U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/21/2012 - 08/22/2012 ** EVENT NUMBERS ** | Agreement State | Event Number: 48184 | Rep Org: TENNESSEE DIV OF RAD HEALTH Licensee: NON-LICENSEE Region: 1 City: MEMPHIS State: TN County: License #: Agreement: Y Docket: NRC Notified By: ALLEN GREWE HQ OPS Officer: JOHN KNOKE | Notification Date: 08/13/2012 Notification Time: 12:29 [ET] Event Date: 08/11/2012 Event Time: [EDT] Last Update Date: 08/14/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): ART BURRITT (R1DO) FSME EVENTS RESOURCE (EMAI) | Event Text AGREEMENT STATE REPORT - INDIUM-111 VIAL DAMAGED IN SHIPMENT The following information was provided by the State of Tennessee via facsimile: "On August 11, 2012, the shipper contacted the Division of Radiological Health to report that a package containing 31.7 mCi of Indium-111 was run over in the 'courtyard' area. Caps were off all six internal shielding pigs. Vials in four pigs were intact. The fifth vial was found and returned to the pig. The sixth vial was crushed and the contents (5.3 mCi) released. The shipper's fire personnel responded and washed the area (20 to 30 feet in diameter) and released the water to the storm water runoff drain. One area about 4 inches by 4 inches could not be decontaminated. A steel plate was bolted onto the asphalt in that area and dose rates of 0.5 mR/hr at a meter was observed. This area is not an occupied area. The half-life for Indium-111 is 2.8 days. The plate will be removed in 30 days and the area will be reassessed. No injuries, [and] no personnel contamination." Event Report ID No.: TN-12-207 * * * UPDATE ON 8/14/12 AT 1456 EDT FROM BETH SHELTON TO DONG PARK * * * The following update was provided by the State of Tennessee via email: "The sixth vial was crushed and the contents (4.4 mCi) released. One area about 4 cm in diameter could not be decontaminated. A steel plate was bolted onto the asphalt in that area and dose rates of 0.05 mR/hr at a meter were observed." Notified R1DO (Powell) and FSME Events Resource via email. | Power Reactor | Event Number: 48214 | Facility: DUANE ARNOLD Region: 3 State: IA Unit: [1] [ ] [ ] RX Type: [1] GE-4 NRC Notified By: TERRY BRANDT HQ OPS Officer: DONALD NORWOOD | Notification Date: 08/21/2012 Notification Time: 06:14 [ET] Event Date: 08/21/2012 Event Time: 04:07 [CDT] Last Update Date: 08/21/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): ERIC DUNCAN (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 94 | Power Operation | 94 | Power Operation | Event Text TECHNICAL SUPPORT CENTER OUT OF SERVICE "A planned maintenance evolution at the Duane Arnold Energy Center (DAEC) will remove the emergency power supply to the TSC from service. The TSC would be rendered non-functional with the loss of emergency power. The repair to the power supply is expected to last three days. "If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures. Maintenance will be expedited to restore the emergency power supply to service. "This notification is being made in accordance with 10CFR50.72(b)(3)(xiii) due to the loss of an Emergency Response Facility (ERF). An update will be provided once the TSC emergency power supply has been restored to normal operation. "NRC Resident has been notified." | Power Reactor | Event Number: 48215 | Facility: MILLSTONE Region: 1 State: CT Unit: [ ] [2] [ ] RX Type: [1] GE-3,[2] CE,[3] W-4-LP NRC Notified By: KENNETH HAJNAL HQ OPS Officer: STEVE SANDIN | Notification Date: 08/21/2012 Notification Time: 07:50 [ET] Event Date: 08/21/2012 Event Time: 00:38 [EDT] Last Update Date: 08/21/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): WILLIAM COOK (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | N | 0 | Cold Shutdown | 0 | Cold Shutdown | Event Text BOTH EMERGENCY DIESEL GENERATORS INOPERABLE At 0038 EDT on 08/21/12, EDG "A" was declared Inoperable after the Engineered Safeguards Actuation System (ESFAS) fuse failed . EDG "B" had been Inoperable for planned maintenance since 2223 EDT on 08/15/12. With both EDGs Inoperable, Unit 2 entered Tech Spec LCO 3.8.1.2 which requires suspension of all operations involving core alteration and positive reactivity additions. At 0713 EDT on 08/21/12, the licensee declared EDG "B" Operable exiting the Tech Spec LCO. The cause of the ESFAS fuse failure on EDG "A" is under investigation. The licensee will notify state and local agencies and has informed the NRC Resident Inspector. | Power Reactor | Event