The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for April 14, 2003








                    U.S. Nuclear Regulatory Commission

                              Operations Center



                              Event Reports For

                           04/11/2003 - 04/14/2003



                              ** EVENT NUMBERS **



39749  39750  39751  39752  39753  39754  



+------------------------------------------------------------------------------+

|Power Reactor                                    |Event Number:   39749       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| FACILITY: CLINTON                  REGION:  3  |NOTIFICATION DATE: 04/11/2003|

|    UNIT:  [1] [] []                 STATE:  IL |NOTIFICATION TIME: 06:23[EDT]|

|   RXTYPE: [1] GE-6                             |EVENT DATE:        04/11/2003|

+------------------------------------------------+EVENT TIME:        01:45[CDT]|

| NRC NOTIFIED BY:  PAT RYAN                     |LAST UPDATE DATE:  04/11/2003|

|  HQ OPS OFFICER:  ARLON COSTA                  +-----------------------------+

+------------------------------------------------+PERSON          ORGANIZATION |

|EMERGENCY CLASS:          NON EMERGENCY         |MICHAEL PARKER       R3      |

|10 CFR SECTION:                                 |                             |

|ARPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|1     M/R        Y       30       Power Operation  |0        Hot Shutdown     |

|                                                   |                          |

|                                                   |                          |

+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| MANUAL REACTOR TRIP DUE TO VIBRATIONS ON THE MAIN TURBINE                    |

|                                                                              |

| "A manual scram was initiated at 0145 on April 11, 2003, due to vibrations   |

| on the Main Turbine trending up to the trip setpoint.  A scheduled plant     |

| shutdown was in progress for a maintenance outage [of the 'B' recirculation  |

| flow control valve sensor].  All plant systems operated normally on the      |

| scram.  The plant is shutdown at 0% power in Mode 3.  The turbine vibrations |

| returned to normal values after the turbine tripped."                        |

|                                                                              |

| All rods inserted normally.  All safety and electrical systems operated as   |

| designed during and after the reactor trip.  The plant is stable and using   |

| normal feedwater.  There was nothing unusual or not understood.              |

|                                                                              |

| The NRC Resident Inspector has been notified.                                |

+------------------------------------------------------------------------------+



+------------------------------------------------------------------------------+

|Power Reactor                                    |Event Number:   39750       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| FACILITY: DAVIS BESSE              REGION:  3  |NOTIFICATION DATE: 04/11/2003|

|    UNIT:  [1] [] []                 STATE:  OH |NOTIFICATION TIME: 17:17[EDT]|

|   RXTYPE: [1] B&W-R-LP                         |EVENT DATE:        04/11/2003|

+------------------------------------------------+EVENT TIME:        17:00[EDT]|

| NRC NOTIFIED BY:  LARRY MYERS                  |LAST UPDATE DATE:  04/11/2003|

|  HQ OPS OFFICER:  MIKE RIPLEY                  +-----------------------------+

+------------------------------------------------+PERSON          ORGANIZATION |

|EMERGENCY CLASS:          NON EMERGENCY         |MICHAEL PARKER       R3      |

|10 CFR SECTION:                                 |GENE IMBRO           NRR     |

|AUNA 50.72(b)(3)(ii)(B)  UNANALYZED CONDITION   |                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |

|                                                   |                          |

|                                                   |                          |

+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| UNANALYZED CONDITION COULD CAUSE HIGH PRESSURE INJECTION PUMP DAMAGE         |

