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Event Notification Report for April 18, 2005

U.S. Nuclear Regulatory Commission
Operations Center

Event Reports For
04/15/2005 - 04/18/2005

** EVENT NUMBERS **


41591 41596 41601 41602 41604 41605 41606 41607

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General Information or Other Event Number: 41591
Rep Org: MA RADIATION CONTROL PROGRAM
Licensee: AEA TECHNOLOGY QSA
Region: 1
City: BURLINGTON State: MA
County:
License #: 12-8361
Agreement: Y
Docket:
NRC Notified By: ROBERT GALLAGHER
HQ OPS Officer: CHAUNCEY GOULD
Notification Date: 04/12/2005
Notification Time: 09:35 [ET]
Event Date: 04/08/2005
Event Time: 17:30 [EST]
Last Update Date: 04/12/2005
Emergency Class: NON EMERGENCY
10 CFR Section:
AGREEMENT STATE
Person (Organization):
JOHN WHITE (R1)
MELVYN LEACH (NMSS)
RICHARD BORRI (NYC)
ED BAILEY/RAD CONT (CA)
RUSSELL TAKATA/ RAD (HI)
REBECCA NEASE (R4)
UNDINE SHOOP (EDO)

Event Text

TWO AMERICIUM-241 SOURCES BEING SHIPPED TO AUSTRALIA WERE REPORTED POTENTIALLY LOST

Report # MA050006

"AEA Technology QSA Inc is reporting a potentially lost radioactive material shipment. The shipment contains two Type A packages each containing a 1 Ci AmBe source US model number AMN. PE2. The source serial numbers are 1865NN and 1858NN.

"The sources were shipped from AEA Technology on 30 Mar 05 and were designated to leave on a flight to Australia on 2 Apr 05 with arrival scheduled on 5 Apr 2005. AEA was notified on 7 Apr 05 that the shipment had not arrived. The shipment was sent to Surtech Systems Pty Ltd, in Wangara Perth, WA 6055 Australia.

"Indication from the airline (Qantas) in New York (JFK) that the packages were on the plane, however the airline in Perth cannot confirm that [they] have the packages.

"Discussions with the carrier and freight forwarders indicate that they have so far been unsuccessful in locating the packages. A conference call is currently being arranged between all parties to try and locate the packages."

The sources were finally found today (04/12/04) at a Qantas airlines facility in Melbourne, Australia.

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General Information or Other Event Number: 41596
Rep Org: ARIZONA RADIATION REGULATORY AGENCY
Licensee: JERRY HURACEK
Region: 4
City: PHOENIX State: AZ
County:
License #: AZ 7-496
Agreement: Y
Docket:
NRC Notified By: AUBREY GODWIN
HQ OPS Officer: JEFF ROTTON
Notification Date: 04/13/2005
Notification Time: 18:25 [ET]
Event Date: 04/13/2005
Event Time: 11:00 [MST]
Last Update Date: 04/13/2005
Emergency Class: NON EMERGENCY
10 CFR Section:
AGREEMENT STATE
Person (Organization):
REBECCA NEASE (R4)
SCOTT FLANDERS (NMSS)
CNSNS (FAX)
AARON DANIS (TAS)

Event Text

AGREEMENT STATE - STOLEN TROXLER MOISTURE DENSITY GAUGE

The following information was provided via email from the State of Arizona (State text in quotes):

"At approximately 11:00 AM April 13, 2005, the Agency was informed that the Licensee had a pickup truck stolen with a Troxler Model 3401B gauge, SN 10444. The theft occurred between 7:00 PM, 4/12/2005 and 4:00 AM, 4/13/2005. The truck is a green 1995 Nissan. The Troxler gauge was locked in a 16 gauge steel box with a hardened and anti-theft designed lock and hasp. The steel box is bolted to the frame of the truck. The truck license number is Arizona [DELETED]. The gauge contains 8 mCi of Cesium-137 and 40 mCi Am:Be-241.

"Phoenix PD is investigating and has issued report number 2005-50689301.

"The Licensee is offering a $500.00 reward for the recovery of the truck and sources. A press release is to be made.

"The Agency continues to look for the source.

"The states of CA, NV, CO, UT, and NM and Mexico and U.S. NRC and FBI are being notified of this event."

