time: 13:59 [ET] Event Date: 11/17/2018 Event Time: 00:00 [EST] Last Update Date: 11/19/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 70.50(b)(1) - UNPLANNED CONTAMINATION | Person (Organization): SHANE SANDAL (R2DO) NMSS_EVENTS_NOTIFICATION (EMAIL) GRETCHEN RIVERA-CAPELLA (NMSS EO) | Event Text UNPLANNED CONTAMINATION DUE TO KILN SEAL LEAK
"On 11/17/2018, at approximately 1445 EST, it was discovered that the Fuel Manufacturing Operation (FMO) Dry Conversion Line 1 kiln seal began to leak and caused an alarm on the Hydrogen Fluoride (HF) room detection system. This manufacturing process equipment is within an established FMO contamination-controlled area which is designed to contain and control this type of release. The area was not occupied at the time, there were no personnel exposures or releases from the area and the affected process was shut-down.
"As a precautionary measure consistent with current NRC radiation protection requirements, an appropriate, additional radiological control was imposed by requiring respiratory protection for entry into the room to keep personnel exposures as low as reasonably achievable until the area could be decontaminated in a safe and timely manner. Although the affected equipment remains shutdown, this additional radiological control remained in place for more than 24 hours.
"NRC Fuel Cycle Safety and Safeguards staff recently clarified its position for this type of reportability determination in a letter sent to the Nuclear Energy Institute dated October 5, 2018. Because of this letter, this event is conservatively being reported pursuant to the requirements of 10 CFR 70.50 (b)(1)."
The NRC region will be notified. Additionally, the North Carolina Radiation Protection Commission and New Hanover County Emergency Management will also be notified. |
Fuel Cycle Facility | Event Number: 53746 | Facility: WESTINGHOUSE ELECTRIC CORPORATION RX Type: URANIUM FUEL FABRICATION Comments: LEU CONVERSION (UF6 to UO2) COMMERCIAL LWR FUEL Region: 2 City: COLUMBIA State: SC County: RICHLAND License #: SNM-1107 Docket: 07001151 NRC Notified By: GERARD COUTURE HQ OPS Officer: ANDREW WAUGH | Notification Date: 11/20/2018 Notification Time: 11:15 [ET] Event Date: 11/19/2018 Event Time: 00:00 [EST] Last Update Date: 11/20/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 70.50(b)(3) - MED TREAT INVOLVING CONTAM PART 70 APP A (c) - OFFSITE NOTIFICATION/NEWS REL | Person (Organization): SHANE SANDAL (R2DO) EDWARD HARVEY (NMSS DAY) FUELS GROUP (EMAIL) GRETCHEN RIVERA-CAPELLA (NMSS EO) | Event Text CONTAMINATED WORKER REQUIRING MEDICAL TREATMENT
"On November 19, 2018, at approximately 1130 [EST], a conversion area worker was cleaning up a spill of liquid uranyl fluoride (UO2F2) that can contain hydrofluoric acid (HF). During the cleanup effort, some amount of this solution was able to come in contact with the worker's clothing potentially impacting their skin on the legs above the ankle. Appropriate treatment for exposure to HF was provided by onsite medical response staff. When the operator attempted to exit the chemical side of the plant, radioactive material contamination was detected on both hands. The contamination on both hands was above free release criteria and was unable to be removed by normal decontamination methods. The worker was transported to an offsite medical facility accompanied by plant health physics personnel. The worker was sent to the hospital for observation due to the potential chemical exposure.
"The Columbia plant is a licensed Part 70 facility subject to 10 CFR 70 Subpart H. Spills within the conversion area of the plant are evaluated in the Integrated Safety Analysis and Summary. This issue does not challenge the performance requirements of 10 CFR 70.61.
"Operations staff finished cleaning up the spill. At the time of this notification, the employee reported to management that they are awaiting discharge from the hospital. This issue has been entered into the facility's corrective action program.
"24-Hour Event Notification based on 10 CFR 70.50(b)(3), 'An event that requires unplanned medical treatment at a medical facility of an individual with spreadable radioactive contamination on the individual's clothing or body.' Also applicable to this issue is a 24-Hour Event Notification based on 10 CFR 70 Appendix A(c), 'Any event or situation, related to the health and safety of the public or onsite personnel, or protection of the environment, for which a news release is planned or notification to other government agencies has been or will be made, shall be reported to the NRC Operations Center concurrent to the news release or other notification.' This issue requires notification to the South Carolina (SC) Department of labor, Division of Occupational Safety and Health."
