Event Notification Report for April 2, 2002
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/01/2002 - 04/02/2002 ** EVENT NUMBERS ** 38602 38819 38820 38821 38822 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38602 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CRYSTAL RIVER REGION: 2 |NOTIFICATION DATE: 01/01/2002| | UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 10:08[EST]| | RXTYPE: [3] B&W-L-LP |EVENT DATE: 01/01/2002| +------------------------------------------------+EVENT TIME: 09:19[EST]| | NRC NOTIFIED BY: BILL BANDHAUER |LAST UPDATE DATE: 04/02/2002| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ANNE BOLAND R2 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFFSITE NOTIFICATION DUE RESCUED SEA TURTLE | | | | EN #37902 started the biennial report period. | | | | On January 1, 2002 at 0919, a rescued sea turtle was identified as a green | | sea turtle. This is the 62nd rescue of a live sea turtle at Crystal River | | Unit 3 (CR-3) in this biennial period. Notification to the National Marine | | Fisheries Service and the Florida Fish and Wildlife Conservation Commission. | | | | | | The licensee intends to notify the NRC Resident Inspector. | | | | * * * UPDATE ON 1/05/02 @ 1002 BY RAWLS TO GOULD * * * | | | | On January 5, 2002, at 0720, a rescued sea turtle was identified as a | | Loggerhead Sea Turtle. This is the 63rd rescue of a live sea turtle at | | Crystal River Unit 3 (CR3) in this biennial period. This is reportable as a | | 4-hour report under 10 CFR 50.72(b)(2)(xi) as this event is related to the | | protection of the environment for which a notification to other government | | agencies (National Marine Fisheries Service and Florida Fish and Wildlife | | Conservation Commission) has been or will be made. | | | | The NRC Resident Inspector was notified. | | | | Reg 2 RDO (Decker) was notified. | | | | * * * UPDATE ON 01/09/02 @ 1107 EST BY ANDY BARNES TAKEN BY MACKINNON * * * | | | | On January 9, 2002, at 0838, a rescued sea turtle was identified as a Kemp's | | Ridley Sea Turtle. This is the 64th rescue of a live turtle at Crystal River | | Unit 3 (CR-3) in this biennial period. This is reportable as a 4-hour 10 CFR | | 50.72 (b)(2)(xi) as this event is related to the protection of the | | environment for which a notification to other government agencies (National | | Marine Fisheries Service and Florida Fish and Wildlife Conservation | | Commission) has been or will be made. | | | | The NRC Resident Inspector was notified. | | | | Reg 2 (Brian Bonser) was notified. | | | | * * * UPDATE ON 02/17/02 at 0940 EST BY RICKY RAWLS TO FANGIE JONES * * * | | | | "On February 17, 2002 at 0820, a rescued injured sea turtle was identified | | as a Kemp's Ridley Sea Turtle. The injury will require transportation to | | Clearwater Marine Science Center or Florida Fish and Wildlife Conservation | | Refuge. The Injury appears to be from a boat propeller. This is the 65th | | rescue of a live sea turtle at Crystal River Unit 3 (CR-3) in this biennial | | period. This is Reportable as a 4-Hour Report under 10 CFR 50.72(b) (2) (xi) | | as this event is related to the protection of the environment for which a | | notification to other government agencies (National Marine Fisheries Service | | and Florida Fish and Wildlife Conservation Commission) has been or will be | | made. This Is an update to event 38602." | | | | The NRC Resident Inspector will be notified. R2DO (Stephen Cahill) has been | | notified. | | | | * * * UPDATE ON 03/01/02 AT 1122 EST BY RICKY RAWLS TO GERRY WAIG * * * | | | | "On March 1, 2002 at 0952, a healthy rescued sea turtle was identified as a | | Green Sea Turtle. This is the 66th rescue of a live sea turtle at Crystal | | River Unit 3 (CR-3) in this biennial period. This is Reportable as a 4-Hour | | Report under 10 CFR 50.72 (b) (2) (xi) as this event is related to the | | protection of the environment for which a notification to other government | | agencies (National Marine Fisheries Service and Florida Fish and Wildlife | | Conservation Commission) has been or will be made. This is an update to | | event 38602." | | | | The