U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/28/2012 - 12/31/2012 ** EVENT NUMBERS ** | Agreement State | Event Number: 48613 | Rep Org: ILLINOIS EMERGENCY MGMT. AGENCY Licensee: PACTIV LLC Region: 3 City: FRANKLIN PARK State: IL County: License #: 9222886 Agreement: Y Docket: NRC Notified By: DAREN PERRERO HQ OPS Officer: DONG HWA PARK | Notification Date: 12/20/2012 Notification Time: 12:21 [ET] Event Date: 12/18/2012 Event Time: [CST] Last Update Date: 12/20/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): JAMNES CAMERON (R3DO) FSME EVENTS RESOURCE () | Event Text AGREEMENT STATE REPORT - SHUTTER FAILURE The following information was received via email from the Illinois Emergency Management Agency: "On December 19, 2012 this general license registrant called to advise that a shutter on one of their process gauges had failed. The registrant had discovered the failure as a result of conducting their routine 6-month safety checks of the device. A makeshift shield was placed over the beam opening following the manufacturer's instructions, pending repair. Arrangements were made to have a field engineer from the company come to the site the next day to replace the shutter. No exposures to operating personnel were reported due to the circumstances of the gauge installation and low activity of the source involved. "Source/Radioactive Material: SEALED SOURCE GAUGE "Radionuclide: AM-241, 0.025 Ci, 0.925 GBq "Manufacturer: QSA GLOBAL "Model Number: AMC.P6 "Serial Number: 7734AR" Illinois Item Number: IL12018 | Agreement State | Event Number: 48614 | Rep Org: MARYLAND DEPT OF THE ENVIRONMENT Licensee: UNIVERSITY OF MARYLAND COLLEGE PARK Region: 1 City: COLLEGE PARK State: MD County: PRINCE GEORGES License #: MD-33-004-03 Agreement: Y Docket: NRC Notified By: KENNETH BRENNEMAN HQ OPS Officer: HOWIE CROUCH | Notification Date: 12/20/2012 Notification Time: 13:46 [ET] Event Date: 12/19/2012 Event Time: 15:00 [EST] Last Update Date: 12/20/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): GORDON HUNEGS (R1DO) FSME RESOURCE (EMAI) | Event Text MARYLAND AGREEMENT STATE REPORT - IRRADIATOR SOURCE CHAIN FAILED TO FUNCTION The following information was obtained from the State of Maryland via fax: On December 19, 2012 at 1500 EST, the licensee's irradiator chain became "kinked" and failed to function as required. The sources were being raised at the time of the incident. The chain was de-kinked from around the sprocket and the elevator/sources were returned to their lowest position in the pool. The sources will remain stored at the lowest position until an internal investigation determines the cause of the event. | Power Reactor | Event Number: 48629 | Facility: LIMERICK Region: 1 State: PA Unit: [1] [2] [ ] RX Type: [1] GE-4,[2] GE-4 NRC Notified By: DAN WILLIAMSON HQ OPS Officer: CHARLES TEAL | Notification Date: 12/28/2012 Notification Time: 09:55 [ET] Event Date: 12/28/2012 Event Time: 03:30 [EST] Last Update Date: 12/28/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(xi) - OFFSITE NOTIFICATION 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): RICHARD CONTE (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text LOSS OF COMMUNICATIONS WITH ALL EMERGENCY PLANNING ZONE SIRENS "Limerick and associated local counties have lost communications with all Emergency Planning Zones (EPZ) sirens for greater than 1 hour. This exceeds the 25% notification threshold. The contract vendor is responding to the loss to determine repair actions and timeline. "The EPZ plan contains alternate methods of notifying the public in the event of an evacuation. "Notifications have been made to the State and local agencies regarding this loss of Emergency Preparedness capability at 0913 EST on 12/28/12, which constitutes the 'Offsite Notification' per 10CFR50.72(b)(2)(xi)." The licensee has notified Montgomery, Chester, Burkes counties, and the NRC Resident Inspector. * * * UPDATE AT 1258 EST ON 12/28/12 FROM DAN WILLIAMSON TO HUFFMAN * * * Communications with all EPZ sirens have been restored. The licensee will notify the affected counties and the NRC Resident Inspector. R1DO (Conte) notified. | Power Reactor | Event Number: 48635 | Facility: DRESDEN Region: 3 State: IL Unit: [ ] [2] [3] RX Type: [1] GE-1,[2] GE-3,[3] GE-3 NRC Notified By: RYAN CHAMBERLAIN HQ OPS Officer: PETE SNYDER | Notification Date: 12/28/2012 Notification Time: 18:02 [ET] Event Date: 12/28/2012 Event Time: 14:10 [CST] Last Update Date: 12/28/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.719 - FITNESS FOR DUTY | Person (Organization): ROBERT DALEY (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | 3 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text FITNESS FOR DUTY - ACCESS DENIED On December 28, 2012, at approximately 1410 hours CDT, Dresden Station was informed by Station Security that a Contract Supervisory (non-licensed) individual had a confirmed positive Fitness-For-Duty test for a controlled substance. This event affects both Dresden and Braidwood Stations. The individuals access to both Dresden and Braidwood Stations has been terminated. The licensee notified the NRC Resident Inspectors. | Power Reactor | Event Number: 48636 | Facility: SUSQUEHANNA Region: 1 State: PA Unit: [1] [2] [ ] RX Type: [1] GE-4,[2] GE-4 NRC Notified By: JAY BARNES HQ OPS Officer: DONG HWA PARK | Notification Date: 12/29/2012 Notification Time: 01:20 [ET] Event Date: 12/28/2012 Event Time: 11:00 [EST] Last Update Date: 12/29/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.719 - FITNESS FOR DUTY | Person (Organization): RICHARD CONTE (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 98 | Power Operation | 98 | Power Operation | 2 | N | Y | 18 | Power Operation | 18 | Power Operation | Event Text COMPUTER PROGRAM ERROR IDENTIFIED IN THE FITNESS FOR DUTY PROGRAM "On December 28, 2012 at approximately 1100 [EST], Susquehanna discovered a computer program error that affected the Susquehanna Fitness for Duty (FFD) program. Specifically, thirty-nine Behavioral Observation Program (BOP) inquiries were without proper documentation of the required need to continue unescorted access (UA) and without verification of an actual observation within the required thirty day timeframe. The computer error resulted in answers for two of the three questions on the Behavior Observation Inquiry form not being recorded when the form was submitted by the supervisor. This resulted in the thirty-nine security accounts being re-zeroed and allowing UA for an additional thirty days. All thirty-nine BOP supervisors were contacted, and it was determined that thirty-six of the individuals were intended to continue with UA. The remaining three accounts should have terminated to prevent UA; however, none of these three individuals gained unauthorized access to the Protected Area after their UA should have been terminated. Seven of the thirty-six intended to continue with UA did access the Protected Area, but per follow-up with the Behavior Observation Supervisors, these individuals were in compliance with the BOP. In accordance with 10 CFR 26.719(b)(4), this report is being made based on being a potential programmatic failure, degradation, or discovered vulnerability of the FFD program that may permit undetected drug or alcohol use or abuse by individuals within a protected area, or by individuals who are assigned to perform duties that require them to be subject to the FFD program. The [NRC] Resident Inspector and the Branch Chief for the Region I Division of Reactor Safety were briefed." | Power Reactor | Event Number: 48637 | Facility: GRAND GULF Region: 4 State: MS Unit: [1] [ ] [ ] RX Type: [1] GE-6 NRC Notified By: CHAD ROGERS HQ OPS Officer: VINCE KLCO | Notification Date: 12/29/2012 Notification Time: 05:05 [ET] Event Date: 12/29/2012 Event Time: 00:18 [CST] Last Update Date: 12/29/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL | Person (Organization): HEATHER GEPFORD (R4DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | A/R | Y | 100 | Power Operation | 0 | Hot Shutdown | Event Text AUTOMATIC REACTOR SCRAM DUE TO A TURBINE/GENERATOR TRIP "Actuation of RPS [Reactor Protection System] with reactor critical. Reactor Scram occurred at 0018 [CST], 12/29/12, from 100% CTP [Core Thermal Power]. The cause of scram appears to be a Generator/Turbine trip. "Appropriate off normal event procedures were entered to mitigate the transient with all systems responding as designed. No loss of offsite or ESF [engineered safety feature] power occurred. No ECCS initiation signals were reached and no ECCS or Diesel Generator initiation occurred. "MSIVs [Main