Event Notification Report for October 24, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 10/23/2000 - 10/24/2000 ** EVENT NUMBERS ** 37441 37450 37451 +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37441 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WESTINGHOUSE ELECTRIC CORPORATION |NOTIFICATION DATE: 10/19/2000| | RXTYPE: URANIUM FUEL FABRICATION |NOTIFICATION TIME: 08:53[EDT]| | COMMENTS: LEU CONVERSION (UF6 to UO2) |EVENT DATE: 10/18/2000| | COMMERCIAL LWR FUEL |EVENT TIME: 09:30[EDT]| | |LAST UPDATE DATE: 10/23/2000| | CITY: COLUMBIA REGION: 2 +-----------------------------+ | COUNTY: RICHLAND STATE: SC |PERSON ORGANIZATION | |LICENSE#: SNM-1107 AGREEMENT: Y |CAUDLE JULIAN R2 | | DOCKET: 07001151 |BRIAN SMITH NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM HEATH | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | FAILURE OF VAPORIZE LEVEL PROBE IN "3A" VAPORIZER | | | | NRC BULLETIN 91-01 24 HOUR NOTIFICATION | | | | Periodic testing of the condensate level detection system in the 3A | | vaporizer steam chest determined that the system could not perform its | | intended function due to blockage in the system by loose debris. Further | | investigation determined that paint flaked from the recently processed | | cylinder and collected in the bottom of the vaporizer. However, the debris | | did not block the main condensate removal drain which allowed condensate to | | be removed from the vaporizer, so there was no condensate accumulation. | | | | The vaporizer bottom was cleaned and the level detection system was checked. | | The system responded correctly. | | | | SAFETY SIGNIFICANCE OF EVENTS: | | | | No contingency occurred. No accumulation of water in the bottom of the | | vaporizer occurred. No SNM was involved. | | | | CONTROLLED PARAMETER: | | | | Mass and moderator are the controlled parameters for the vaporizer. | | | | ESTIMATED AMOUNT, ENRICHMENT, FORM of LICENSED MATERIAL: | | | | Cylinders heated in the vaporizer contain uranium hexafluoride gas with a | | uranium-235 enrichment less than 5.0 weight percent. No SNM was involved in | | this incident since uranium hexafluoride was contained at all times within | | the uranium hexafluoride piping system. | | | | NUCLEAR CRITICALITY SAFETY CONTROL(s) OR CONTROLLED SYSTEM(s) AND | | DESCRIPTION OF THE FAILURES OR DEFICIENCIES: | | | | The condensate level detection system in the 3A vaporizer was rendered | | inoperable as a result of a drain line that was blocked by debris which came | | from the most recently processed cylinder. | | | | CORRECTIVE ACTIONS TO RESTORE SAFETY SYSTEMS AND WHEN EACH WAS IMPLEMENTED: | | | | The debris in the 3A vaporizer was removed and proper functioning of the | | level detection system was verified. The 3A vaporizer was released for | | restart on October 19, 2000 at 0730 hours. Other vaporizers not in use at | | the time of the incident were checked for proper functioning of the level | | detection system; each system responded correctly. Other vaporizers in use | | at the time were subject to increased-frequency checks to verify proper | | functioning of the condensate removal system; all vaporizers were draining | | properly. In addition, the condensate level detection system for in-use | | vaporizers will be function-tested immediately after the uranium | | hexafluoride cylinder currently being processed is removed. | | | | | | * * * UPDATE ON 10/23/00 @ 1210 BY HEATH TO GOULD * * * | | | | Reason for submitting supplemental information: | | | | Supplemental information is submitted to provide further information on the | | as found condition and to clarify the safety significance of the event. | | | | Double Contingency Protection: | | | | 30B UF6 cylinders are heated in the vaporizers with saturated steam. The | | steam is removed via a condensate removal system. Double contingency | | protection for the vaporizers is based on mass and moderator control. Mass | | control consists of controls to prevent and detect an uncontrolled release | | of UF6 inside the vaporizer. Moderator control consists of controls to | | detect accumulation of moderator (specifically condensate) and prevent the | | accumulation of moderator in the bottom of the vaporizer. | | | | As Found Condition: | | | | Two drains are present in the bottom of each vaporizer which allow steam to | | enter the condensate removal system. Each drain has an individual drain | | screen. A larger removable debris screen rests in the bottom of the | | vaporizer above the two individual drain screens. One drain flows