Arizona State Report ID: 05-03

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Power Reactor Event Number: 41601
Facility: COOPER
Region: 4 State: NE
Unit: [1] [ ] [ ]
RX Type: [1] GE-4
NRC Notified By: STEVEN JOBE
HQ OPS Officer: PETE SNYDER
Notification Date: 04/15/2005
Notification Time: 09:26 [ET]
Event Date: 04/15/2005
Event Time: 04:36 [CDT]
Last Update Date: 04/15/2005
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(A) - ECCS INJECTION
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION
50.72(b)(3)(v)(D) - ACCIDENT MITIGATION
Person (Organization):
REBECCA NEASE (R4)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
1 A/R Y 100 Power Operation 0 Hot Shutdown

Event Text

REACTOR SCRAM AND SPECIFIED SYSTEM ACTUATIONS

"This is both a four hour and eight hour report for the following event:

"4 hour Non-Emergency for ECCS Discharge to the RCS and RPS Actuation;

"8 hour Non-Emergency for Groups 2 & 6. Also, HPCI [High Pressure Coolant Injection] was placed in pull-to-lock, thereby making HPCI unavailable.

"At 0436 [hrs.] CDT 04/15/2005, Cooper Nuclear Station experienced a reactor feed water level transient followed by reactor vessel water level low level alarm and an automatic scram. HPCI and RCIC [Reactor Core Isolation Cooling] automatically initiated and injected into the reactor vessel. Groups 2, 3, and 6 actuated on low reactor water level. Both reactor recirculation pumps tripped and RWCU [Reactor Water Clean-Up system] isolated. Reactor vessel water level reached approximately [minus] 70 inches (instrument zero, approximately 90 inches of water remained above the fuel) and recovered after HPCI and RCIC had begun to inject. All post-scram automatic actions were as expected. HPCI was placed in pull-to-lock to prevent over feeding. The plant is being cooled down to establish natural circulation flow and permit recovery of recirculation pumps.

"Investigation into the cause of the reactor feed water level transient is ongoing."

All rods inserted during the scram. No safety relief valves lifted during the transient. All group isolation signals have been reset. The electrical grid is stable. Decay heat is being removed via steam dumps to the main condenser.

The licensee has notified the NRC Resident Inspector.

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Power Reactor Event Number: 41602
Facility: WOLF CREEK
Region: 4 State: KS
Unit: [1] [ ] [ ]
RX Type: [1] W-4-LP
NRC Notified By: KEN PETERSEN
HQ OPS Officer: PETE SNYDER
Notification Date: 04/15/2005
Notification Time: 10:02 [ET]
Event Date: 04/15/2005
Event Time: 05:17 [CDT]
Last Update Date: 04/15/2005
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(ii)(A) - DEGRADED CONDITION
Person (Organization):
REBECCA NEASE (R4)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N N 0 Refueling 0 Refueling

Event Text

STEAM GENERATOR BOWL DRAIN LINE WELD LEAK DISCOVERED DURING VISUAL EXAM

"During the performance of Alloy 600 bare metal visual examinations, the presence of boric acid deposits indicated a leak in a weld in the steam generator D (EBB01D) bowl drain line.

"This condition is being reported as a degraded condition on the primary coolant system under 10 CFR 50.72 (B)(3)(ii)(A).

"During investigation the defect was characterized as a 1/16" rounded indication in the drain line to boss weld.

"This condition cannot be found acceptable under ASME Section XI, IWB-3600, 'Analytical Evaluation of Flaws' or ASME Section XI, Table IWB-3410-1, 'Acceptable Standards.'

"The [NRC] Resident Inspector has been notified."

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Power Reactor Event Number: 41604
Facility: DUANE ARNOLD
Region: 3 State: IA
Unit: [1] [ ] [ ]
RX Type: [1] GE-4
NRC Notified By: DAN KELLEY
HQ OPS Officer: MIKE RIPLEY
Notification Date: 04/15/2005
Notification Time: 14:09 [ET]
Event Date: 04/15/2005
Event Time: 08:30 [CST]
Last Update Date: 04/15/2005
Emergency Class: NON EMERGENCY
10 CFR Section:
26.73 - FITNESS FOR DUTY
Person (Organization):
JOHN MADERA (R3)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N N 0 Refueling 0 Refueling

Event Text

FITNESS FOR DUTY

A contract supervisor tested positive for alcohol during a for-cause fitness for duty test. The individual's access to the plant was terminated. The licensee notified the NRC Resident Inspector. Contact the Headquarters Operations Officer for additional details.