Steam Isolation Valves] remained open and SRVs [Safety Relief Valves] lifted. Currently, reactor water level is being maintained by the condensate and feedwater system in normal band and reactor pressure is being controlled to limit cooldown." All control rods inserted. The plant is in hot shutdown with decay heat removal to the condenser and the electrical line-up is in a normal configuration. The cause of the turbine/generator trip is under investigation. The licensee notified the NRC Resident Inspector. | Power Reactor | Event Number: 48638 | Facility: SURRY Region: 2 State: VA Unit: [ ] [2] [ ] RX Type: [1] W-3-LP,[2] W-3-LP NRC Notified By: BRET RICKERT HQ OPS Officer: BILL HUFFMAN | Notification Date: 12/29/2012 Notification Time: 15:21 [ET] Event Date: 12/29/2012 Event Time: 08:03 [EST] Last Update Date: 12/29/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): BINOY DESAI (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text EMERGENCY DIESEL GENERATOR AUTO-START AND LOAD UPON TRIP OF RESERVE STATION TRANSFORMER "At 0803 EST on 12/29/2012 With Unit 1 and Unit 2 operating at 100%, the Supply breaker to 'B' Reserve Station Transformer (RSST), 0-EP-BKR-252 tripped on an instantaneous over current of the B-C phases due to a Pelican contacting the lines. This resulted in a lockout of the 'B' RSST and loss of power to the Unit 2 'H' Emergency Bus from its normal off site power supply. #2 Emergency Diesel Generator auto started on under voltage and loaded onto the Unit 2 'H' Emergency Bus. The Operations staff entered abnormal operating procedure 2-AP-10.07, Loss of Unit 2 Power, to recover from the electrical transient. All equipment performed as expected during the event and there were no unexplained occurrences. Maintenance has verified there is no damage to the line, breaker or 'B' RSST and at 1242 EST offsite power was restored to Unit 2 'H' Emergency Bus. At 1501, #2 Emergency Diesel Generator was secured in accordance with Station Operating procedures. "Currently Unit 1 is operating at 100%, 922 MWE. "Currently Unit 2 is operating at 100%, 915 MWE. "All electrical distribution systems were restored to a normal alignment. "No adverse radiological consequences resulted from this event. There were no radiation releases due to this event, nor were there any personnel injuries or contamination events. "This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) due to the auto start of #2 Emergency Diesel Generator." The licensee has notified the NRC Resident Inspector. | Power Reactor | Event Number: 48639 | Facility: COLUMBIA GENERATING STATION Region: 4 State: WA Unit: [2] [ ] [ ] RX Type: [2] GE-5 NRC Notified By: RICK KERRONE HQ OPS Officer: BILL HUFFMAN | Notification Date: 12/30/2012 Notification Time: 15:45 [ET] Event Date: 12/30/2012 Event Time: 05:30 [PST] Last Update Date: 12/30/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(C) - POT UNCNTRL RAD REL 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): HEATHER GEPFORD (R4DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text SECONDARY CONTAINMENT MOMENTARILY INOPERABLE "Technical Specification 3.6.4.1 (Secondary Containment) requires that the secondary containment be operable. Surveillance requirement 3.6.4.1.3 requires verifying each secondary containment access inner door or each secondary containment access outer door in each access opening is closed. "During a fire tour, a security officer proceeded through Reactor Building outer security door (R-204) and opened the inner door (R-205) prior to the outer security door completely closing. This resulted in both the Reactor Building inner and outer access doors being simultaneously open for a short duration. Normally, the doors are interlocked in which the inner door would not be able to be opened prior to the outer security door being closed. "The security officer immediately notified the Main Control Room and operations personnel verified both doors were locked and closed. The outer security door (R205) has been key-locked closed until corrective actions are determined. "Columbia Generating Station is investigating why the interlock feature failed. "There were no radiological releases associated with the event. "No safety system actuations or isolations occurred." The Licensee has notified the NRC Resident Inspector. | |