Event Notification Report for June 6, 2000
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/05/2000 - 06/06/2000 ** EVENT NUMBERS ** 37056 37057 37058 37059 37060 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 37056 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NC DIVISION OF RADIATION PROTECTION |NOTIFICATION DATE: 06/05/2000| |LICENSEE: DURHAM VA HOSPITAL |NOTIFICATION TIME: 09:53[EDT]| | CITY: DURHAM REGION: 2 |EVENT DATE: 06/04/2000| | COUNTY: STATE: NC |EVENT TIME: 16:15[EDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 06/05/2000| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |EDWARD MCALPINE R2 | | |DON COOL NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ALBRIGHT | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THE DURHAM, N.C. VA HOSPITAL SENT SOME RADIOACTIVE WASTE TO THE DURHAM WASTE | | TRANSFER STATION. | | | | A WASTE INDUSTRIES TRUCK SETOFF THE PORTAL MONITOR AT THE DURHAM WASTE | | TRANSFER STATION. THE TRUCK HAD PICKED UP A LOAD OF WASTE FROM THE DURHAM | | VA HOSPITAL. THE WASTE WAS RETURNED TO THE HOSPITAL. ONE BAG CONTAINED IN | | THE WASTE WAS MEASURING 150,000 CPM AT ONE FOOT AND OFF SCALE AT THE BAG. | | A DIAPER IN THE BAG WAS DETERMINED TO BE THE SOURCE. IT WAS DISCOVERED THE | | PATIENT WHO HAD WORN THE DIAPER HAD RECEIVED 20 MILLICURIES OF TECHNETIUM-99 | | ON THAT MORNING. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 37057 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 06/05/2000| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 13:22[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 06/05/2000| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 09:27[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 06/05/2000| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |JOHN JACOBSON R3 | | DOCKET: 0707002 |BRIAN SMITH NMSS | +------------------------------------------------+CHARLES MILLER IRO | | NRC NOTIFIED BY: KEITH VANDERPOOL | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NBNL RESPONSE-BULLETIN | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | 4 HOUR NRC BULLETIN 91-01 NOTIFICATION CONCERNING LOSS OF 2 CONTROLS OF | | DOUBLE CONTINGENCY | | | | ON 6/5/00 AT 0927 HOURS PLANT PERSONNEL WERE REMOVING INSULATION FROM THE | | X-705 PROCESS PIPING WHEN THEY DISCOVERED EVIDENCE OF A FAILURE OF THE | | INTEGRITY OF SAID PIPING (material residue visible on the insulation). THIS | | FAILURE VIOLATES NCSA-0705_076 WHICH TAKES CREDIT FOR THE INTEGRITY OF THE | | PROCESS PIPING, THUS CONSTITUTING A LOSS OF ONE CONTROL. THE FACT THAT THE | | ENCAPSULATING INSULATION PHYSICALLY CAPTURED THE LEAKING MATERIAL MEETS THE | | DEFINITION FOR AN INADVERTENT CONTAINER THUS CONSTITUTING A LOSS OF ONE | | CONTROL AS DESCRIBED BY NCSA-0705_076 WHICH TAKES CREDIT FOR COVERING, | | MODIFICATION OR ELEVATION OF ABSORBENT MATERIALS TO PREVENT THE COLLECTION | | OF URANIUM BEARING LIQUID IN AN INADVERTENT CONTAINER. | | | | IT SHOULD BE NOTED THAT IT IS NOT CLEAR WHETHER OR NOT THE TOTAL VOLUME OF | | MATERIAL INVOLVED WAS GREATER THAN THE ALLOWED SAFE VOLUME (4.8 Liters ) | | CREDITED IN THE EVALUATION FOR ENSURING DOUBLE CONTINGENCY. BASED ON VISUAL | | INSPECTION OF THE MATERIAL PRESENT IN/ON THE INSULATION, IT IS ESTIMATED | | THAT THE TOTAL AMOUNT OF URANIUM BEARING MATERIAL IS LESS THAN 350 GRAMS. | | MORE RELIABLE ANALYSIS IS CURRENTLY BEING PERFORMED FOR MORE PRECISE | | DETERMINATION OF THE AMOUNT OF MATERIAL. SINCE THE FAILURE TIME OF THE | | PROCESS PIPING IS UNKNOWN, THE ENRICHMENT PERCENTAGE OF THE MATERIAL COULD | | BE (worst case) 100% wt. U-235. THE MATERIAL PROCESSED IN THE X-705 RECOVERY | | AREA PRIMARILY INVOLVES URANYL NITRATE, ALTHOUGH SOME URANYL FLUORIDE MAY BE | | PRESENT. | | | | THE PSS HAS SUSPENDED ALL WORK/PROCESS EVOLUTIONS IN THE AFFECTED AREA | | PENDING INVESTIGATION. CONTROLS WERE RE-ESTABLISHED UNDER THE DIRECTION OF | | THE NUCLEAR CRITICALITY SAFETY STAFF AT 1156 HOURS THIS DATE. | | | | Safety Significance of Events: | | | | On June 5, 2000, it was discovered that the insulation around the A loop | | density pot was contaminated by uranium-bearing material. This insulation | | was approximately 1 to 3 inches in thickness and constructed out of an | | absorbent material. The density pot is 4-inch schedule 40 piping located | | below the A loop evaporator and is approximately | | 24-inches in length. Clamp-on density transmitters are used for density | | control in the uranium-bearing feed solution to the extractor/strippers. | | After removal from the density pot, the insulation was observed to be coated | | with a yellowish material, which, based on high count readings, appears to | | be uranium-bearing. The material appeared dry in nature. It is not clear | | when the material accumulated on/in the insulation or how much was present | | during that accumulation. This insulation represents a violation of | | NCSA-0705_076 in that the absorbent material (i.e., the insulation) was not | | covered or modified properly. | | | | In addition, there is a potential loss of control in the failure of the | | nearby system integrity. It is not clear when or exactly how the | | uranium-bearing material