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Power Reactor Event Number: 41605
Facility: KEWAUNEE
Region: 3 State: WI
Unit: [1] [ ] [ ]
RX Type: [1] W-2-LP
NRC Notified By: DAVID KARST
HQ OPS Officer: MIKE RIPLEY
Notification Date: 04/15/2005
Notification Time: 16:32 [ET]
Event Date: 04/15/2005
Event Time: 07:35 [CST]
Last Update Date: 04/15/2005
Emergency Class: NON EMERGENCY
10 CFR Section:
26.73 - FITNESS FOR DUTY
Person (Organization):
JOHN MADERA (R3)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N N 0 Refueling Shutdown 0 Refueling Shutdown

Event Text

FITNESS FOR DUTY

A non-licensed employee supervisor tested positive for alcohol during a for-cause fitness for duty test. The employee's access to the plant has been terminated. The licensee notified the NRC Resident Inspector. Contact the Headquarters Operations Officer for additional details.

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Power Reactor Event Number: 41606
Facility: PRAIRIE ISLAND
Region: 3 State: MN
Unit: [ ] [2] [ ]
RX Type: [1] W-2-LP,[2] W-2-LP
NRC Notified By: JEFF HUMAN
HQ OPS Officer: MIKE RIPLEY
Notification Date: 04/15/2005
Notification Time: 22:33 [ET]
Event Date: 04/15/2005
Event Time: 21:30 [CDT]
Last Update Date: 04/15/2005
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(i) - PLANT S/D REQD BY TS
Person (Organization):
JOHN MADERA (R3)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
2 N Y 100 Power Operation 96 Power Operation

Event Text

PLANT SHUTDOWN REQUIRED BY TECHNICAL SPECIFICATIONS - INOPERABLE EMERGENCY DIESEL GENERATOR

"Unit 2 Train A emergency diesel generator D5 was removed from service at 0838 CDT on 4/11/05 for surveillance testing and Technical Specification (TS) 3.8.1, 'AC Source - Operating,' Condition B, 'One DG inoperable,' was entered. TS Required Action 3.8.1.B.4 requires D5 be restored to operable status with a Completion Time of 7 days. At 1026 CDT, the test was halted due to high-indicated crankcase pressure on Engine 2 (D5 is a tandem engine generator). The test procedure specifies shutting down the DG if crankcase pressure exceeds 30 mm for more than a few minutes (the setpoint for the crankcase pressure trip is 52 mm).

"Investigation of the cause of the high-indicated crankcase pressure on Engine 2 (and whether Engine 1 was effected) started immediately. Unit 2 Train B emergency diesel generator was demonstrated operable by completing a surveillance test at 0423 CDT on 4/12/05. Evaluation of the scope of work to return D5 to operable status and the schedule for completing the work indicated that repairs could not be completed within the 7 days allowed outage time. Based on this assessment an orderly shutdown of Unit 2 is being performed.

"Shutdown of Unit 2 commenced at 21:30 CDT on 4/15/05. Unit 2 shutdown will continue until D5 is restored to operable status."

The licensee intends to issue a press release. The licensee notified the NRC Resident Inspector.

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Power Reactor Event Number: 41607
Facility: MILLSTONE
Region: 1 State: CT
Unit: [ ] [ ] [3]
RX Type: [1] GE-3,[2] CE,[3] W-4-LP
NRC Notified By: MICHAEL GOBELI
HQ OPS Officer: JOHN KNOKE
Notification Date: 04/17/2005
Notification Time: 09:23 [ET]
Event Date: 04/17/2005
Event Time: 08:42 [EDT]
Last Update Date: 04/17/2005
Emergency Class: ALERT
10 CFR Section:
50.72(a) (1) (i) - EMERGENCY DECLARED
50.72(b)(2)(iv)(A) - ECCS INJECTION
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION
Person (Organization):
SAM COLLINS (RA)
TIM MCGINTY (IRD)
JIM DYER (ET)
R1 BLAST DIAL ()
E. BRENNER (PAO)
THOMAS (NRC)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
3 A/R Y 100 Power Operation 0 Hot Standby

