Information Notice No.90-55: Recent Operating Experience on Loss ofReactor Coolant Inventory While In a Shutdown Condition
UNITED STATES NUCLEAR REGULATORY COMMISSION OFFICE OF NUCLEAR REACTOR REGULATION WASHINGTON, D.C. 20555 AUGUST 31, 1990 Information Notice No. 90-55: RECENT OPERATING EXPERIENCE ON LOSS OF REACTOR COOLANT INVENTORY WHILE IN A SHUTDOWN CONDITION Addressees: All holders of operating licenses or construction permits for nuclear power reactors. Purpose: This information notice is being provided to alert addressees to recent operating experience involving losses of reactor coolant inventory caused by deficiencies in human performance while in a shutdown condition. It is expected that recipients will review the information for applicability to their facilities and consider actions, as appropriate, to avoid similar problems. However, suggestions contained in this information notice do not constitute NRC requirements; therefore, no specific action or written response is required. Background: A number of NRC generic communications have been written describing events at operating reactor facilities involving inadvertent loss of reactor coolant inventory while in shutdown conditions (e.g., IN 84-81, "Inadvertent Reduction In Primary Coolant Inventory In Boiling Water Reactors During Shutdown and Startup" and IN 86-74, "Reduction of Reactor Coolant Inventory Because of Misalignment of RHR Valves"). IN 90-25, "Loss Of Vital AC Power With Subsequent Reactor Coolant System Heat-up" describes a March 20, 1990 event at Vogtle Unit 1 in which a significant event occurred during shutdown conditions in which human performance played an important role. Generic Letter 88-17, "Loss Of Decay Heat Removal", stated that these types of events indicated an apparent lack of a complete industry understanding of the potential seriousness of such events with the reactor in a shutdown condition. Description of Circumstances: The following are examples of recent events that were caused or initiated by deficiencies in human performance with the reactor in a shutdown condition. CATAWBA 1, 6/11/90 At Catawba Unit 1, on June 11, 1990, 5000 gallons of water from the reactor coolant system (RCS) were transferred inadvertently to the 9008270047 . IN 90-55 August 31, 1990 Page 2 of 3 refueling water storage tank (RWST). This coolant was transferred because the reactor operator ordered isolation valves to be opened while performing Residual Heat Removal (RHR) check valve testing before ensuring that the manual isolation valve to the RWST was closed. The loss of RCS inventory occurred over a 30 second period while a motor-operated cross-tie RHR isolation valve was partially open. MAINE YANKEE, 6/4/90 While performing the RCS fill and vent procedure with the reactor in cold shutdown, the licensee inadvertently transferred 6000 gallons of coolant to the RWST. The RCS was being pressurized with nitrogen for venting of the reactor coolant pumps and loops. Pressurizer level was being monitored by means of one cold- and two hot-calibrated level instruments. As the RCS pressure increased, the hot- and cold-calibrated level instruments were not in agreement. The operators requested that a calibration be performed on the pressurizer level instruments while continuing to fill the pressurizer. With the hot-calibrated level instruments indicating 67 percent, the operators decided to reduce the level to 25 percent by draining to the RWST. Because the hot-calibrated level instruments were not reading correctly, the actual RCS level was below the bottom of the pressurizer for 3 hours. BRAIDWOOD 2, 3/20/90 While performing activities for defueling with the reactor in cold shutdown, the reactor operators inadvertently transferred about 9500 gallons of reactor coolant to the RWST while preparing to switch operation of the RHR trains. RHR train B was in operation with train A operating in the recirculation mode to the RWST. A licensed operator inadvertently opened the RHR train A hot leg suction valve in preparation for shifting from train B operation to train A operation. Opening this valve established a flow path from the RCS to the RWST. The operator immediately recognized the error and started to close the hot leg suction valve. However, the valve takes 4 minutes to close. About 9500 gallons of reactor coolant were transferred to the RWST. In addition, this error allowed a rapid reduction in pressurizer level and RCS pressure to occur, resulting in the pressurizer exceeding its technical specification limit on the pressurizer cooldown rate (200 degrees F/hour). Discussion: The events described above are examples where RCS inventory was inadvertently reduced as a result of deficiencies in human performance with the reactor in a shutdown condition. These types of events are of concern because with the reactor in a shutdown condition, many pieces of ESF equipment can be removed from service at the same time unusual valve lineups are performed. Human performance then becomes a major factor in maintaining safety and system configuration control during shutdown conditions. . IN 90-55 August 31, 1990 Page 3 of 3 This information notice requires no specific action or written response. If you have any questions about the information in this notice, please contact the technical contact listed below or the appropriate NRR project manager. Charles E. Rossi, Director Division of Operational Events Assessment Office of Nuclear Reactor Regulation Technical Contact: John Thompson, NRR (301) 492-1171 Attachment: List of Recently Issued NRC Information Notices .ENDEND
Page Last Reviewed/Updated Tuesday, March 09, 2021
Page Last Reviewed/Updated Tuesday, March 09, 2021