|                                                                              |

| "As a result of an in-depth design and performance capability review, a      |

| non-conforming condition was identified whereby, utilizing only safety grade |

| equipment, long term cyclic repressurizations of the reactor coolant system  |

| (RCS) may occur following a subset of postulated very small Loss of Coolant  |

| Accidents (LOCAs) with effective break sizes in a range between 0.0021 ft2   |

| to 0.0045 ft2.  The repressurization cycles were not previously analyzed,    |

| but are predicted by a new application of the license basis 10 CFR 50.46     |

| Evaluation Model.  Although non-safety grade equipment would be available to |

| prevent repressurizatons, if only safety grade LOCA mitigating equipment is  |

| credited, these repressurizazion cycles could be postulated to damage both   |

| High Pressure Injection (HPI) pumps.  This could occur due to pump           |

| deadheading after HPI recirculation flow back to the borated water storage   |

| tank is procedurally isolated upon tank low level and pump suction has been  |

| manually transferred to the containment emergency sump at minimum of         |

| approximately 20 hours into the postulated event.  Minimum recirculation     |

| flow back to the borated water storage tank initially provided protection    |

| against deadheading the pump and previously assumed reactor coolant system   |

| pressures would have allowed continued HPI pump flow.  During part of the    |

| newly predicted repressurization cycle, RCS pressure would exceed the        |

| shutoff head of the HPI pumps.  Without minimum flow, the pumps would be     |

| damaged.                                                                     |

|                                                                              |

| "This issue is currently evaluated by Condition Report 02-06702.             |

| Davis-Besse has determined this condition is reportable under �              |

| 50.72(b)(3)(ii)(B) 'Any event or condition that results in ..'The nuclear    |

| power plant being in an unanalyzed condition that significantly degrades     |

| plant safety.'  Although the plant is currently in cold shutdown and the HPI |

| pumps are not required to be operable per the Technical Specifications, this |

| issue represents a historical condition that existed within the last three   |

| years."                                                                      |

|                                                                              |

| The licensee has notified the NRC Resident Inspector.                        |

+------------------------------------------------------------------------------+



+------------------------------------------------------------------------------+

|Fuel Cycle Facility                              |Event Number:   39751       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| FACILITY: WESTINGHOUSE ELECTRIC CORPORATION    |NOTIFICATION DATE: 04/12/2003|

|   RXTYPE: URANIUM FUEL FABRICATION             |NOTIFICATION TIME: 17:02[EDT]|

| COMMENTS: LEU CONVERSION (UF6 to UO2)          |EVENT DATE:        04/11/2003|

|           COMMERCIAL LWR FUEL                  |EVENT TIME:        18:30[EDT]|

|                                                |LAST UPDATE DATE:  04/12/2003|

|    CITY:  COLUMBIA                 REGION:  2  +-----------------------------+

|  COUNTY:  RICHLAND                  STATE:  SC |PERSON          ORGANIZATION |

|LICENSE#:  SNM-1107              AGREEMENT:  Y  |BRIAN BONSER         R2      |

|  DOCKET:  07001151                             |JANET SCHLUETER      NMSS    |

+------------------------------------------------+                             |

| NRC NOTIFIED BY:  CARL SNYDER                  |                             |

|  HQ OPS OFFICER:  JOHN MacKINNON               |                             |

+------------------------------------------------+                             |

|EMERGENCY CLASS:          NON EMERGENCY         |                             |

|10 CFR SECTION:                                 |                             |

|NBNL                     RESPONSE-BULLETIN      |                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

+------------------------------------------------------------------------------+



                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| LOSS OF DOUBLE CONTINGENCY PROTECTION                                        |

