U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/10/2004 - 06/11/2004 ** EVENT NUMBERS ** | General Information or Other | Event Number: 40794 | Rep Org: COLORADO DEPT OF HEALTH Licensee: TERRACON Region: 4 City: FORT COLLINS State: CO County: License #: Agreement: Y Docket: NRC Notified By: JAMES S. JARVIS HQ OPS Officer: MIKE RIPLEY | Notification Date: 06/07/2004 Notification Time: 13:28 [ET] Event Date: 06/05/2004 Event Time: 11:00 [MDT] Last Update Date: 06/07/2004 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): JACK WHITTEN (R4) TOM ESSIG (NMSS) | Event Text COLORADO AGREEMENT STATE REPORT - DAMAGED MOISTURE DENSITY GAUGE The following information was received by facsimile: "At approximately 11 am on 6/5/04, a watering truck on a housing development construction project near Fort Collins, Colorado (County Roads 11, and 52), ran over a Troxler moisture density gauge (Troxler model 3430; Serial # 28846) owned by Terracon (Colorado Specific License #664-02). The gauge was being used for soil compaction measurements but was in the safe (up) position when it was run over. The technician responsible for using the gauge was reported to be in close proximity to the gauge at the time of the incident but may have had the gauge to his right and not in direct frontal view. As a result of the incident, the index rod was knocked off and the source rod above the unit casing was bent at a 90 degree angle but remained attached to the unit. The gauge casing was described to be mostly intact (i.e. not fully crushed) with the exception of damage to the display. Discussions with the RSO indicated that the gauge source was believed to have remained within the internal shielding following the incident. "The RSO for Terracon reported to the scene at approximately 11:50 am (6/5/04) and performed initial radiation measurements of the gauge. The initial radiation measurements on scene indicated values of approximately 1.0. millirem/hour on/near the surface of the gauge and 0.2 [millirem/hr] at 1 meter. The gauge was placed in the transport case and returned to the Terracon main offices located at 301 North Howes, Fort Collins, CO, 80521. The damaged gauge (in the case) was placed in an outbuilding located near the main office and was secured and the area posted per the RSO. The Department mandated that a leak test be performed prior to shipment of the gauge to a repair facility - results are pending. "Based upon the nature of the incident and the position of the source and rod as, described by the RSO, the source is believed to be intact with no release to the environment or personnel or public exposure. A written report from the licensee is expected within 30 days." | General Information or Other | Event Number: 40796 | Rep Org: ARIZONA RADIATION REGULATORY AGENCY Licensee: WALTER O. BOSWELL HOSPITAL Region: 4 City: SUN CITY WEST State: AZ County: License #: AZ-07-138 Agreement: Y Docket: NRC Notified By: AUBREY GODWIN HQ OPS Officer: CHAUNCEY GOULD | Notification Date: 06/08/2004 Notification Time: 12:33 [ET] Event Date: 06/04/2004 Event Time: 13:00 [MST] Last Update Date: 06/08/2004 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): CHUCK CAIN (R4) LINDA PSYK (NMSS) | Event Text ARIZONA STATE LICENSEE REPORTED A MISSING I-125 SEED The State of Arizona has been informed of a missing source by two State Licensees (Walter O. Boswell Hospital lic # AZ-07-138 and Amersham Health lic # AZ-07-346). The missing source is an Iodine-125 seed containing 0.225 millicuries of Iodine-125. The seed was loaded into a shipping container by two employees of Licensee 1. Both employees independently described and certified the loading of the seed into the shipping container. Licensee 2 received the package but did not locate the seed that was supposed to be inside. This is information from the 30 day report, pursuant to Arizona rules equivalent to 10CFR20.2201(a)(ii). The seed was first detected missing April, 18, 2004. The Agency has opened an active investigation into the circumstances of the loss of this seed. Initial surveys at each Licensee failed to locate the missing seed. | Power Reactor | Event Number: 40802 | Facility: BRUNSWICK Region: 2 State: NC Unit: [1] [2] [ ] RX Type: [1] GE-4,[2] GE-4 NRC Notified By: TOM HACKLER HQ OPS Officer: JOHN MacKINNON | Notification Date: 06/10/2004 Notification Time: 05:36 [ET] Event Date: 06/10/2004 Event Time: 02:05 [EDT] Last Update Date: 06/10/2004 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(xi) - OFFSITE NOTIFICATION | Person (Organization): MARK LESSER (R2) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | 2 | N | Y | 96 | Power Operation | 96 | Power Operation | Event Text OFFSITE NOTIFICATION MADE DUE TO INADVERTENT EMERGENCY SIREN ACTUATION "One emergency response siren (Number 10 Brunswick County) located in Southport, NC inadvertently actuated at 0205, apparently due to a lightning strike, and was silenced at 0312. The Brunswick County, New Hanover County and North Carolina State Emergency Operation Centers (EOC) were notified of the inadvertent actuation. The Brunswick County 911 Center received calls from local residents reporting the siren actuation. "Initial Safety Significance Evaluation: Minimal safety significance. The loss of the single siren will not