Event Notification Report for July 19, 2001
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 07/18/2001 - 07/19/2001 ** EVENT NUMBERS ** 38148 38149 38150 38151 38152 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38148 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 07/18/2001| | UNIT: [] [2] [] STATE: TX |NOTIFICATION TIME: 10:42[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 07/18/2001| +------------------------------------------------+EVENT TIME: 07:59[CDT]| | NRC NOTIFIED BY: RAUL MARTINEZ |LAST UPDATE DATE: 07/18/2001| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WILLIAM JOHNSON R4 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP ON TURBINE TRIP DURING RESTORATION OF AMSAC ALARM | | | | "During restoration of AMSAC [Accident Mitigation System Actuation | | Circuitry] to restore a trouble alarm, a spurious turbine trip signal was | | generated, causing a reactor trip from 100% power. AFW [Auxiliary | | Feedwater] actuation followed the reactor trip and the MSIV's [Main Steam | | Isolation Vales] were closed for temperature control." | | | | All control rods fully inserted. Unit 2 is currently stable at normal | | operating pressure and temperature (NOP, NOT) using the Atmospheric Dumps | | and both motor-driven AFW pumps for decay heat removal. There is no known | | primary-to-secondary tube leakage and samples confirm less than minimum | | detectable activity (less than MDA). Operators are in the process of | | re-opening the MSIV's to place the main condenser back in service. | | All electrical buses remained energized throughout the event. | | | | The licensee notified the NRC resident inspector and does not plan a press | | release. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 38149 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 07/18/2001| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 13:05[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 07/17/2001| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 15:30[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 07/18/2001| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |BRUCE JORGENSEN R3 | | DOCKET: 0707002 |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: SALYERS | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |OCBA 76.120(c)(2) SAFETY EQUIPMENT FAILUR| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | HIGH PRESSURE FIRE WATER SPRINKLER SYSTEM DECLARED INOPERABLE | | | | On 7/17/01 at approximately 1530 hrs, the Plant Shift Superintendent (PSS) | | was notified that during a Fire Protection Engineering assessment/inspection | | that High Pressure Fire Water (HPFW) sprinkler system #165 in the X-333 | | Building contained five adjacent sprinkler heads with visible corrosion | | deposits. Previous engineering reviews have concluded that the system under | | this condition would not be capable of meeting the Technical Safety | | Requirements (TSR) to maintain operability. | | | | The PSS declared the affected sprinkler system inoperable and TSR required | | actions were implemented. | | | | The NRC Resident Inspector was notified along with the DOE Representative. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38150 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MATHY CONSTRUCTION CO |NOTIFICATION DATE: 07/18/2001| |LICENSEE: MATHY CONSTRUCTION CO |NOTIFICATION TIME: 15:11[EDT]| | CITY: ONALASKA REGION: 3 |EVENT DATE: 07/18/2001| | COUNTY: STATE: WI |EVENT TIME: 12:00[CDT]| |LICENSE#: 4818722-01 AGREEMENT: N |LAST UPDATE DATE: 07/18/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |BRUCE JORGENSEN R3 | | |SUSAN FRANT NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DUKATZ | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE REPORTED THEIR TROXLER GAUGE WAS STOLEN | | | | The licensee reported that a Troxler moisture density gauge model 3440 | | serial #26689 containing 8 millicuries of Cs and 40 millicuries of Am/Be was | | stolen from the back of a truck in Barabo, WI. This occurred within 5-10 | | minutes when the driver entered a store to use the bathroom and buy some | | ice. The licensee will notify the local police and the State. | | | | * * * UPDATE ON 7/18/01 @ 1553 FROM DUKATZ TO GOULD * * * | | | | The local police contacted the licensee @ 1550 to inform them the gauge was | | located. There was no damage and the gauge was intact. Licensee has sent a | | technician to retrieve the gauge. | | | | Regon 3 (Darrel Wiedeman) and NMSS (Susan Frant) have been informed. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 38151 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: COLORADO DEPT OF HEALTH |NOTIFICATION DATE: 07/18/2001| |LICENSEE: BOLDER COMMUNITY HOSPITAL |NOTIFICATION TIME: 15:30[EDT]| | CITY: BOLDER REGION: 4 |EVENT DATE: 06/09/2001| | COUNTY: STATE: CO |EVENT TIME: [MDT]| |LICENSE#: 262-01 AGREEMENT: Y |LAST UPDATE DATE: 07/18/2001| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID GRAVES R4 | | |SUSAN FRANT NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JACOBI (BY FAX) | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - LEAKING SEALED SOURCE | | | | The following is taken from a faxed report: | | | | "We have recently experienced an incident resulting in the compromising of | | the shielding around an Iodine-125 prostate implant seed (sealed source). | | This report is filed per the requirements of RH 458 | | | | "On June 5, 2001, during the course of an I-125 seed implant of a patient's | | prostate gland an Iodine-125 seed which was thought to have been