Morning Report for March 1, 1999
Headquarters Daily Report MARCH 01, 1999 *************************************************************************** REPORT NEGATIVE NO INPUT ATTACHED INPUT RECEIVED RECEIVED HEADQUARTERS X REGION I X REGION II X REGION III X REGION IV X PRIORITY ATTENTION REQUIRED MORNING REPORT - REGION I MARCH 1, 1999 Licensee/Facility: Notification: Public Service Electric & Gas Co. MR Number: 1-99-0005 Salem 1 2 Date: 03/01/99 Hancocks Bridge,New Jersey Dockets: 50-272,50-311 PWR/W-4-LP,PWR/W-4-LP Subject: PLANT MANAGEMENT CHANGE Discussion: On February 26, PSE&G informed Region I that Chris Bakken, Salem Plant Manager, will be leaving effective March 11 to become the Site Vice President - Operations at D.C. Cook. Pending permanent management changes, Dave Garchow will be the Acting Salem Plant Manager. Mr. Garchow had been the Salem Plant Manager prior to Mr. Bakken. Regional Action: This Is For Informational Purposes Only. Contact: Glenn Meyer (610)337-5211 _ REGION I MORNING REPORT PAGE 2 MARCH 1, 1999 Licensee/Facility: Notification: New York Power Authority MR Number: 1-99-0006 Fitz Patrick 1 Date: 03/01/99 Lycoming,New York SRI PC Dockets: 50-333 BWR/GE-4 Subject: ONSITE FIRE LASTING LESS THAN 10 MINUTES Reportable Event Number: 35419 Discussion: On February 27, 1999, at 9:56 p.m., the 'A' circulating water pump, one of three at the plant, tripped and the control room dispatched a nuclear plant operator (NPO) to the determine the cause of the pump trip. The NPO observed flames emanating from the pump motor electrical lead box cover; the onsite fire brigade responded and extinguished the fire with a CO2 extinguisher within eight minutes of the start of the event. Plant power was reduced to 65% while the pump was out of service. Subsequent inspection of the electrical lead box for the motor revealed that the pump tripped as a result of a failed connection on the Y winding motor connection, which is the center connection where all three phases are joined. The aluminum lugging used on the copper cable appears to have failed, causing an insulation breakdown and resulting in electrical arcing to the electrical lead box cover which burned a hole in the cover. NYPA repaired the damaged electrical connection and returned the pump to service early on the morning of March 1. NYPA used thermographic techniques to verify a similar condition was not developing on the other two circulating water pumps. Regional Action: The resident inspector responded over the weekend and will continue to follow NYPA's root cause evaluation and extent of condition review in this matter. Contact: John Rogge (610)337-5146 _ REGION I MORNING REPORT PAGE 3 MARCH 1, 1999 Licensee/Facility: Notification: Rochester Gas & Electric Corp. MR Number: 1-99-0007 Ginna 1 Date: 03/01/99 Ontario,New York SRI PC Dockets: 50-244 PWR/W-2-LP Subject: ERRORS IN MAIN STEAM LINE BREAK ANALYSIS Discussion: On February 22, 1999, with the reactor at approximately 75 percent power, the Ginna Station was notified by its NSSS vendor (Westinghouse) of two modeling errors in the analysis for a main steam line break (MSLB) inside containment with an assumed single failure of a feedwater regulating valve (FRV). These errors had a nonconservative impact on calculated peak containment pressure. The first error involved the omission of a previously unaccounted for volume of high temperature feedwater between the main feedwater pump discharge valve and the main FRV. The added energy released to the containment by the flashing of feedwater downstream of the main feedwater pump discharge valve raised calculated containment pressure. The second error was incorrectly assuming a 15-second closure time for the main feedwater pump discharge valve isolation valves after an automatic safety injection occurs, when the actual closure time is 85 seconds. This meant that actual feedwater flow would continue for 70 seconds longer then what was assumed in the analysis. After addressing these errors, the current Westinghouse analysis shows that the peak containment pressure limit of 60 psig would not be exceeded during a MSLB with a failed open FRV at power levels up to 70 percent power, and that sufficient shutdown margin existed to prevent a restart accident. These results were achieved by assuming a maximum heat sink temperature of 80 degrees Fahrenheit. For reactor power levels between 70 percent and 100 percent power, peak containment pressure will not exceed 60 psig, if service water temperature (recirculation temperature) is limited to less than 45 degrees Fahrenheit. Currently, recirculation temperature near the service water bay is 39 degrees Fahrenheit, while lake temperature is 35 degrees Fahrenheit. Thus, plant operation remains within its design basis for these conditions. The licensee has placed a temporary administrative restriction of 40 degrees Fahrenheit maximum on recirculation temperature to ensure adequate margin existed. As part of a regularly scheduled refueling outage, the licensee initiated a plant shutdown on March 1. During the shutdown, RG&E will continue to work with Westinghouse to resolve this issue prior to restart. Regional Action: Resident inspectors are monitoring licensee activities. Contact: Scott Barber (610)337-5232 _ REGION III MORNING REPORT PAGE 4 MARCH 1, 1999 Licensee/Facility: Notification: Indiana MR Number: 3-99-0012 Michigan Electric Co. Date: 03/01/99 Cook 1 2 sri via telecon Bridgman,Michigan Dockets: 50-315,50-316 PWR/W-4-LP,PWR/W-4-LP Subject: American Electric Power Names New D.C. Cook Vice President Discussion: On March 1, 1999, Mr. Robert Powers, Senior Vice President - Nuclear Generation for American Electric Power announced that Mr. A. Christopher Bakken will become the new DC Cook Site Vice President. Mr. Bakken succeeds Mr. John Sampson, who was named American Electric Power Indiana/Michigan State President. Mr. Bakken was previously employed at Public Service Electric & Gas Company's Salem Generating Station as the General Manager Salem Operations. Regional Action: Information Only Contact: A. Vegel (630)829-9620 _ REGION III MORNING REPORT PAGE 5 MARCH 1, 1999 Licensee/Facility: Notification: Commonwealth Edison Co. MR Number: 3-99-0013 Dresden 3 Date: 03/01/99 Morris,Illinois E-Mail from RIO Dockets: 50-249 BWR/GE-3 Subject: Completion of Refueling Outage on Unit 3 Discussion: On February 25, 1999, Dresden operators synchronized the Unit 3 main generator to the electrical grid at 9:43 p.m. ending the Dresden Unit 3 refueling outage (D3R15). The outage officially commenced on January 30, 1999, when operators tripped the turbine main generator off-line. The outage, completed in 26 days, was the shortest duration refueling outage in ComEd history. Major activities completed during the outage included: refueling of the reactor; general maintenance on the 3C low pressure turbine; bellows assembly replacements in the main condenser; hydrolazing of the condenser tubes; and plant material condition improvements. As of March 1, 1999, plant power was at approximately 80 percent power and startup testing was in progress. Regional Action: The resident inspection staff monitored the outage activities and plant startup and startup testing activities.. Contact: M.Ring (630)829-9703 _ REGION III MORNING REPORT PAGE 6 MARCH 1, 1999 Licensee/Facility: Notification: Northern States Power Co. MR Number: 3-99-0014 Prairie Island 1 2 Date: 03/01/99 Welch,Minnesota Phone call from Res.Inspector off. Dockets: 50-282,50-306 PWR/W-2-LP,PWR/W-2-LP Subject: Management Changes Announced Discussion: Northern States Power Company (NSP) has named Joel Sorensen to the newly created position of Site General Manager at Prairie Island. The appointment is effective today. Mr. Sorensen had previously been plant manager. In his new position, he will have the plant manager and the managers of security, training, nuclear generation services, and other, non-technical areas reporting to him. Northern States Power Company has also named Mr. Don Schuelke to the plant manager position. Mr. Schuelke had previously been the general superintendent of radiation protection and chemistry. In his new position, he will have responsibility for operations, maintenance, engineering, radiation protection, and chemistry. Mr. Albert Johnson of the Prairie Island radiation protection staff has been named to replace Mr. Schuelke. Contact: Roger Lanksbury (630)829-9631 _ REGION III MORNING REPORT PAGE 7 MARCH 1, 1999 Licensee/Facility: Notification: Northern States Power Co. MR Number: 3-99-0015 Monticello 1 Date: 03/01/99 Monticello,Minnesota Phone call from Res. Inspector off. Dockets: 50-263 BWR/GE-3 Subject: Management Changes announced Discussion: Northern States Power Company (NSP) has named Mr. Mike Hammer to the newly created position of Site General Manager at Monticello. The assignment is effective today. Mr. Hammer had previously been plant manager. In his new position, he will have the plant manager and the managers of security, training, nuclear generation services, and other, non-technical areas reporting to him. Northern States Power Company has also named Mr. Byron Day to the plant manager position. Mr. Day had previously been the general superintendent of plant operations. In his new position, he will have responsibility for operations, maintenance, engineering, radiation protection, and chemistry. Contact: Roger Lanksbury (630)829-9631 _
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021