Event Notification Report for November 17, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/16/2000 - 11/17/2000 ** EVENT NUMBERS ** 37524 37525 37527 37528 37529 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37524 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 11/15/2000| | UNIT: [] [2] [] STATE: NC |NOTIFICATION TIME: 15:49[EST]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 11/15/2000| +------------------------------------------------+EVENT TIME: 14:22[EST]| | NRC NOTIFIED BY: VERITA BELLAMY |LAST UPDATE DATE: 11/16/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE ERNSTES R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 M/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO FAILURE OF TURBINE RUNBACK ACTUATION CIRCUITS | | | | Unit 2 experienced a turbine runback at 1410 EST. The control room | | operators noticed all status lights for overpower and overtemperature delta | | T runback were illuminated. The operators decided to manually trip the | | reactor from about 23 % rated thermal power. The reactor trip resulted in a | | turbine trip as expected. Auxiliary feedwater pumps started due to low-low | | steam generator levels. The unit is stable in Mode 3. | | | | The runback bistables are locked in without having the logic bistables | | tripped that feed the trip circuit. The licensee is troubleshooting the | | problem and the cause is unknown at this time. The plant will remain in | | Mode 3 until the problem is corrected. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE 1345EST FROM TIM HEADNON TO BOB STRANSKY * * * | | | | The licensee is updating their report to include the following information: | | | | "On November 15, 2000, McGuire Unit 2 experienced a turbine runback which | | ultimately resulted in plant operators manually tripping the reactor (RPS | | Actuation). Following the trip, the Unit 2 Auxiliary Feedwater Pumps started | | due to low-low steam generator levels (ESF Actuation) | | | | "Further investigation has determined that the turbine runback was caused by | | actuation of all four channels of over power delta temperature (OPDT) and | | over temperature delta temperature (OTDT) runback logic following a trip of | | an electrical breaker which supplies power to the logic circuitry. The | | turbine runback was a result of the breaker trip and was not initiated by a | | valid OPDT or OTDT condition. Subsequent to the turbine runback, a decision | | was made to manually trip the reactor. Plant equipment necessary to safely | | shutdown the unit operated correctly and the Unit is stable and in Mode 3. | | The Unit 2 Auxiliary Feedwater Pumps have been secured. Actions needed to | | restart Unit 2 are in progress." | | | | The licensee informed the NRC resident inspector. Notified R2DO(Ernstes). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37525 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OYSTER CREEK REGION: 1 |NOTIFICATION DATE: 11/15/2000| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 19:04[EST]| | RXTYPE: [1] GE-2 |EVENT DATE: 11/15/2000| +------------------------------------------------+EVENT TIME: 17:50[EST]| | NRC NOTIFIED BY: JERE FREEMAN |LAST UPDATE DATE: 11/16/2000| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 1 Startup |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM DUE TO LOW REACTOR WATER LEVEL | | | | The plant received a low water level reactor scram during turbine | | manipulation after 2 turbine bypass valves opened. All systems functioned | | as designed. The actual cause is not fully understood and is under | | investigation. | | | | The licensee notified the NRC Resident Inspector. | | | | * * * UPDATE 1513EST ON 11/16/00 FROM STEVE FULLER TO S. SANDIN * * * | | | | The following information was received as an update: | | | | "On 11/15/00 at 1748 EST, Oyster Creek Nuclear Generating Station | | automatically scrammed on reactor low water level (as described on Event | | Number 37525). The station was in the process of restarting from the plant | | from the recent 1 SR refueling outage. The operators were in the process of | | securing High Pressure Turbine warm-up and preparing to perform Steam Chest | | warm-up. As they transitioned between these activities, the turbine bypass | | valves opened. As a result of the bypass valves opening, reactor water level | | increased. The operators responded to the reactor water level transient but | | failed to recognize the pressure reduction. The loss of inventory resulted | | in a low water level reactor scram. | | | | "The station has conducted a transient assessment of this incident. The | | preliminary root cause was identified as a procedural deficiency. The | | Turbine System Operating Procedure did not provide the appropriate guidance | | for preventing the bypass valves from opening. Additionally, the operators | | demonstrated a lack of integrated system knowledge and response regarding | | the turbine controls system. | | | | "Subsequent reviews of the plant data revealed that the cool down rate | | exceeded the plant's Technical Specification limit of 100 degrees per hour. | | This occurred because of the low initial power level coupled with the bypass | | valves not being closed in a timely manner. Engineering has assessed this | | condition and determined that the plant response was within our design | | bases. Additionally, the Post Transient Review Group (PTRG) identified a | | potential concern regarding the operation of the reactor low water level | | transmitters. One of the four reactor low water level scram switches did not | | actuate. Even though the PTRG suspected this switch didn't actuate because | | the decrease in reactor water level wasn't sufficient due to the low initial | | power level, this switch was subsequently tested and operated | | appropriately. | | | | "Following completion of the required restart activities, the plant | | commenced startup activities at 2:57 EST on 11/16/00. In accordance with | | 10CFR50.73 a Licensee Event Report will be submitted to describe this | | incident, the root cause, and associated corrective actions." | | | | The licensee will inform the NRC resident inspector. Notified | | R1DO(Barkley). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37527 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FARLEY REGION: 2 |NOTIFICATION DATE: 11/16/2000| | UNIT: [] [2] [] STATE: AL |NOTIFICATION TIME: 05:10[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 11/16/2000| +------------------------------------------------+EVENT TIME: 03:23[CST]| | NRC NOTIFIED BY: BRAD MOORE |LAST UPDATE DATE: 11/16/2000| | HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE ERNSTES R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP ON HIGH-HIGH STEAM GENERATOR WATER LEVEL FOLLOWING A | | MASTER STEAM GENERATOR FEEDWATER PUMP CONTROLLER FAILURE AND SLUGGISH | | CONTROLS AFTER SWITCHING TO MANUAL | | | | The master steam generator feedwater pump controller failed low and caused | | feedwater pump speeds to slow down. (Both pumps dropped to 3,200 rpm.) In | | an attempt to regain feedwater pump speed and steam generator water level in | | manual, a high-high level was reached in the 2A steam generator. This | | caused a turbine trip and subsequent reactor trip. All control rods fully | | inserted. Auxiliary feedwater actuation and feedwater isolation occurred as | | expected. All systems functioned as required. | | | | It was reported that the controller was sluggish after manual control was | | taken and that operators were not able to terminate the rising level in the | | 2A steam generator before the high-high level trip setpoint was reached. | | The lowest steam generator water level attained was approximately 27%. The | | low level trip occurs at 25%. The cause of the controller failure is | | currently under investigation. | | | | The unit is currently stable in Hot Standby. Pressurizer heaters and | | sprays, normal charging and letdown, and the reactor coolant pumps are | | currently being utilized for primary system pressure, level, and transport | | control. Secondary steam is being dumped to the main condenser, and | | auxiliary feedwater is supplying water to the steam generators. All | | containment parameters are normal. | | | | The licensee plans to notify the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37528 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 11/16/2000| | UNIT: [1] [] [] STATE: FL |NOTIFICATION TIME: 13:06[EST]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 11/16/2000| +------------------------------------------------+EVENT TIME: 12:15[EST]| | NRC NOTIFIED BY: JAMES HURCHALLA |LAST UPDATE DATE: 11/16/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MIKE ERNSTES R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNIT 1 PRESSURIZER LEVEL INSTRUMENTATION MAY NOT MEET CABLE SEPARATION | | CRITERIA | | | | "During development of a cable separation modification package for the | | upcoming 2001 Unit 1 Outage SL1-17, a re-evaluation of the Unit 1 | | Containment Shutdown Safety Assessment was performed. The re-evaluation | | identified a separation issue with the cables for pressurizer level | | instruments LT-1110X and LT-1110Y in the annulus area. At certain | | locations, these cables are not separated as required by 10 CFR Part 50 | | Appendix R, Section lll.G.2 as required by the plant design basis as | | delineated in the FSAR. | | | | "Fire protection for nuclear plants is based on the defense in depth concept | | with three primary barriers - prevention, detection and control, and | | protection of safe shutdown capabilities. The above concern is considered a | | degradation of the protection of safe shutdown capability. The affect of | | this concern on the fire protection program does not eliminate the ability | | to achieve safe shutdown. The remaining two 'defense in depth' barriers | | remain intact - (prevention of fires and prompt detection and control of | | fires that due occur). In an area such as containment (large volume, high | | ceilings, minimal ignition sources, limited combustibles, limited access, | | etc.) the potential for a fire of consequence during operation is highly | | unlikely. In the particular area described, the potential for a fire is even | | more remote since the combustible loading is negligible. The location where | | the separation issue exists (at the end of the annulus area near the pipe | | chase) does not contain significant equipment, significant exposed | | combustible materials or significant ignition sources. The cable trays | | routed in this area (between radius lines 1 and 3) are relatively lightly | | loaded since most cables have previously exited the tray enroute to their | | respective equipment (e.g., only one tray continues past radius line 2 to | | radius line 1). | | | | "The probability of a fire in Containment is very low. The probability of a | | fire causing significant damage such that required function is impaired is | | very low. Therefore, the equipment and system affected by this condition is | | considered degraded but operable. Based on the guidance provided in GL 91-18 | | a reasonable assurance of safety is provided." | | | | The licensee informed the NRC resident inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 37529 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: USAF RADIOISOTOPE COMMITTEE |NOTIFICATION DATE: 11/16/2000| |LICENSEE: U.S. AIR FORCE |NOTIFICATION TIME: 21:32[EST]| | CITY: SARASOTA REGION: 2 |EVENT DATE: 11/16/2000| | COUNTY: STATE: FL |EVENT TIME: 17:20[EST]| |LICENSE#: 42-23539-01AF AGREEMENT: Y |LAST UPDATE DATE: 11/16/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MIKE ERNSTES R2 | | |LINDA HOWELL R4 | +------------------------------------------------+E. WILLIAM BRACH NMSS | | NRC NOTIFIED BY: LT. COL. SWENSON | | | HQ OPS OFFICER: STEVE SANDIN | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF TWO AMERICIUM-241 SOURCES (4 MICROCURIES EACH) DUE TO THE CRASH OF | | AN F-16 NEAR SARASOTA, FLORIDA | | | | An F-16 crashed near Sarasota, Florida which may have been carrying two (2) | | Am-241 sources used in the LANTIRN (Low Altitude Navigation Targeting | | Infrared for Night) pod. The Air Force will followup to determine whether | | the sources were onboard and, if so, attempt recovery from the crash scene. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021