The licensee has notified NRC Region 2. |
Agreement State | Event Number: 53747 | Rep Org: TEXAS DEPT OF STATE HEALTH SERVICES Licensee: TEXAS A&M UNIVERSITY Region: 4 City: COLLEGE STATION State: TX County: License #: Agreement: Y Docket: NRC Notified By: IRENE CASARES HQ OPS Officer: JEFFREY WHITED | Notification Date: 11/20/2018 Notification Time: 15:26 [ET] Event Date: 11/08/2018 Event Time: 00:00 [CST] Last Update Date: 11/20/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): GREG WERNER (R4DO) NMSS_EVENTS_NOTIFICATION (EMAIL) | This material event contains a "Less than Cat 3" level of radioactive material. | Event Text AGREEMENT STATE REPORT - LIQUID SCINTILLATION COUNTER SENT TO RECYCLING CENTER
The following information was received via e-mail from the State of Texas:
"On November 20, 2018, the licensee reported that a Liquid Scintillation Counter (LSC) (LKB -WALLAC 1410), potentially containing an internal source and also H-3/C-14 standards, was surplused on November 8, 2018. Surplus staff informed that the unit had gone to metal recycling. On November 19, 2018, radiation safety retrieved broken glass standards (approx. 100,000 dpm each vial, November 1987) from metal recycling [Madison Metals in Bryan TX]. This particular model WALLAC 1410 was known to contain approximately 12 microCi Eu-152. The activity currently could be as low as 2.45 microCi. Neither the source nor shielding was found. A contamination survey was completed with probes and the wipes were counted in an LSC, and nothing was found over background. The metal recycling center is closed for the holidays and no one is expected to receive an exposure. More information will be forwarded once it is received. The investigation is ongoing."
Texas Incident Number: I-9639
THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL
Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf |
Agreement State | Event Number: 53748 | Rep Org: FLORIDA BUREAU OF RADIATION CONTROL Licensee: THE HEART AND VASCULAR CLINIC, LLC. Region: 1 City: WEST PALM BEACH State: FL County: License #: 4000-1 Agreement: Y Docket: NRC Notified By: MATTHEW SENISON HQ OPS Officer: JEFFREY WHITED | Notification Date: 11/20/2018 Notification Time: 16:04 [ET] Event Date: 11/16/2018 Event Time: 00:00 [EST] Last Update Date: 11/20/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): RAY POWELL (R1DO) NMSS_EVENTS_NOTIFICATION (EMAIL) | Event Text AGREEMENT STATE REPORT - MISADMINISTRATION OF SODIUM PERTECHNETATE
The following information was received via e-mail from the State of Florida:
"On Friday, November 16, 2018, [the licensee] called to report a medical event involving licensee 4000-1. A patient was administered 150 milliCi of Sodium Pertechnetate that was originally intended to be used to calibrate a machine. The critical organ dose was less than 50 rem; the effective dose was 7 rem."
A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient. |
!!!!! THIS EVENT HAS BEEN RETRACTED.THIS EVENT HAS BEEN RETRACTED !!!!! | Power Reactor | Event Number: 53756 | Facility: RIVER BEND Region: 4 State: LA Unit: [1] [] [] RX Type: [1] GE-6 NRC Notified By: T. W. GATES HQ OPS Officer: THOMAS KENDZIA | Notification Date: 11/28/2018 Notification Time: 05:40 [ET] Event Date: 11/27/2018 Event Time: 00:00 [CST] Last Update Date: 12/03/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(C) - POT UNCNTRL RAD REL | Person (Organization): JASON KOZAL (R4DO) | Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 99 | Power Operation | 99 | Power Operation | Event Text INOPERABILITY OF EQUIPMENT FOR CONTROL OF RADIOLOGICAL RELEASE
"At 2130 CST on 11/27/2018, Division 1 Main Steam Positive Leakage Control System (MS-PLCS) was declared inoperable because of a leaking check valve that caused excessive cycling of the associated air compressor.
"Division 2 MS-PLCS had been declared inoperable on 11/27/2018 at 1400 CST when a pressure control valve in the system exceeded the maximum allowable stroke time.
"Because MS-PLCS supplements the isolation function of the main steam isolation valves (MSIVs) by processing fission products that could leak through the closed MSIVs, both divisions of MS-PLCS inoperable at the same time represents a condition that could prevent the fulfillment of a safety function of an SSC [Structures, Systems and Components] that is needed to control the release of radioactive material.
"The station diesel air compressor is available to supply backup air to the safety relief valves as required by the Technical Requirements Manual." [This is associated with operability of the safety relief valves, due to the inoperable MS-PLCS air compressor.]
