Part 21 Report - 2000-150
Other Nuclear Material |
Event Number: 36931 |
REP ORG: DRESSER EQUIPMENT GROUP |
NOTIFICATION DATE:04/26/2000 |
LICENSEE: DRESSER VALVE DIVISION |
NOTIFICATION TIME:14:40[EDT] |
CITY: BURLINGTON REGION: |
EVENT DATE:04/25/2000 |
COUNTY: STATE: |
EVENT TIME:14:00[EST] |
|
LAST UPDATE DATE:04/26/2000 |
LICENSE#: |
AGREEMENT: N |
DOCKET: |
PERSON |
ORGANIZATION |
|
PAUL FREDRICKSON |
R2 |
|
VERN HODGE |
NRR |
NRC NOTIFIED BY: L. H. WINDFIELD |
|
HQ OPS OFFICER: JOHN MacKINNON |
|
EMERGENCY CLASS: N/A |
|
10 CFR SECTION: |
|
CCCC 21.21 UNSPECIFIED PARAGRAPH |
|
EVENT TEXT DRESSER VALVES NAME PLATE AND CODE PLATE HAVE INCORRECT SET PRESSURE INFORMATION AT HATCH.
PART 21 FROM DRESSER EQUIPMENT GROUP, DRESSER VALVE DIVISION, BURLINGTON, ONTARIO, CANADA.
The following noncompliance has been determined to be reportable within the requirements of 10CFR Part 21. The noncompliance involves seven safety relief valves that were purchased for the Hatch Electric Generating Plant by the Georgia Power Company through its agent, Southern Nuclear Operating Company, Inc. The valves are for use in a safely related service.
The valves were purchased on Southern Nuclear Operating Company purchase order #6040304 and produced on Dresser Valve Division sales order #119588N and are further described as follows:
Contract Item 002 Quantity 7 |
Part Number 3990C-1-S4-MS-33-SC-SC-GS produced ASME Section III Class 2 valves with the following serial numbers and required set pressures: |
SERIAL NO. |
SET PRESSURE REQD |
B119588-2-1 |
250 psig |
B119588-2-2 |
250 psig |
B119588-2-3 |
250 psig |
B119588-2-4 |
250 psig |
B119588-2-5 |
250 psig |
B119588-3-1 |
170 psig |
B119588-3-2 |
170 psig |
NONCOMPLIANCE SITUATION AND BRIEF HISTORY
On Tuesday April 25, 2000, the customer was performing receiving inspection and noticed that the set pressure information on the Code Plates and the Name Plates do not conform to the specification requirements or the history docket testing information. The customer called the Quality Assurance Department of Dresser Valve Division to discuss the finding. It appears that the set pressure information on the plates has been interchanged.
A summary of the information is as follows:
SERIAL NO |
SET PRESSURE REQD |
CODE PLATE |
NAME PLATE |
B119588-2-1 |
250 psig |
170 psig |
170 psig |
B119588-2-2 |
250 psig |
170 psig |
170 psig |
B119588-2-3 |
250 psig |
170 psig |
170 psig |
B119588-2-4 |
250 psig |
170 psig |
170 psig |
B119588-2-5 |
250 psig |
170 psig |
170 psig |
B119588-3-1 |
170 psig |
250 psig |
250 psig |
B119588-3-2 |
170 psig |
250 psig |
250 psig |
Our investigation has begun and we have conducted a full review of our records to confirm that the valves are set correctly to the contract requirements. A notice has been given to the customer to return the affected valves to Dresser Valve Division for confirmation of the plate information and correction if required. The ANI will be involved in the investigation and corrective actions as required.
We have conducted a full review of our records and confirmed that these are the only valves involved. A full review of our procedures regarding plate preparation, inspection and installation will be completed. Corrective actions will be initiated to address the internal issues, if warranted, and details will be provided in our closure reports at the completion of our investigation into the cause of this situation.
DRESSER VALVE DIVISION
TO: USNRC |
301-816-5161 |
REPORTING ORGANIZATION: |
DRESSER EQUIPMENT GROUP |
LICENSEE: |
DRESSER VALVE DIVISION |
CITY: |
BURLINGTON ONTARIO, CANADA |
NOTIFICATION DATE: |
4/26/2000 |
NOTIFICATION TIME: |
1430 |
EVENT DATE: |
4/25/2000 |
EVENT TIME: |
1400 EDT |
SUBMITTED BY: |
L.H. WINFIELD |
EVENT TEXT
NAME PLATE AND CODE PLATE HAVE INCORRECT SET PRESSURE INFORMATION
The following noncompliance has been determined to be reportable within the requirements of 10CFR Part 21. The non-compliance involves seven safety relief valves that were purchased for the Hatch Electric Generating Plant by the Georgia Power Company through its agent, SouthernNuclear Operating Company Inc. The valves are for use in a safety-related service.
The valves were purchased on Southern Nuclear Operating Company purchase order #6040304 and produced on Dresser Valve Division sales order #119588N and are further described as follows:
1. |
Contract Item 002 Qty7 |
Part Number 3990C-1-S4-MS-33-SC-SC-GS produced ASME Section III Class 2 valves with the following serial numbers and required set pressures: |
SERIAL NO. |
SET PRESSURE REQD |
B119588-2-1 |
250 psig |
B119588-2-2 |
250 psig |
B119588-2-3 |
250 psig |
B119588-2-4 |
250 psig |
B119588-2-5 |
250 psig |
B119588-3-1 |
170 psig |
B119588-3-2 |
170 psig |
NONCOMPLIANCE SITUATION AND BRIEF HISTORY
On Tuesday April 25, 2000, the customer was performing receiving inspection and noticed that the set pressure information on the Code Plates and the Name Plates do not conform to the specification requirements or the history docket testing information. The customer called the Quality Assurance Department of Dresser Valve Division to discuss the finding. It appears that the set pressure information on the plates has been interchanged. A summary of the information is as follows:
SERIAL NO |
SET PRESSURE REQD |
CODE PLATE |
NAME PLATE |
B119588-2-1 |
250 psig |
170 psig |
170 psig |
B119588-2-2 |
250 psig |
170 psig |
170 psig |
B119588-2-3 |
250 psig |
170 psig |
170 psig |
B119588-2-4 |
250 psig |
170 psig |
170 psig |
B119588-2-5 |
250 psig |
170 psig |
170 psig |
B119588-3-1 |
170 psig |
250 psig |
250 psig |
B119588-3-2 |
170 psig |
250 psig |
250 psig |
Our investigation has begun and we have conducted a full review of our records to confirm that the valves are set correctly to the contract requirements. A notice has been given to the customer to return the affected valves to Dresser Valve Division for confirmation of the plate information and correction if required. The ANI will be involved in the investigation and corrective actions as required.
We have conducted a full review of our records and confirmed that these are the only valves involved. A full review of our procedures regarding plate preparation, inspection and installation will be completed. Corrective actions will be initiated to address the internal issues, if warranted, and details will be provided in our closure reports at the completion of our investigation into the cause of this situation.
Respectfully submitted,
L.H. Winfield
Nuclear Business Unit Manager
CONSOLIDATED, GROVE, LEDEEN, MASONEILAN, NIL-COR, TEXSTEAM, TK VALVE TOM WHEATLEY, WHEATLEY
www.haliburton.com
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