Morning Report for September 20, 1999
Headquarters Daily Report SEPTEMBER 20, 1999 *************************************************************************** REPORT NEGATIVE NO INPUT ATTACHED INPUT RECEIVED RECEIVED HEADQUARTERS X REGION I X REGION II X REGION III X REGION IV X PRIORITY ATTENTION REQUIRED MORNING REPORT - HEADQUARTERS SEP. 20, 1999 MR Number: H-99-0086 NRR DAILY REPORT ITEM SIGNIFICANT EVENTS Subject: Scram on Loss of Condenser Vacuum and Recovery with Complications On August 24, 1999, the NRR Events Assessment, Generic Communications and Non-Power Reactors Branch classified this event as a Significant Event for the NRC Performance Indicator Program. The basis for this classification is the number of complications that resulted and produced unnecessary burdens on licensee personnel. On June 15, 1999, the Hatch licensee manually scrammed Unit 2 in anticipation of receiving an automatic scram signal on a turbine trip due to loss of condenser vacuum (Licensee Event Report 50-366/99-06). Several factors complicated recovery from the event: (1) failure of automatic realignment of two Unit 2 4160-volt buses because a transfer blocking relay was out of calibration; (2) an arcing ground fault on a 600-volt bus fed from Unit 1, tripping several safety-related Unit 1 600-volt circuit breakers, which actuated some Unit 1 engineered safeguards features but did not otherwise interfere with Unit 1 operation; (3) loss of Unit 2 main feedwater pumps requiring use of the Unit 2 reactor core isolation cooling system to maintain reactor level; (4) failure of a Unit 2 inboard main steam isolation valve to close due to an alternating current solenoid valve being stuck in the energized position; and (5) a leak in the Unit 2 residual heat removal service water system because of a broken 3/4-inch vent line. The licensee complied with the required limiting condition for operation 3.6.2.1 and brought Unit 2 to cold shutdown about 36 hours after the manual scram. The NRC Region II Office conducted a special inspection of the circumstances of this event (NRC Special Team Inspection Report 50-321(366)/99-10). The inspectors concluded that the licensee missed two opportunities to improve early detection of loss of condenser vacuum following similar events at this unit in 1995 and 1997. The licensee took several corrective actions for this event, adding level instruments in the circulating water pump pits, promulgating an operating order on condenser operating parameters, repairing the grounded conductor, replacing the 4160-volt fast transfer blocking relay, shortening the broken vent line, and instituting the checking of all MSIV solenoid valves for audible buzzing, an indication of undesirable presence of debris. The risk assessment for this event is low in spite of the number of complications, which were generally related to balance of plant equipment. All emergency core cooling systems were operable and the scope of the event remained within plant design parameters. A calculation using the conservative simplified plant analysis risk model indicated that the conditional core damage probability is less than 1E-6. A review of 1998-1999 event notifications using the search string HEADQUARTERS MORNING REPORT PAGE 2 SEP. 20, 1999 MR Number: H-99-0086 (cont.) "vacuum" disclosed ten reports with similar initiating conditions but with no similar complications. Consequently, the Hatch 2 event appears to be an isolated occurrence. The susceptibility to electrical noise of breaker trip devices, similar to ones that tripped some of the breakers in this event, is addressed in Information Notices 96-62 and 93-75. On 18 Aug 99, this event was briefed to senior NRC management because of the number of factors that were confusing to licensee operators. Contact: C. Vernon Hodge, NRR 301-415-1861 Email:_ @nrc.gov>
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Page Last Reviewed/Updated Wednesday, March 24, 2021