through a | | pot in which reside the high and high-high level probes. The second drain | | proceeds directly to the condensate system. In this event the screen which | | covers the drain which flows to the level pot was obstructed with paint | | residue, thereby isolating the level probes. As a result of the isolation | | of the level probes, the ability to detect high level was lost. However, at | | no time was the condensate removal path closed. There was no accumulation | | of water in the vaporizer and no SNM was present. | | | | The cylinder from which the paint residue came was provided by Urenco. | | Urenco has been advised by this facility of the situation. Prior to | | processing, the paint showed no indication of being defective. The paint was | | not chipped, peeling, bubbling from the surface, discolored, or otherwise | | distinguishable as flawed. | | | | It is also very likely that the plugging of the drain occurred as a result | | of the functional test which detected it. The functional test of the | | vaporizer level probes is performed by filling the bottom of the empty | | vaporizer with water from a hose. During steady state operation the | | expected flow rate of condensate through a vaporizer is on the order of 1.48 | | gallons per hour. As was described earlier, the larger debris screen rests | | above the two drains. The seal along the bottom perimeter of the debris | | screen is not air or water tight and need not be due to the fact that it | | sees a low flow rate of steam and not a flow of liquid. During the | | functional test, it is likely the paint debris was sluiced underneath the | | debris screen by the relatively high flow rate of water which is used for | | the test. Notification was nevertheless made due to the fact that there is a | | small possibility that the vaporizer was operated in this condition. | | | | | | Conclusions related to safety significance: | | | | * Loss of double contingency protection may have occurred. | | * No UF6 leaks occurred in the vaporizer. No failure of mass controls | | occurred. No SNM was involved. | | * The condensate flow path from the vaporizer was not blocked. No moderator | | accumulated in the vaporizer | | * At no time was there any risk to the health or safety of any employee or | | member of the public. No exposure to hazardous material was involved. | | * The safety significance of this event is evaluated to be low. | | | | | | The Reg 2 RDO(Belise) and the MNSS EO(Schnieder) were notified | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37450 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 10/23/2000| | UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 13:31[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 10/23/2000| +------------------------------------------------+EVENT TIME: 13:00[EDT]| | NRC NOTIFIED BY: BREEN |LAST UPDATE DATE: 10/23/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |AL BELISLE R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE LICENSEE MADE NOTIFICATION TO FLORIDA FISH AND WILDLIFE CONSERVATION | | COMMISSION | | | | This notification was made due to a live loggerhead turtle being found in | | the intake net. The turtle was not in very good condition. It will be sent | | off site for rehabilitation. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37451 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 10/23/2000| | UNIT: [] [2] [] STATE: CA |NOTIFICATION TIME: 21:25[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 10/23/2000| +------------------------------------------------+EVENT TIME: 16:37[PDT]| | NRC NOTIFIED BY: BAHNER |LAST UPDATE DATE: 10/23/2000| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GREG PICK R4 | |10 CFR SECTION: | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT HAD AUTO START OF ALL THREE DIESEL GENERATORS DUE TO PERSONNEL ERROR | | | | Startup Power was being cleared to Unit 1 for refueling outage maintenance. | | Part of the clearance was to open switch 211-1 for Unit 1 Startup | | Transformer. Operators inadvertently opened switch 211-2 for Unit 2 Startup | | Transformer. This caused all three Unit 2 Diesel Generators (D/G) to start | | on loss of Startup Power signal. Starting of the D/G's is considered to be | | an ESF actuation and constitutes a 4 hour non-emergency report per | | 10CFR50.72(B)(2). Startup Power was restored three minutes later and the | | D/G's returned to standby condition. The D/G's did not load on the bus and | | no other ESF systems were affected. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021