Morning Report for April 9, 1999
Headquarters Daily Report APRIL 09, 1999 *************************************************************************** REPORT NEGATIVE NO INPUT ATTACHED INPUT RECEIVED RECEIVED HEADQUARTERS X REGION I X REGION II X REGION III X REGION IV X PRIORITY ATTENTION REQUIRED MORNING REPORT - HEADQUARTERS APRIL 9, 1999 Licensee/Facility: Notification: Part 21 Database MR Number: H-99-0032 Bw/Ip Date: 04/09/99 Subject: Part 21 - Scram Discharge Volume Drain Valve Stroke Timing Failures Discussion: VENDOR: BW/IP PT21 FILE NO: 99-18-0 DATE OF DOCUMENT: 02/10/99 ACCESSION NUMBER: SOURCE DOCUMENT: LER 271/98-025-01 REVIEWER: PECB, D. Skeen NEW ISSUE. On December 7, 1998, during a quarterly surveillance, a scram discharge volume (SDV) drain valve failed to close at Vermont Yankee. It was refurbished, tested, and returned to service on December 10, 1998. On December 11, 1998, during accelerated testing of other SDV drain valves, two more were found that did not meet stroke time requirements of the inservice testing program (see Licensee Event Report 50-271/98-025-01). The licensee reports that the root cause of these failures appears to be an inadequate actuator sizing calculation for the design conditions specified in the licensee's procurement specification. The valve and actuator were supplied by BW/IP International, Inc., Valve Division, of Williamsport PA. The licensee replaced all the valve actuators in this system with larger actuators and is addressing questions regarding the vendor's quality assurance program. _ REGION III MORNING REPORT PAGE 2 APRIL 9, 1999 Licensee/Facility: Notification: Commonwealth Edison Co. MR Number: 3-99-0027 Braidwood 1 Date: 04/08/99 Braceville,Illinois SRI/RI PC Dockets: 50-456 PWR/W-4-LP Subject: Change in Status of Braidwood Unit 1 Discussion: On April 5, at approximately 2:00 a.m., operators at ComEds Braidwood Station commenced a Unit 1 shutdown following a failure of a rupture disc on the Unit 1 heater drain tank. The turbine generator breaker was opened at 9:30 am, April 5, 1999, and the reactor was shutdown at 11:00 am, April 5, 1999. The shutdown was observed by the resident inspectors. An investigation into the cause of the rupture disc was initiated. On April 8, after relocating the rupture disc to a different section of the piping, a startup of the unit was commenced. Plant return to service is expected the evening of April 8, 1999. Contact: Michael Jordan (630)829-9637 _
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Page Last Reviewed/Updated Wednesday, March 24, 2021