was transported such that it accumulated on/in the | | insulation. It should be noted that it is not clear whether or not the total | | volume of material involved (i.e., which could /did accumulate on/in the | | insulation) was greater than the allowed (i.e., safe) volume credited in the | | evaluation for ensuring double contingency. Thus, while the anomalous | | condition is being treated as a loss of both controls the most likely | | scenario is that the material involved less than a safe amount of material | | and so the safety significance of this event is low. | | | | 2. Potential Criticality Pathways Involved; | | | | If a sufficient amount of uranium-bearing material had accumulated on/in the | | insulation, an unsafe geometry could have resulted and if the leaking | | solution had contained a sufficient amount of uranium, the resulting | | configuration could have been sufficient for a criticality to occur. It | | should be noted that the allowed safe geometry and volume limits established | | in NCSA-0705_076 are based on optimally moderated, UO2F2 and water solution | | which contains uranium enriched to 100 wt%. | | | | 3. Controlled Parameters: | | | | The parameter which was violated during this upset was the geometry of | | potential accumulation present on/in the insulation. In addition, the | | physical integrity of nearby piping was violated at some point in the past. | | As stated previously, the total amount of solution involved (i.e., the | | volume of solution which leaked onto the insulation and resulted in the | | uranium-bearing material being deposited on/in the insulation) is unknown, | | so it is conservatively being evaluated as though the volume was greater | | than the safe volume allowed. This represents the failure of both controls | | relied upon for ensuring double contingency. | | | | 4 Estimated Amount, Enrichment, Form of Licensed Material: | | | | Based on visual inspection of the material present on/in the insulation, it | | is estimated that the total amount of uranium-bearing material is less than | | 350 grams. More reliable analysis is currently being performed for a more | | precise determination of the amount of material. Since the failure time is | | unknown, the enrichment of the material could be up to 100 wt% U-235. The | | material processed in the X-705 recovery primarily involves uranyl nitrates | | (U02(N03)2) , although some uranyl fluoride (UO2F2) may also be present. | | | | 5. Nuclear Criticality Safety Control(s) or control system(s) and | | description of the failures or deficiencies: | | | | NCSA-0705_076.A00 takes credit for the physical integrity of systems which | | contain uranium-bearing material and that unsafe volume/geometry containers | | (including absorbent materials like the insulation) are either modified, | | covered, or oriented to prevent an unsafe configuration from resulting in | | the event of a leak. The absorbent material was not modified, covered, or | | oriented to prevent an unsafe configuration. In addition, there is evidence | | that at some time in the past a loss of nearby system integrity occurred | | such that the insulation was exposed to an uranium-bearing solution. | | | | 6. Corrective Actions to Restore Safety System and when each was | | Implemented: | | | | Under the direction of the nuclear criticality safety staff NCSA controls | | were re-established at 1156 hours, with all maintenance work and process | | evolutions suspended pending the ongoing investigation by facility | | management and nuclear criticality safety staff personnel. | | | | The NRC Resident Inspector was notified of this event by the certificate | | holder. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37058 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: VOGTLE REGION: 2 |NOTIFICATION DATE: 06/05/2000| | UNIT: [1] [] [] STATE: GA |NOTIFICATION TIME: 13:52[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/05/2000| +------------------------------------------------+EVENT TIME: 11:40[EDT]| | NRC NOTIFIED BY: CECIL H. WILLIAMS |LAST UPDATE DATE: 06/05/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |EDWARD MCALPINE R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 M/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MANUAL REACTOR TRIP DUE TO MAIN STEAM ISOLATION VALVE CLOSING. | | | | AT 1140 EDT the Unit One Control Room crew received a trouble alarm on Steam | | Generator Loop 4 Inboard Main Steam Isolation Valve (MSIV). The operators | | observed no light indication on the MSIV, a decreasing level in the Steam | | Generator, a large decrease in indicated steam flow, and control rods began | | inserting. The Shift Superintendent directed that the reactor be manually | | tripped. The reactor was manually tripped and all systems functioned as | | required with the exception of a non-1E 4160 V bus (loss steam dump bypass | | control panel open/close indication) , which failed to auto transfer to | | it's startup power source. Auxiliary Feedwater System (both motor and the | | turbine driven pumps) actuated as expected on Steam Generator Lo-Lo levels. | | | | | | The Control Room crew has exited the Emergency