Event Notification Report for August 3, 1999
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/02/1999 - 08/03/1999 ** EVENT NUMBERS ** 35980 35981 35982 35983 35984 35985 35986 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35980 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SURRY REGION: 2 |NOTIFICATION DATE: 08/02/1999| | UNIT: [1] [2] [] STATE: VA |NOTIFICATION TIME: 09:58[EDT]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 08/02/1999| +------------------------------------------------+EVENT TIME: 09:15[EDT]| | NRC NOTIFIED BY: BILL WEBSTER |LAST UPDATE DATE: 08/02/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |ROBERT HAAG R2 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY THAT PREVENTS A 3 HOUR FIRE BARRIER FROM MEETING ITS DESIGN | | | | "On 7/26/99 a 3-5/8 inch gap approximately 7 feet long was identified to | | exist between the Auxiliary Building (Fire Area #17) and the #2 Mechanical | | Equipment Room (Fire Area #31). A deviation report was submitted on the | | above date for this condition. On 8/2/99 following additional evaluation by | | the plant staff, it was determined that this gap would have prevented this | | fire barrier from meeting its 3-hour fire rating. This condition is | | considered to have existed since original design and construction of the | | plant. This condition constitutes a condition outside the Appendix R design | | basis of the plant. This condition is being reported pursuant to | | 10CFR5O.72(b)(1)(ii)(B). A continuous fire watch has been established on | | one side of the affected fire barrier as a compensatory measure in | | accordance with the station Appendix R Program." | | | | The discovery occurred during a quarterly inspection in an area that was | | difficult to access normally. The corrective actions have been determined | | and will be completed before the fire watch is removed. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35981 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALISADES REGION: 3 |NOTIFICATION DATE: 08/02/1999| | UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 12:03[EDT]| | RXTYPE: [1] CE |EVENT DATE: 08/01/1999| +------------------------------------------------+EVENT TIME: 15:25[EDT]| | NRC NOTIFIED BY: MALONE |LAST UPDATE DATE: 08/02/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |GEOFFREY WRIGHT R3 | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 99 Power Operation |99 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DROWNING FATALITY IN LAKE MICHIGAN | | | | THE LICENSEE MADE AN INFORMATION CALL OF A DROWNING FATALITY IN LAKE | | MICHIGAN WHICH OCCURRED NEAR THE PALISADES PLANT. ACCESS TO THE VICTIM BY | | EMERGENCY VEHICLE WAS OBTAINED THROUGH THE PLANT PROTECTED AREA. THE | | LICENSEE DID NOT ISSUE ANY PRESS RELEASES, BUT THE MEDIA DID MENTION THE | | PLANT IN ITS REPORTS. | | | | THE NRC RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 35982 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 08/02/1999| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:17[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/02/1999| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 12:22[CDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 08/02/1999| | CITY: PADUCAH REGION: 3 +-----------------------------+ | COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION | |LICENSE#: GDP-1 AGREEMENT: Y |MARK RING R3 | | DOCKET: 0707001 |DON COOL NMSS | +------------------------------------------------+AARON DANIS IAT | | NRC NOTIFIED BY: JONES |JOSEPH GIITTER IRO | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | BOMB THREAT AT LANDFILL | | | | THE LICENSEE REPORTED AN UNCLASSIFIED EMERGENCY, AS A COURTESY NOTIFICATION, | | THAT THERE WAS A POTENTIAL BOMB THREAT, WHICH HAS NOT YET REACHED THE | | CREDIBLE STATE, AT A LANDFILL NORTH OF THE PLANT. THIS THREAT IS BASED ON | | UNIDENTIFIED AND SUSPICIOUS ITEMS BEING FOUND AT THE LANDFILL. THE LOCAL | | POLICE BOMB SQUAD IS RESPONDING. NO PROTECTIVE ACTION IS RECOMMENDED AT | | THIS TIME, SIRENS HAVE NOT BEEN ACTIVATED, NO EAS MESSAGE WAS REQUIRED AND | | NO RELEASES HAVE OCCURRED. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED ALONG WITH THE COUNTY AND STATE DISASTER | | AND EMERGENCY SERVICES, AND DOE. | | | | *** UPDATE ON 8/2/99 @ 1526 BY JONES TO GOULD *** | | | | THE POLICE BOMB SQUAD WILL EVALUATE THE SUSPICIOUS ITEMS AT THE SITE. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | | | | *** UPDATE ON 8/2/99 @ 1617 BY JONES TO GOULD *** | | | | THE POLICE BOMB SQUAD DETERMINED THE CONTAINERS AT THE LAND FILL CONTAINED | | ANTIFREEZE, THE EMERGENCY WAS TERMINATED AT 1458 CDT. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. THE NMSS EO(MOORE) AND THE REG 3 | | RDO(RING) AND DANIS(IAT) WERE NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35983 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: BRAIDWOOD REGION: 3 |NOTIFICATION DATE: 08/02/1999| | UNIT: [1] [2] [] STATE: IL |NOTIFICATION TIME: 16:43[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/02/1999| +------------------------------------------------+EVENT TIME: 14:45[CDT]| | NRC NOTIFIED BY: DORAZIO |LAST UPDATE DATE: 08/02/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |MARK RING R3 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST SECURITY KEY. COMPENSATORY MEASURES TAKEN. SEE LOG FOR ADDITIONAL | | INFORMATION. | | | | THE RESIDENT INSPECTOR WAS NOTIFIED. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35984 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 08/02/1999| | UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 17:21[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/02/1999| +------------------------------------------------+EVENT TIME: 15:53[CDT]| | NRC NOTIFIED BY: SEWEEL |LAST UPDATE DATE: 08/02/1999| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |TOM STETKA R4 | |10 CFR SECTION: | | |AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLATFORM GRATING CLAMPS(FASTENERS) APPEAR NOT TO BE SEISMICALLY QUALIFIED. | | | | THE LICENSEE HAS DETERMINED THAT THE PLATFORM GRATING CLAMPS DO NOT APPEAR | | TO HAVE BEEN QUALIFIED FOR THE REQUIREMENTS OF A SEISMIC CATEGORY 1 | | COMPONENT WHEN LOADED. WITH THE GRATINGS UNLOADED, HOWEVER, THIS CONDITION | | DOES NOT AFFECT THE ABILITY OF SAFETY RELATED SYSTEMS TO PERFORM THERE | | INTENDED FUNCTIONS DURING A DESIGN BASIS EARTHQUAKE. ENGINEERING IS | | CONTINUING TO EVALUATE THIS CONDITION. | | | | THE RESIDENT INSPECTOR WILL BE NOTIFIED | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 35985 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 08/02/1999| | UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 23:46[EDT]| | RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/02/1999| +------------------------------------------------+EVENT TIME: 22:35[EDT]| | NRC NOTIFIED BY: JOHN HUNTER |LAST UPDATE DATE: 08/02/1999| | HQ OPS OFFICER: FANGIE JONES +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: N/A |RICHARD BARKLEY R1 | |10 CFR SECTION: | | |DDDD 73.71 UNSPECIFIED PARAGRAPH | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFEGUARDS SYSTEM DEGRADATION RELATED TO VITAL AREA BOUNDARY. COMPENSATORY | | MEASURES TAKEN UPON DISCOVERY. THE LICENSEE INFORMED THE NRC RESIDENT | | INSPECTOR. CONTACT THE OPERATIONS CENTER FOR ADDITIONAL DETAILS. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 35986 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: U.S. STEEL, GARY WORKS |NOTIFICATION DATE: 08/03/1999| |LICENSEE: U.S. STEEL |NOTIFICATION TIME: 04:55[EDT]| | CITY: GARY REGION: 3 |EVENT DATE: 08/02/1999| | COUNTY: LAKE STATE: IN |EVENT TIME: 20:58[CDT]| |LICENSE#: GA458-3G AGREEMENT: N |LAST UPDATE DATE: 08/03/1999| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MARK RING R3 | | |CHARLEY HAUGHNEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: DEAN LARSON | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: N/A | | |10 CFR SECTION: | | |NDAM DAMAGED GAUGE/DEVICE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POSSIBLE DAMAGED THICKNESS GAUGE | | | | The licensee reported a strip break on the #6 continuous galvanizing line | | struck a NDS Model #200 (Serial #2061T) thickness gauge and knocked it from | | its mount. The gauge contains a sealed source of 2 curies of Americium-241. | | The area was isolated and a survey and wipe test indicated normal readings | | as indicated by recent surveys. The licensee notified its contractor, Val | | Met, who will actually go the plant to move the gauge and verify any actual | | damage to the gauge. Val Met is the company that replaced NDS. | | | | No injuries, personnel exposures, or contamination occurred in this | | incident. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021