The unit is in a 7 day shutdown Limiting Condition for Operation (LCO), 1-TS1-18-Div 1 & 2 MSPLCS-685, for the two divisions of MS-PLCS being inoperable.
The licensee notified the NRC Resident Inspector.
* * * RETRACTION ON 12/03/18 AT 1551 EST FROM TIM GATES TO BETHANY CECERE * * *
"This event was initially reported under 10 CFR 50.72(b)(3)(v)(C) as a condition that could have prevented the Main Steam Positive Leakage Control System (MS-PLCS) from fulfilling its safety function to control the release of radioactive material. Division I was declared inoperable due to a failed component. Division II was declared inoperable due to a pressure control valve in the system exceeding the maximum allowable time to close by 0.50 seconds. An engineering evaluation has since been performed and concluded that the 2 second maximum allowable time to close was based on the pressure control valve being classified as a rapid closure valve and was established from the original baseline data of 0.50 seconds. This baseline data is an administrative target value per the In-Service Testing Program. There are no technical specification requirements associated with the 2 second closure time.
"The engineering evaluation also determined that the volume of air supplied through the pressure control valve during the extra 0.50 seconds of valve closure would have an inconsequential effect on the pressure within the volume of leakage barrier between the Main Steam Isolation Valves associated with the MS-PLCS pressure control valve or have any effect on containment over-pressurization.
"Based on the information provided by the engineering evaluation, the Division II MS-PLCS has been declared operable-degraded non-conforming since time of initial discovery. Consequently, this event is not reportable as a condition that could have prevented the Main Steam Positive Leakage Control System (MS-PLCS) from fulfilling its safety function.
"The [NRC] Resident Inspector has been notified via e-mail."
Notified the R4DO (Gaddy). |
Power Reactor | Event Number: 53757 | Facility: PRAIRIE ISLAND Region: 3 State: MN Unit: [1] [2] [] RX Type: [1] W-2-LP,[2] W-2-LP NRC Notified By: JEFF HUMAN HQ OPS Officer: KARL DIEDERICH | Notification Date: 11/28/2018 Notification Time: 12:30 [ET] Event Date: 11/28/2018 Event Time: 00:00 [CST] Last Update Date: 11/28/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(xi) - OFFSITE NOTIFICATION | Person (Organization): BILLY DICKSON (R3DO) | Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text OFFSITE NOTIFICATION DUE TO INADVERTENT SIREN ACTIVATION
"At 0752 CST, on November 28, 2018, Dakota County inadvertently actuated their sirens while performing a scheduled weekly [Emergency Planning Fixed Siren Test]. All seven (7) Dakota County sirens actuated for approximately 9 seconds before Dakota County Dispatch canceled the activation. This 4-hour non-emergency report is being made per 10 CFR 50.72(b)(2)(xi), Offsite Notification [which was made to Dakota County Dispatch]. Capability to notify the public was never degraded during this time. All Emergency Notification sirens remain in service. No press release is planned at this time."
The licensee has notified the NRC Resident Inspector. |
Power Reactor | Event Number: 53759 | Facility: CALLAWAY Region: 4 State: MO Unit: [1] [] [] RX Type: [1] W-4-LP NRC Notified By: BRANDON LONG HQ OPS Officer: KARL DIEDERICH | Notification Date: 11/28/2018 Notification Time: 17:25 [ET] Event Date: 11/28/2018 Event Time: 00:00 [CST] Last Update Date: 11/28/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(B) - POT RHR INOP 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): JASON KOZAL (R4DO) | Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text DISCOVERY OF A CONDITION THAT COULD HAVE PREVENTED FULFILLMENT OF A SAFETY FUNCTION
"On November 28, 2018, while performing an engineering review of the bases for environmental qualification (EQ) requirements for the Atmospheric Steam Dumps (ASDs), it was determined that applicable EQ requirements had not been applied to a key component of each of the ASDs. The result of this issue is that it the availability of the ASDs for a controlled plant cooldown following a postulated steam line break outside containment cannot be assured.
"Callaway is developing a compensatory action temporary plant modification to install insulation that will protect the affected ASD components from the post Main Steam Line Break temperature.
"This condition is reportable 10 CFR 50.72(b)(3)(v) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to (B) remove residual heat, or (D) mitigate the consequences of an accident."
The issue places the plant in a 24-hour Technical Specification (TS) Limiting Condition for Operations (LCO), 3.7.4.
The licensee has notified the NRC Resident Inspector. | |