Event Text

ALERT DECLARED DUE TO UNIT 3 MAIN STEAM RELIEF VALVES NOT RESEATING AFTER ACTUATION

At 09:23 the licensee indicated that several Main Steam Relief Valves lifted and stayed open. A high pressure flow signal from the secondary Steam Generator caused initiation of Unit 3 Safety Injection, which in turn caused the Reactor to trip. All rods fully inserted as required. Activation of the Safety Injection subsequently caused the Pressurizer level to go solid. About 30 minutes into the event the primary Reactor Coolant and Main Steam Systems stabilized, including the Pressurizer level and pressure. During the initial briefing, about 09:35, the licensee reported that all secondary Safety Relief Valves have reseated. Decay heat is being directed to the Atmospheric Dumps due to the Main Condenser not being available. The licensee is attempting to establish ERDS.

Initial assessment of this incident is believed not to be security related, however, follow-up is being conducted to verify same. At 09:48, NRC management made a decision to enter into Monitoring Mode. At about 11:15 the licensee indicated that a valve in the Charging System indicated some leakage, therefore it was isolated. Licensee stated that no radiological releases and no S/G tube leakage was indicated.

Licensee notified State and local emergency response agencies. They will notify the NRC Resident Inspector.

Notified DHS (Doyle), FEMA (Biscue), DOE (Smith), USDA (Magners), and HHS (Hogan).

* * * UPDATE FROM D. DODSON TO W. GOTT 1328 EDT 04/17/05 * * *

"At approximately 0830 on April 17, 2005 Millstone Unit 3 experienced an automatic reactor trip from full power. The Reactor is in a stable shutdown condition and is proceeding to Mode 5 cold shutdown. No release of radioactivity other than those minor releases associated with normal plant operation has occurred. There were no personnel injuries associated with the event.

"In addition to the Reactor Trip, half-train Safety Injection (SI) and half-train Main Steam Isolation (MSI) actuations occurred. Control room personnel were successful at manually initiating full SI and MSI. SI has since been terminated and RCS pressure control has been restored. Multiple steam line safety valves (MSSV) lifted with at least one MSSV indicating a failure to reclose. As a result, an ALERT was declared at approximately 0853 due to the failure of at least one MSSV failing to reclose. All MSSVs are currently closed. Auxiliary Feedwater (AFW) actuated automatically as expected, however, the turbine driven auxiliary feedwater pump (TDAFWP) tripped on start-up and was subsequently reset locally. Both motor driven auxiliary feedwater pumps (MDAFWPs) operated as expected to maintain steam generator water levels. Due to the additional inventory injected to the Reactor Coolant System (RCS) as a result of the SI actuation, the pressurizer filled and a primary system safety valve (PSSV) actuated at a lower than expected pressure. All PSSVs are currently closed, however, there is indication of leakage past either a PSSV or Pilot Operated Relief Valve (PORV). Upon alignment of the Charging system to Refueling Water Storage Tank recirculation flow path, 2 valves had indication of packing leakage. Those packing leaks have been terminated.

"The cause of the event is under investigation."

The licensee has issued a press release. The licensee will notify the NRC Resident Inspector.
Notified R1 DO (J. White) and IRD Manager (T. McGinty)

* * * UPDATE FROM D. DODSON TO W. GOTT AT 1915 ON 04/17/05 * * *

"The previously reported time of the Alert declaration should be corrected to read 08:42. Millstone Unit 3 entered Mode 4 [Hot Shutdown] at approximately 19:03 on April 17, 2005. The event at Millstone Unit 3 was terminated at 19:05. The cause of the event is under investigation. A recovery plan is being formulated."

Internal NRC notifications, DHS (Frost), NRC/EPA (Threatt), FEMA (Erwin), DOE (Morone), USDA (Smeltzer), HHS (Desi)

The licensee will notify the NRC Resident Inspector.

At 23:45 the Agency exited Monitoring Mode and entered into Normal Mode.

Page Last Reviewed/Updated Wednesday, March 24, 2021