|                                                                              |

| NRC BULLETIN 91-01 24 HOUR NOTIFICATION                                      |

|                                                                              |

| Westinghouse Electric Company, Commercial Fuel Fabrication Facility,         |

| Columbia SC, low enriched (less than or equal to  5.0 wt. % U-235) PWR fuel  |

| fabricator for commercial light water reactors. License: SNM-1107.           |

|                                                                              |

| Time and Date of Event:  18:30 hours, April 11, 2003.                        |

|                                                                              |

| Reason for Notification:                                                     |

|                                                                              |

| On March 19, 2003, six UF6 cylinders were placed on hold because             |

| Westinghouse questioned if the cylinders were properly tested following      |

| repair. The ANSI N14.1 nameplate had been removed from supporting "feet"     |

| and-welded directly onto the pressure vessel dome. The "U" Stamp had been    |

| replaced with an "R" Stamp and documentation from the shipper indicated that |

| the fillet weld on the dome had undergone dye-penetrant testing. The UF6     |

| cylinder pressure vessel, however, had not undergone hydrostatic testing.    |

|                                                                              |

| The "hold" consisted of a flag in the UF6 cylinder tracking computer         |

| database, which was inserted as a manual edit. The hold flag should have     |

| prevented the cylinders from being transferred into work in process (WIP) to |

| allow processing.  On March 31, 2003 one of  the six cylinders was allowed   |

| by the tracking database to be processed. A second cylinder with the hold    |

| flag was allowed to be processed on April 1, 2003.                           |

|                                                                              |

| Unaware of the failure of the hold flags, the safety analysis proceeded. On  |

| April 10, 2003 NCS and process engineering completed the safety review begun |

| on March 19, 2003 of the nameplate welding using applicable pressure vessel  |

| standards including an on-site interview with a certified boiler code        |

| inspector. The conclusion of the safety review was that the "R" Stamp        |

| cylinders met the ANSI N 14.1 requirements and were acceptable for           |

| processing.                                                                  |

|                                                                              |

| On April 11, 2003, NCS began a review of the sequence of events leading to   |

| the processing of the two hold tagged cylinders. At approximately 18:30      |

| hours April 11, 2003 NCS completed its final interview. Shortly thereafter,  |

| it was determined that there had been a loss of previously documented        |

| double contingency protection. NCS immediately informed the EH&S manager of  |

| the event.                                                                   |

|                                                                              |

| Double Contingency Protection:                                               |

|                                                                              |

| The parameters that directly affect neutron multiplication for the           |

| vaporizers are mass (density) and geometry (level control). A criticality    |

| could be possible in a vaporizer under the following conditions:             |

|                                                                              |

| Sufficient material is discharged from the cylinder into the vaporizer in    |

| order to form a critical UO2F2 H2O density (optimum moderation), and water   |

| slab height increases to a critical height.                                  |

|                                                                              |

| Cylinder  integrity maintains mass control.  The U235 mass control depends   |

| upon maintaining the structural integrity of the cylinder to  ensure that no |

| material is released due to a sudden uncontrollable rupture.                 |

|                                                                              |

| The geometry control consists of ensuring that condensate drains properly    |

| from the vaporizer, and detecting water accumulation should it occur.        |

|                                                                              |

| It has been determined that less than previously documented double           |

| contingency protection remained for the system and that greater than a safe  |

| mass was involved. Double Contingency protection was restored within 4       |

| hours. In accordance with Westinghouse Operating License (SNM-1107),         |

| paragraph 3.7.3 (c.5b), this event satisfies the criterion for a 24-hour     |

| notification.                                                                |

|                                                                              |

| As Found Condition:                                                          |

|                                                                              |

| See "Reason for Notification." As detailed above, the Investigation found    |

| that the cylinders were safe to process. In fact, there never was an actual  |

| safety issue. The event did point out a weakness in our control of UF6       |

| cylinders that will be addressed.                                            |

|                                                                              |

| Summary of Activity:                                                         |

|                                                                              |

| 1) The four remaining cylinders were physically tagged out.                  |

| 2) A complete inventory and inspection of all cylinders on-site was          |

| performed.                                                                   |

| 3) It was verified that no movement of UF6 cylinders onto the site or into   |

| processing will occur for the next week.                                     |

|                                                                              |

| Conclusions:                                                                 |

|                                                                              |

| 1) Loss of double contingency protection occurred. Greater than a safe mass  |

| was involved.                                                                |

| 2) At no time was the health or safety to any employee or member of the      |

| public in jeopardy. No exposure to hazardous material was involved.          |

| 3)The Incident Review Committee (IRC) determined that this is a safety       |

| significant incident in accordance with governing procedures.                |

| 4) Notification was the result of an event, not a deficient NCS analysis.    |

| 5) A causal analysis will be performed.                                      |

+------------------------------------------------------------------------------+



+------------------------------------------------------------------------------+

|Power Reactor                                    |Event Number:   39752       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| FACILITY: PEACH BOTTOM             REGION:  1  |NOTIFICATION DATE: 04/12/2003|

|    UNIT:  [2] [] []                 STATE:  PA |NOTIFICATION TIME: 20:55[EDT]|

|   RXTYPE: [2] GE-4,[3] GE-4                    |EVENT DATE:        04/12/2003|

+------------------------------------------------+EVENT TIME:        18:47[EDT]|

| NRC NOTIFIED BY:  STEVEN SULLIVAN              |LAST UPDATE DATE:  04/12/2003|

|  HQ OPS OFFICER:  JOHN MacKINNON               +-----------------------------+

+------------------------------------------------+PERSON          ORGANIZATION |

|EMERGENCY CLASS:          NON EMERGENCY         |JAMES TRAPP          R1      |

|10 CFR SECTION:                                 |                             |

|ARPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|                             |

|AESF 50.72(b)(3)(iv)(A)  VALID SPECIF SYS ACTUAT|                             |

|                                                |                             |

|                                                |                             |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|2     A/R        Y       100      Power Operation  |0        Hot Shutdown     |

|                                                   |                          |

|                                                   |                          |

+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| AUTOMATIC REACTOR SCRAM- ALL RODS FULLY INSERTED                             |

|                                                                              |

| At 1847 hours on 04/12/03 the Peach Bottom Atomic Power Station Unit 2       |

| experienced an automatic reactor scram and shutdown following an air line    |

| failure which resulted in the closure of the "D" outboard main steam line    |

| isolation valve.  The closure of this valve resulted in a Reactor High       |

| Pressure Automatic Scram Signal.  This caused a actuation of the Alternate   |

| Rod Insertion system on reactor high pressure of 1106 psi.  All rods fully   |

| inserted. Additionally reactor vessel water level lowered to approximately   |

| negative 10 inches which resulted in a RPS and  PCIS Group 2 & 3             |

| isolations.  All systems activated as required. The outage control center is |

| currently staffed and repair/planning and restart preparation activities are |

| in progress.  Peach Bottom Atomic Power Station Unit 2 plant conditions are  |

| currently stable.                                                            |

|                                                                              |

| A copper air line going to the solenoid valve which operated the "D"         |

| outboard main steam isolation valve failed.  Cause of the line failure is    |

| unknown at this time.  The offsite electrical grid is stable and all         |

| emergency core cooling systems are fully operable if needed.                 |

|                                                                              |

| The NRC Resident Inspector was notified of this event by the licensee.       |

+------------------------------------------------------------------------------+



+------------------------------------------------------------------------------+

|Power Reactor                                    |Event Number:   39753       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| FACILITY: SEQUOYAH                 REGION:  2  |NOTIFICATION DATE: 04/12/2003|