implanted | | was instead withdrawn with the implant plunger back into a position partly | | in the implant applicator and partly in the seed cartridge. This seed | | position will not allow the cartridge to be removed normally from the | | implant applicator. A GM counter (thin end window) survey was performed | | over that section of the implant applicator but the presence of the seed was | | not detected. The cartridge was then forcefully removed from the applicator. | | The applicator was rinsed into a stainless steel basin to remove blood clots | | that were present. The routine survey at the end of the procedure indicated | | that a seed was present in this washbasin. A bent seed was found in a | | blood clot. When the seed was removed from the basin, a survey of the basin | | indicated that the water was also contaminated. It was concluded that the | | shielding around the seed had been compromised. | | | | "The contents of the rinse basin were poured into a plastic container that | | could be sealed. All equipment, which had come in contact with the seeds, | | was surveyed and cleaned until wipe tests demonstrated that removable | | contamination had been reduced to less than 200 dpm. The sealed plastic | | container containing the contaminated liquid, and all of the cleaning | | materials were placed in our long-term waste storage facility for decay. | | Absorbent material was added to this container on July 11th to soak up any | | remaining liquid and eliminate any potential spill hazard over the two years | | (10 half-lives) this container will be in storage. | | | | "The two individuals most closely involved in extracting the seed cartridge | | and performing the cleanup were given thyroid bioassay exams in the week | | immediately following the incident. Those exams were negative. The patient | | was given the same exam approximately one month following the procedure that | | indicated an uptake of 0.2 � 0.09 �Ci corrected to the day of the implant. | | If this uptake is real and not the result of radiation scatter from his | | active prostate seed implant (87 seeds, 22.3 mCi on the day of the thyroid | | scan), this would result in a radiation dose to the thyroid of not more that | | 0.8 cGy. This radiation dose has no clinical significance. | | | | "Corrective Actions: This incident occurred because the applicator plunger, | | which most likely had a blood clot adhering at the point normally in contact | | with the iodine-125 seed, extracted the seed previously pushed into the | | prostate gland. The seed, believed to have been implanted, instead came to | | rest across the space between the applicator body and the seed cartridge. A | | GM survey of the applicator body and cartridge combination failed to detect | | the presence of the seed. The seed was damaged when the cartridge was | | forcefully withdrawn. | | | | "This incident could have been averted using the following procedure: | | | | 1. Assume that any cartridge jam is caused by an unaccounted for I-125 | | seed. | | 2. Remove the implant needle from the applicator body. (If there is believed | | to be only one seed involved in the jam, the applicator body may be surveyed | | by directing the sensitive portion of the GM detector down the barrel of the | | applicator previously occupied by the implant needle. The GM detector may | | not be sensitive enough to detect radiation though the sides of the | | applicator body.) | | 3. Place the body of the applicator with the cartridge still in place, into | | the rinse pan. | | 4. Advance the plunger slowly through the seed cartridge until the seed is | | visible and can be rinsed away from the body of the applicator. (This may | | requite lifting the cartridge plunger to allow the applicator plunger past | | such that it can traverse the full extent of the cartridge.) If the | | cartridge is not empty the seed causing the jam will be pushed out by | | another seed so two seeds will deposit in the rinse basin. | | 5. Withdraw the applicator plunger completely and remove the seed cartridge | | normally. | | 6. NEVER forcefully remove a seed cartridge! | | | | "All individuals involved In this incident have reviewed this procedure." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38152 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 07/19/2001| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 05:16[EDT]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 07/19/2001| +------------------------------------------------+EVENT TIME: 03:00[CDT]| | NRC NOTIFIED BY: RYAN RODE |LAST UPDATE DATE: 07/19/2001| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |BRUCE JORGENSEN R3 | |10 CFR SECTION: | | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |90 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TECH SPEC REQUIRED SHUTDOWN DUE TO TIME LIMIT ON NON-SAFETY POWER TO | | INSTRUMENT BUS | | | | The licensee entered Technical Specification 15.3.7(b)(1)(j) at 1900 CDT on | | 7/18/2001, which allowed 8 hours to restore electrical power from a safety | | powered bus to the Unit 1 instrument bus. Non-safety power was provided | | when a problem caused an automatic transfer. At 0300 CDT on 7/19/2001 a | | Technical Specification required shutdown was commenced. The plant has 6 | | hours to reach Hot Shutdown and another 44 hours to reach Cold Shutdown. | | The licensee has been and continues to research the problem and does not | | know when safety power will be restored to the instrument bus. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021