NRC Resident Inspector was notified. R2DO (Julian) was notified. | | | | * * * UPDATE ON 03/07/02 AT 1114 EST BY CHUCK MORRIS TO MIKE NORRIS * * * | | | | "On March 7, 2002 at 0835, two healthy sea turtles rescued at CR#3 were | | identified as Green Sea Turtles. These are the 67th and 68th live sea turtle | | rescues at the Crystal River Energy Complex in this biennial period. This is | | Reportable as a 4-Hour Report under 10 CFR 50.72(b) (2) (xi) as this event | | is related to the protection of the environment for which a notification to | | other government agencies (National Marine Fisheries Service and Florida | | Fish and Wildlife Conservation Commission) has been or will be made. This is | | an update to event 38602." | | | | The NRC Resident Inspector was notified. R2DO (Henson) was notified. | | | | * * * UPDATE ON 04/02/02 at 0408 EST BY RICKY RAWLS TO FANGIE JONES * * * | | | | "On April 2, 2002 at 0236, two sea turtles previously rescued at CR#3 intake | | area were identified by FPC Mariculture staff as Kemp Ridley Sea Turtles. | | One of the turtles appears to be in distress and may require transportation | | to Clearwater Marine Science Center of Florida Fish and Wildlife | | Conservation Refuge. These are the 69th and 70th live sea turtle rescues at | | the Crystal River Energy Complex in this biennial period. This is Reportable | | as a 4-Hour Report under 10 CFR 50.72(b) (2) (xi) as this event is related | | to the protection of the environment for which a notification to other | | government agencies (National Marine Fisheries Service and Florida Fish and | | Wildlife Conservation Commission) has been or will be made. This is an | | update to event 38602." | | | | The NRC Resident Inspector will be notified. The R2DO (Carolyn Evans) was | | notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38819 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 04/01/2002| | UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 13:05[EST]| | RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 04/01/2002| +------------------------------------------------+EVENT TIME: 09:17[CST]| | NRC NOTIFIED BY: THOMAS JESSESSKY |LAST UPDATE DATE: 04/01/2002| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DAVID HILLS R3 | |10 CFR SECTION: | | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NITROGEN BACKUP SYSTEM FOR CHARGING PUMP SPEED CONTROL FOUND NOT TO SATISFY | | APPENDIX R FIRE ASSUMPTION. | | | | At 0917 CT on 04/01/02, it was determined that a condition identified on | | 03/28/02 potentially represents a significant degradation of plant safety | | during response to an Appendix R event. The Appendix R credited nitrogen | | backup system for charging pump speed control is unable to satisfy its | | design function of controlling Charging System flow to the Reactor Coolant | | System (RCS) for the time required to place the plant in Mode 5 (Cold | | Shutdown). During an Appendix R fire it is assumed that the normal motive | | force (instrument air) for charging control is unavailable and an installed | | backup is credited. This installed nitrogen system allows inventory control | | while in Mode 3 (Hot Standby) and is used to control RCS inventory and | | pressure while the RCS is cooled down and depressurized from Mode 3 (Hot | | Standby) to Mode 5 (Cold Shutdown). A nitrogen bottle 12-pack is calculated | | to last for approximately 8 hours. PBNP has 1 spare approved nitrogen pack | | on site - - it has been calculated that up to 15 spares would be required | | for 72 hours of charging pump operation. Mode 5 (Cold Shutdown) is expected | | to be reached in 30 hours but may be as long as 72 hours. | | | | This issue places the plant in an unanalyzed condition that has the | | potential to significantly degrade plant safety (RCS Inventory Control) and | | thus is reportable. | | | | The associated charging pumps have been declared out of service for Appendix | | R use and compensatory actions undertaken that establish appropriate fire | | rounds. Fire rounds will be continued until the condition is corrected or a | | suitable evaluation is completed. | | | | The NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38820 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 04/01/2002| | UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 18:46[EST]| | RXTYPE: [1] GE-3 |EVENT DATE: 04/01/2002| +------------------------------------------------+EVENT TIME: 14:36[CST]| | NRC NOTIFIED BY: DUANE BISTODEAU |LAST UPDATE DATE: 04/01/2002| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DAVID HILLS R3 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DURING SURVEILLANCE TEST "A" DIVISION OF CONTROL ROOM VENTILATION SYSTEM | | FAILED TO AUTOSTART ON A LOW FLOW SIGNAL. | | | | | | At 1436 CT on 04/01/02, during a low flow start surveillance test the "A" | | division of the Control Room Ventilation System failed to autostart. At the | | time, the "B" division was disabled in order to perform the test. Thus, the | | Control Room Ventilation System accident mitigation function was lost. | | Division "B" Control Room Ventilation was restored to operability at 1600 | | hours CT. The "A" division is operating with the control switch in the run | | mode. The cause of the failure to Autostart is under investigation. | | | | The NRC Resident Inspection will be notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38821 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OCONEE REGION: 2 |NOTIFICATION DATE: 04/01/2002| | UNIT: [1] [] [] STATE: SC |NOTIFICATION TIME: 21:23[EST]| | RXTYPE: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-L|EVENT DATE: 04/01/2002| +------------------------------------------------+EVENT TIME: 18:00[EST]| | NRC NOTIFIED BY: STEVE GODFREY |LAST UPDATE DATE: 04/01/2002| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |CAROLYN EVANS R2 | |10 CFR SECTION: |JOHN HANNON NRR | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | CONTROL ROD DRIVE MECHANISM NOZZLE NO. 7 PENETRATION FOUND TO HAVE A SMALL | | LEAK PATH. | | | | Qualified visual inspection of the Unit 1 reactor vessel head Control Rod | | Drive Mechanism head penetrations found two penetrations with very slight | | boron accumulations. Ultrasonic testing of these penetrations has | | determined that one nozzle (No. 7, near the center of the reactor vessel | | head) has a potential reactor coolant system leak path. Any reactor coolant | | system leakage from penetration No. 7 would have been so small it would be | | below the threshold of measurability by the reactor coolant system leakage | | measurement processes. The leaking nozzle will be repaired prior to restart | | from the present refueling outage. | | | | The NRC Resident Inspector will be notified by the licensee of this event. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 38822 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 04/02/2002| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 00:49[EST]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 04/02/2002| +------------------------------------------------+EVENT TIME: 00:29[EST]| | NRC NOTIFIED BY: ROGER LONGLEY |LAST UPDATE DATE: 04/02/2002| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |GLENN MEYER R1 | |10 CFR SECTION: |JOHN HANNON NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |NADER MAMISH IRO | | |KEN SWEETSER FEMA | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO FIRE SUPPRESSION SYSTEM CO2 DISCHARGE IN | | TURBINE BUILDING | | | | The licensee declared an unusual event at 0029 EST due to a broken hose reel | | on the turbine building fire suppression CO2 system during work activities. | | The turbine building, reactor building, radioactive waste building, and | | control building were evacuated. The control room was not evacuated. The | | broken hose reel was isolated to terminate the release of CO2. No personnel | | injuries were identified as a result of the event. | | | | The NRC Resident Inspector will be notified by the licensee. | | | | * * * UPDATE ON 4/2/02 AT 0123 BY ROGER LONGLEY TO GERRY WAIG * * * | | | | The licensee terminated the unusual event at 0120 EST. | | | | Notified R1DO (Glenn Meyer), NRR EO (Hannon) and FEMA (Ken Sweetser) | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021