Event Notification Report for May 9, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/08/2003 - 05/09/2003 ** EVENT NUMBERS ** 39824 39832 39833 39834 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39824 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: SC DIV OF HEALTH & ENV CONTROL |NOTIFICATION DATE: 05/05/2003| |LICENSEE: STERIS-ISOMEDIX SERVICES |NOTIFICATION TIME: 16:25[EDT]| | CITY: SPARTENBURG REGION: 2 |EVENT DATE: 05/05/2003| | COUNTY: STATE: SC |EVENT TIME: 11:30[EDT]| |LICENSE#: 267 AGREEMENT: Y |LAST UPDATE DATE: 05/05/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOEL MUNDAY R2 | | |TOM ESSIG NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DAVID KING | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MALFUNCTIONING IRRADIATOR CARRIER DOOR HINGE PIN ASSEMBLY | | | | Steris-Isomedix Services reported to the state that they had an incident | | where the hinge pin assembly on the carrier door of an irradiator | | malfunctioned. This resulted in the door opening and jamming at the source | | rack which in turn left the source in a fully unshielded position. The | | operator then went to the hoist cables for the source rack, which is in a | | shielded area, moved the cables around a bit and unjammed the source rack | | returning the source to the fully shielded position. The amount of time | | taken to return the source to the fully shielded position was approximately | | 20-30 minutes. The licensee is shutting down all irradiators to check the | | hinge pin assemblies. There were no exposures. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39832 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GRAND GULF REGION: 4 |NOTIFICATION DATE: 05/08/2003| | UNIT: [1] [] [] STATE: MS |NOTIFICATION TIME: 10:40[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 05/08/2003| +------------------------------------------------+EVENT TIME: 08:00[CDT]| | NRC NOTIFIED BY: BRIAN BLANCHE |LAST UPDATE DATE: 05/08/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |LINDA SMITH R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EMERGENCY SIREN ACCIDENTLY INITIATED. | | | | The Claiborne County Civil Defense department inadvertently initiated an | | emergency siren. The siren has been secured, and a "No Emergency" message | | has been issued to the local media. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 39833 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GLOBAL NUCLEAR FUEL - AMERICAS |NOTIFICATION DATE: 05/08/2003| | RXTYPE: URANIUM FUEL FABRICATION |NOTIFICATION TIME: 16:16[EDT]| | COMMENTS: LEU CONVERSION (UF6 TO UO2) |EVENT DATE: 05/08/2003| | LEU FABRICATION |EVENT TIME: 04:00[EDT]| | LWR COMMERICAL FUEL |LAST UPDATE DATE: 05/08/2003| | CITY: WILMINGTON REGION: 2 +-----------------------------+ | COUNTY: NEW HANOVER STATE: NC |PERSON ORGANIZATION | |LICENSE#: SNM-1097 AGREEMENT: Y |PAUL FREDRICKSON R2 | | DOCKET: 07001113 |ERIC LEEDS NMSS | +------------------------------------------------+JOHN JOLICOEUR IRO | | NRC NOTIFIED BY: RICK FOLECK | | | HQ OPS OFFICER: HOWIE CROUCH | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |KSAF 70.50(b)(2) SAFETY EQUIPMENT FAILUR| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY EQUIPMENT FAILURE DUE TO SEVERE THUNDERSTORM CONDITIONS | | | | The following information was received from the licensee via facsimile: | | | | "At approximately 4:00 a.m. [EDT] on May 8, 2003, the Criticality Warning | | System (CWS) coverage was temporarily lost due to severe thunderstorm | | conditions. The two Data Acquisition Modules (DAMS) providing redundant | | criticality detector coverage of the Dry Conversion Process (DCP) plant area | | were simultaneously lost. Additional isolated DAM failures occurred at | | other locations, but CWS coverage was maintained for the remainder of the | | facility. | | | | "In DCP, operations were suspended, and all movement of fissile material was | | halted. Personnel were restricted from affected plant areas. Maintenance | | instrumentation personnel diagnosed and successfully restored CWS coverage | | for the DCP plant area at approximately 7:00 a.m. Normal plant operations | | were resumed at approximately 9:30 a.m. Restoration of remaining redundant | | CWS coverage for all areas was completed at 11:45 a.m. | | | | "This condition is reported pursuant to 10CFR70.50(B)(2) as an event in | | which equipment is disabled or fails to function as designed when required | | by license or regulation to be available to mitigate the consequences of an | | accident. Incident investigation and evaluation of additional corrective | | actions pending." | | | | Licensee will be notifying New Hanover County Emergency Management, North | | Carolina Department of Radiation Protection, NRC Region 2 and NRC | | Headquarters Global Nuclear Fuels Project Manager. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39834 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: WOLF CREEK REGION: 4 |NOTIFICATION DATE: 05/08/2003| | UNIT: [1] [] [] STATE: KS |NOTIFICATION TIME: 21:53[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 05/08/2003| +------------------------------------------------+EVENT TIME: 19:30[CDT]| | NRC NOTIFIED BY: RICK HUBBARD |LAST UPDATE DATE: 05/08/2003| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |LINDA SMITH R4 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF FIVE EMERGENCY SIRENS DUE TO POWER OUTAGE | | | | The following information was obtained from the licensee via facsimile: | | | | "On 05/08/2003 at 1840 CDT, the National Weather Service in Topeka, KS | | declared a Tornado Warning for the area around Wolf Creek Generating | | Station. The Tornado Warning was in effect until 1930 CDT. The storm cell | | moved through Burlington, KS, approximately 6 miles southwest of the | | facility, causing power to be lost to the city of Burlington. Plant | | Security notified the Control Room that the loss of power to Burlington had | | caused power to be lost to five (5) E-Plan Sirens and an intrusion alarm on | | one additional E-Plan Siren. This information was relayed to Security via | | the installed telemetric monitoring system. At this time, Burlington is | | without power and the sirens remain without power." | | | | There is no ETA for power restoration. | | | | The licensee has informed the NRC Resident Inspector and the local | | authorities. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021