|    UNIT:  [] [2] []                 STATE:  TN |NOTIFICATION TIME: 23:50[EDT]|

|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        04/12/2003|

+------------------------------------------------+EVENT TIME:        22:21[EDT]|

| NRC NOTIFIED BY:  MITCHEL TAGGART              |LAST UPDATE DATE:  04/13/2003|

|  HQ OPS OFFICER:  RICH LAURA                   +-----------------------------+

+------------------------------------------------+PERSON          ORGANIZATION |

|EMERGENCY CLASS:          NON EMERGENCY         |BRIAN BONSER         R2      |

|10 CFR SECTION:                                 |                             |

|ARPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|                             |

|AESF 50.72(b)(3)(iv)(A)  VALID SPECIF SYS ACTUAT|                             |

|                                                |                             |

|                                                |                             |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|                                                   |                          |

|2     A/R        Y       100      Power Operation  |0        Hot Standby      |

|                                                   |                          |

+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| TURBINE TRIP CAUSES REACTOR TRIP AT SEQOUYAH UNIT 2                          |

|                                                                              |

| "While resetting a turbine trip supervisory module, the unit 2 turbine       |

| tripped from "Turbine High Vibration Turbine Trip" at 22:21. The reactor     |

| tripped as a result of the turbine trip. Investigation is pending concerning |

| the turbine vibration equipment.                                             |

|                                                                              |

| "Auxiliary feed water system initiated as designed. All secondary plant      |

| equipment performed as expected.                                             |

|                                                                              |

| "The plant is being maintained in Mode 3 at NOT/NOP, 547  degrees F and 2235 |

| psig, with auxiliary feed water supplying the Steam Generators and steam     |

| dumps removing the decay heat."                                              |

|                                                                              |

| All control rods inserted into the core with no problems. The NRC Resident   |

| Inspector was notified.                                                      |

+------------------------------------------------------------------------------+



+------------------------------------------------------------------------------+

|Power Reactor                                    |Event Number:   39754       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| FACILITY: SOUTH TEXAS              REGION:  4  |NOTIFICATION DATE: 04/13/2003|

|    UNIT:  [1] [] []                 STATE:  TX |NOTIFICATION TIME: 19:06[EDT]|

|   RXTYPE: [1] W-4-LP,[2] W-4-LP                |EVENT DATE:        04/13/2003|

+------------------------------------------------+EVENT TIME:        16:56[CDT]|

| NRC NOTIFIED BY:  RON GIBBS                    |LAST UPDATE DATE:  04/13/2003|

|  HQ OPS OFFICER:  STEVE SANDIN                 +-----------------------------+

+------------------------------------------------+PERSON          ORGANIZATION |

|EMERGENCY CLASS:          NON EMERGENCY         |DAVID LOVELESS       R4      |

|10 CFR SECTION:                                 |                             |

|ADEG 50.72(b)(3)(ii)(A)  DEGRADED CONDITION     |                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|1     N          N       0        Cold Shutdown    |0        Cold Shutdown    |

|                                                   |                          |

|                                                   |                          |

+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| REACTOR VESSEL BOTTOM HEAD DEGRADED CONDITION                                |

|                                                                              |

| "On 4/12/2003, during the Unit 1 11th (1RE11) refueling outage, an           |

| inspection was performed of the vessel bottom head. This bare metal          |

| inspection identified a potential leak indication at the head to penetration |

| interface for Bottom Mounted Instrumentation (BMI) penetrations 1 and 46.    |

| There was a small amount of residue around the outer circumference of the    |

| BMI penetrations. No wastage was observed. Samples of the residue were taken |

| and the area was cleaned with demineralized water. Chemical sample results   |

| available as of 1300 on 4/13/2003 are not conclusive; however, they have     |

| confirmed that the residue found at the Penetration 46 contains boron,       |

| indicating that this could be an RCS leak. The residue removed from          |

| Penetration 1 was characterized as 'gummy' and its composition is still      |

| under investigation. Additional exams are planned to confirm the likely      |

| origin of the residue and to determine the scope of any repairs. There has   |

| been no indication of RCS leakage observed at the BMI penetrations during    |

| previous operational cycles. This notification is being made in accordance   |

| with 10 CFR 50.72(b)(3)(ii)(A)."                                             |

|                                                                              |

| Unit 1 will remain in mode 5 until appropriate corrective actions are        |

| identified.  The licensee informed the NRC resident inspector.               |

+------------------------------------------------------------------------------+





                    

Page Last Reviewed/Updated Wednesday, March 24, 2021