NUREG 0933
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The objective of this task was to reduce the sensitivity of B&W plants to feedwater transients, with emphasis on the overcooling transients that had been observed at B&W operating plants. ITEM II.E.5.1: DESIGN EVALUATION DESCRIPTION Historical Background …
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The objective of this task was to clarify deficiency report requirements to obtain uniform reporting and earlier identification and correction of problems. ITEM II.J.4.1: REVISE DEFICIENCY REPORTING REQUIREMENTS DESCRIPTION This TMI Action Plan [1] item …
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The objective of this task was to upgrade the emergency preparedness of nuclear power plants. Specific criteria to meet this objective were delineated in NUREG-0654. [1] ITEM III.A.2.1: AMEND 10 CFR 50 AND 10 CFR 50, APPENDIX E The four parts of this item …
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DESCRIPTION Historical Background A memorandum [1] from AEOD to NRR dated May 23, 1980 drew attention to the generic issue of BWR jet pump integrity. The concern that motivated the AEOD memo was a February 1980 jet pump failure at Dresden Unit 3, together …
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DESCRIPTION This issue concerns the slow loss of control air pressure in the scram system of BWRs. [1] Air pressure dropping at a certain rate will first allow some of the CRD scram outlet valves to open slightly, thus filling the scram discharge volume …
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DESCRIPTION Historical Background On June 28, 1980, during a routine shutdown of the Browns Ferry Unit 3 reactor, a manual scram from approximately 36% power failed to insert about 40% of the control rods. Two additional manual scrams followed by an …
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DESCRIPTION Historical Background In January 1982, AEOD published a report (AEOD/C201 [1] ) on safety concerns associated with reactor vessel level instrumentation in BWRs. The report was forwared to NRR for further action. Safety Significance BWRs use …
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DESCRIPTION Historical Background This issue was identified at an NRC Operating Reactor Events meeting on January 7, 1982, [1] and addressed fire protection system (FPS) actuations that resulted in adverse interactions with safety-related equipment at …
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DESCRIPTION Historical Background On March 18, 1983, B&W expressed [1] concern for unanalyzed reactor vessel thermal stress that could occur during natural convection cooldown of PWRs. The concern emerged from a preliminary B&W evaluation of a voiding …
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DESCRIPTION Historical Background On August 18, 1982, the ACRS issued a letter [1] to the Commission which: (1) identified deficiencies in the maintenance and testing of engineered safety features designed to maintain control room habitability; (2) …
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DESCRIPTION Historical Background This concern was raised by an NRC resident inspector who questioned the practice of leaving the refueling canal drain valve in the closed position during operations at H. B. Robinson Unit 2. [1] A subsequent investigation …
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DESCRIPTION Historical Background Issue 50 addressed several areas of concern with BWR water level instrumentation and its resolution involved voluntary implementation of water level measurement improvements for all of the staff concerns, except the one …
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DESCRIPTION Historical Background In January 1984, AEOD issued a special study report (AEOD/S401) [1] describing the number of events that resulted from human error in identification of the correct unit or train. This study focused on LERs issued during …
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DESCRIPTION Historical Background Issue B-63, which was resolved and implemented as MPA B-45, required leak-testing of the check valves that isolate those low pressure systems that are connected to the RCS outside the containment. However, except for …
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DESCRIPTION Historical Background Combustible gases such as H 2 , propane, and acetylene are used during normal operations of nuclear power plants in limited quantities and for relatively short periods of time. H 2 , the most prevalent of these gases in …
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DESCRIPTION Historical Background This issue was identified in a DSIR/RES memorandum [1] which addressed the concern for the reliability of breakers used to trip the recirculation pumps at high pressure or low water level signals during ATWS mitigation in …
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The results of ongoing staff-sponsored research which culminated in the assessment of risk at five U.S. nuclear reactors (NUREG-1150 [1] ) indicated that, for the Peach Bottom MARK I containment, the core-melt probability was relatively low. However, it …
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Issue Identification The NRC identified [1] this issue in June 1992 to address an NRC staff members concern, given in a DPO dated December 3, 1991, [2] and modified March 27, 1992, [3] about the potential for a main steamline break (MSLB) accident to …
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DESCRIPTION Historical Background At 6:53 a.m. on February 7, 1993, an intruder drove into the TMI site owner-controlled area, through a gate into the protected area of Unit 1, and crashed through a roll-up door on the turbine building. TMI security …
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This task was developed to assure that the number and capabilities of the staff at nuclear power plants are adequate to provide safe operation. To meet this goal, consideration will be given to: (1) the numbers and functions of the staff needed to safely …
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