Number: 48217 | Facility: SUMMER CONSTRUCTION Region: State: SC Unit: [2] [3] [ ] RX Type: NRC Notified By: GARRETT SANDERS HQ OPS Officer: DONALD NORWOOD | Notification Date: 08/21/2012 Notification Time: 10:45 [ET] Event Date: 08/20/2012 Event Time: 15:30 [] Last Update Date: 08/21/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.719 - FITNESS FOR DUTY | Person (Organization): EUGENE GUTHRIE (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | N | 0 | | 0 | | 3 | N | N | 0 | | 0 | | Event Text FITNESS FOR DUTY POLICY VIOLATION A non-licensed contract employee supervisor and a non-licensed contract employee committed a Fitness-For-Duty policy violation. Construction area access for both contract employees have been suspended, and the licensee has initiated an investigation. Contact the Headquarters Operations Officer for additional details. The NRC Resident Inspector has been notified of this event. | Power Reactor | Event Number: 48219 | Facility: BRUNSWICK Region: 2 State: NC Unit: [1] [2] [ ] RX Type: [1] GE-4,[2] GE-4 NRC Notified By: LEE GRZECK HQ OPS Officer: JOHN SHOEMAKER | Notification Date: 08/21/2012 Notification Time: 20:13 [ET] Event Date: 08/21/2012 Event Time: 19:30 [EDT] Last Update Date: 08/21/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(xi) - OFFSITE NOTIFICATION | Person (Organization): ROBERT HAAG (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text DAMAGED PACKAGING CONTAINING RADIOACTIVE MATERIAL "In accordance with 49 CFR 171.15, Duke Energy contacted the Department of Transportation National Response Center at 1930 [EDT] on August 21, 2012, Report Number 1021811, to inform them of a breach of a package containing a limited quantity of radioactive material. This breach was considered 'breakage' in accordance with Title 49 of the Code of Federal Regulations, Transportation. Although the packaging of the radioactive material was damaged during transportation, the radioactive material itself was not released, and the damage did not result in any external radioactive contamination or any radiation exposure. This event did not result in any adverse impact to the health and safety of the public. The State of North Carolina (NC) has also been notified of this event. Mecklenburg County, NC will be notified of this event. "This event is being reported in accordance with 10 CFR 50.72(b)(2)(xi) as a result of the notification to another government agency. "The safety significance of the breached package is minimal. "The condition will be entered into the Corrective Action Program for evaluation. Corrective actions will be determined based on the results of this evaluation." The container held a torque wrench calibration test tool and cable. The tools had penetrated the container, but no other damage to the tools was noted. The tools will be normally processed for use at the station. The licensee has notified the NRC Resident Inspector. | Power Reactor | Event Number: 48220 | Facility: THREE MILE ISLAND Region: 1 State: PA Unit: [1] [ ] [ ] RX Type: [1] B&W-L-LP,[2] B&W-L-LP NRC Notified By: WILLIAM PRICE HQ OPS Officer: DONALD NORWOOD | Notification Date: 08/22/2012 Notification Time: 03:53 [ET] Event Date: 08/22/2012 Event Time: 02:28 [EDT] Last Update Date: 08/22/2012 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(i) - PLANT S/D REQD BY TS | Person (Organization): WILLIAM COOK (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text TECH SPEC REQUIRED SHUTDOWN DUE TO REACTOR COOLANT SYSTEM PRESSURE BOUNDARY LEAK "On August 22, 2012, it was determined, based on a remote video camera inspection inside the secondary shield wall, that a primary system leak at a Pressurizer Heater bundle exists and is not isolable. Technical Specification (TS) Limiting Condition for Operation (LCO) 3.1.6.4 does not allow any leakage through a nonisolable RCS strength boundary. The discovery of leakage from the Pressurizer Heater bundle is considered a degradation of a principal safety barrier. This condition does not represent a reduction in the public health and safety. "This is reportable as a 4-hour ENS notification under 10CFR50.72(b)(2)(i) due to the initiation of a nuclear plant shutdown required by the plant's Technical Specifications. "The licensee notified the NRC Resident Inspector." The licensee expects to also notify state and local government agencies of the shutdown. The current leak rate, as calculated by the plant process computer, is approximately .2 gallons per minute. | |