Operating Procedures and the | | unit is stable in Mode 3 at normal operating temperature and pressure. | | | | The 4160 V breaker which failed to close was racked out of it's cubicle, | | inspected and racked back into it's operating position, after which it was | | successfully closed by the Control room crew. This reenergized the | | non-1E 4160V bus and its associated loads. | | | | Investigation into the cause of the MSIV closure is ongoing. An Event Review | | Team is being formed, and a restart date will be decided upon following | | management review of the results of their investigation. | | | | Steam Generator Atmospheric valve controller was reduced to its lowest | | setpoint and maintained the Reactor Coolant System at its Tave no load | | condition (Steam Generator 1 & 4 Atmospheric valves opened/closed a few | | times). The Steam Dump Bypass Control System was fully operable and | | operated properly. Approximately one hour after the event non-1E 4160V bus | | was re-energized. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37059 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CATAWBA REGION: 2 |NOTIFICATION DATE: 06/05/2000| | UNIT: [] [2] [] STATE: SC |NOTIFICATION TIME: 15:40[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 06/05/2000| +------------------------------------------------+EVENT TIME: 12:37[EDT]| | NRC NOTIFIED BY: K. PHILLIPS |LAST UPDATE DATE: 06/05/2000| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |EDWARD MCALPINE R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(ii) RPS ACTUATION | | |AESF 50.72(b)(2)(ii) ESF ACTUATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR TRIP ON HIGH STEAM GENERATOR WATER LEVEL | | | | | | Automatic reactor trip from 100% power due to a feedwater transient caused | | by a loss of control power to 2B main feedwater pump. The feedwater | | transient resulted in a 2B steam generator high-high setpoint being reached | | which tripped both main feedwater pumps, caused a feedwater isolation | | signal, and tripped the main turbine which caused the reactor trip. All | | rods fully inserted into the core. Steam generators levels are being | | maintained at normal level with auxiliary feedwater at this time. The loss | | of control power has been attributed to water intrusion into the 2B | | feedwater pump control panel from extremely heavy rains and roof repairs | | being in progress. | | | | All Emergency Core Cooling Systems and the Emergency Diesel Generators are | | fully operable if needed. The electrical grid is stable an Unit 1 was not | | affected by Unit 2's reactor trip. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 37060 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DUANE ARNOLD REGION: 3 |NOTIFICATION DATE: 06/06/2000| | UNIT: [1] [] [] STATE: IA |NOTIFICATION TIME: 06:02[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 06/06/2000| +------------------------------------------------+EVENT TIME: 02:36[CDT]| | NRC NOTIFIED BY: JOHN VAN SICKEL |LAST UPDATE DATE: 06/06/2000| | HQ OPS OFFICER: STEVE SANDIN +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: |JOHN JACOBSON R3 | |10 CFR SECTION: | | |AINC 50.72(b)(2)(iii)(C) POT UNCNTRL RAD REL | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SECONDARY CONTAINMENT DECLARED INOPERABLE DUE TO LOSS OF WATER SEAL CAUSED | | BY PIPE CORROSION | | | | "A 4 inch diameter floor drain outlet pipe inside the Standby Gas Treatment | | Sump was identified by Operating personnel to be corroded through near the | | wall of the sump. This piping is designed to act as a Secondary Containment | | boundary which is used to form a loop seal between the Reactor Building and | | the SBGT room. Normally, the piping would come out from the wall and make a | | 90 degree turn to near the bottom of the sump, and open under water. | | However, with the erosion occurring near the wall of the sump, a breech of | | secondary containment exists. Due to the amount of corrosion, the opening | | was estimated to be 12.57 square inches. Additionally, damaged seals on two | | other doors (#225 and #128) located on airlocks associated with Secondary | | Containment accounted for another 7 square inches, for a total of 19.57 | | square inches. Openings in excess of 12.7 square inches in this | | configuration have not been tested/evaluated. Therefore, Secondary | | Containment was considered inoperable. Operations entered Technical | | Specification LCO 3.6.4.1, condition A, for Secondary Containment inoperable | | in Mode 1 at 0236[CDT]. Required action A.1 is to restore Secondary | | Containment to operable status in 4 hours. | | | | "Operations took actions to prohibit access through the two seal damaged | | doors/airlocks by posting them to prevent access. Once administrative | | control of the doors was established, the known opening in secondary | | containment was reduced to the corroded pipe in the SBGT sump, or 12.57 | | square inches. This is less than the 12.7 square inches allowed. Technical | | Specification LCO 3.6.4.1, condition A, was exited at 0258[CDT]." | | | | The licensee informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Wednesday, March 24, 2021