significantly impact the public notification system. The remaining sirens in both Brunswick and New Hanover Counties have been verified to be operable. "Corrective Actions: The siren was silenced at 0312 on June 10, 2004. The cause of the inadvertent actuation will be determined and repaired." The NRC Resident Inspector was notified of this event by the licensee. | Power Reactor | Event Number: 40804 | Facility: NORTH ANNA Region: 2 State: VA Unit: [ ] [2] [ ] RX Type: [1] W-3-LP,[2] W-3-LP NRC Notified By: BRAD BROWN HQ OPS Officer: ARLON COSTA | Notification Date: 06/10/2004 Notification Time: 16:11 [ET] Event Date: 06/10/2004 Event Time: 13:13 [EDT] Last Update Date: 06/10/2004 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): MARK LESSER (R2) BILL BATEMAN (NRR) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | A/R | Y | 100 | Power Operation | 0 | Hot Standby | Event Text AUTOMATIC REACTOR TRIP WHILE PERFORMING SCHEDULED SOLID STATE PROTECTION TESTING A Unit 2 automatic reactor trip occurred while the licensee was performing planned periodic testing on train "A" solid state protection. All control rods fully inserted into the reactor core. The Auxiliary Feedwater Pumps automatically started as expected immediately following the reactor trip due to low-low level in the steam generators. The unit is being maintained stable in mode 3 and heat sink is being performed via steam dump to the condensers. All other systems functioned as required. The cause of the reactor trip is under investigation. The licensee notified the NRC Resident Inspector. | Fuel Cycle Facility | Event Number: 40805 | Facility: PADUCAH GASEOUS DIFFUSION PLANT RX Type: URANIUM ENRICHMENT FACILITY Comments: 2 DEMOCRACY CENTER 6903 ROCKLEDGE DRIVE BETHESDA, MD 20817 (301)564-3200 Region: 2 City: PADUCAH State: KY County: McCRACKEN License #: GDP-1 Agreement: Y Docket: 0707001 NRC Notified By: CALVIN PITTMAN HQ OPS Officer: GERRY WAIG | Notification Date: 06/10/2004 Notification Time: 16:37 [ET] Event Date: 04/23/2004 Event Time: 05:53 [CDT] Last Update Date: 06/10/2004 | Emergency Class: NON EMERGENCY 10 CFR Section: RESPONSE-BULLETIN | Person (Organization): MARK LESSER (R2) JOHN GREEVES (NMSS) | Event Text PADUCAH GASEOUS DIFfUSSION PLANT - RESPONSE BULLETIN 91-01 24 - HOUR REPORT "At 1550 on 6-09-04, the Plant Shift Superintendent was notified of a failure of a Safety Related Item (SRI) relied upon in Nuclear Criticality Safety Evaluation (NCSE) 052 'Enrichment Cascade During Normal Operations at the Paducah Gaseous Diffusion Plant.' At 0553 hours on 4-23-04, when responding to alarms on Cell 6 in Building C-310, the second bank of motors could not be shut down using the manual motor trip system. Operators opened the Transformer Secondary Breaker (TSB) as an alternate means to shut down the motors. The manual motor trip system is credited to mitigate/minimize the consequences or extent of a Hot Metal Reaction (HMR). "PGDP Problem Report No, ATRC-04-2299; PGDP Event Report No. PAD-2004-17; Event Worksheet [NRC Event Number]: # 40805, Responsible Division: Operations. "SAFETY SIGNIFICANCE OF EVENTS: Minimal. There are multiple methods capable of shutting down equipment suspected of undergoing a HMR. The compressor motors were shut down using one of these methods. The shutdown was accomplished within 2 minutes. "POTENTIAL CRITICALITY PATHWAYS INVOLVED (BRIEF SCENARIOS) OF HOW CRITICALITY COULD OCCUR: In order for a criticality to occur, the equipment would have had to be involved In the initiating event of a HMR. There were no indications of a HMR. Additionally, the HMR event would need to have occurred with a significant inventory of UF6 present. The event was in the purge cascade having UF6 concentrations in the ppm range. Therefore, there is no credible pathway to criticality for this incident. "CONTROLLED PARAMETERS (MASS, MODERATION. GEOMETRY, CONCENTRATION, ETC): This scenario is singly contingent based on moderation control. ESTIMATED AMOUNT, ENRICHMENT, FORM OF LICENSED MATERIAL (INCLUDE PROCESS LIMIT AND % WORST CASE CRITICAL MASS): The event was in the purge cascade having UF6 concentrations in the ppm range at an enrichment of less than [DELETED] wt % 235U. "NUCLEAR CRITICALITY SAFETY CONTROL(S) OR CONTROL SYSTEM(S) AND DESCRIPTION OF THE FAILURES OR DEFICIENCIES: This scenario is singly contingent based on moderation control. The scenario indicates that it is unlikely for a significant HMR to occur resulting in a cooler/cascade breach with subsequent sprinkler activation based on historical operations. The manual motor trip system is credited to mitigate/minimize the consequences or extent of a HMR. The credited trip failed to perform its intended function. Although the credited trip failed, alternative methods were used to shutdown the cell, thereby satisfying the intent of the administrative portion of the control. Also, no HMR, cell breach, or sprinkler activation occurred. Although the SRI failed, the moderation parameter was maintained. "CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS IMPLEMENTED: The cell was shut down using alternate means within 2 minutes. The manual motor trip system was declared inoperable at 0700 on 4-23-04 and repaired. "The NRC Resident Inspector has been notified of this event." | |