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Alert

Due to a lapse in appropriations, the NRC has ceased normal operations. However, excepted and exempted activities necessary to maintain critical health and safety functions—as well as essential progress on designated critical activities, including those specified in Executive Order 14300—will continue, consistent with the OMB-Approved NRC Lapse Plan.

Event Notification Report for October 21, 2025

U.S. Nuclear Regulatory Commission
Operations Center

EVENT REPORTS FOR
10/20/2025 - 10/21/2025

Power Reactor
Event Number: 57952
Facility: South Texas
Region: 4     State: TX
Unit: [1] [] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Marc Hill
HQ OPS Officer: Ernest West
Notification Date: 09/25/2025
Notification Time: 17:36 [ET]
Event Date: 09/25/2025
Event Time: 12:29 [CDT]
Last Update Date: 10/20/2025
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
Person (Organization):
Drake, James (R4DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 100 100
Event Text
EN Revision Imported Date: 10/21/2025

EN Revision Text: TWO TRAINS OF ECCS INOPERABLE

The following information was provided by the licensee via phone and email:

"On 9/23/2025 at 2214 CDT, the South Texas Project Unit 1 (STP-1) train 'B' reactor containment fan cooler (RCFC) chilled water supply outside containment isolation valve, 1-CC-MOV-0137, was declared inoperable due to a material condition. This rendered train 'B' component cooling water inoperable which cascaded to train 'B' emergency core cooling system (ECCS) subsystem to render it inoperable. STP-1 entered technical specification (TS) 3.5.2 action 'A' for train 'B' ECCS, requiring restoration within 7 days or apply the requirements of the Configuration Risk Management Program (CRMP).

"On 09/25/2025 at 1229 CDT, train 'A' essential chiller 12A was declared inoperable due to inability to maintain chiller water outlet temperature less than 52 degrees Fahrenheit. This cascaded down to the train 'A' ECCS subsystem to render it inoperable. STP-1 entered TS 3.5.2 action 'B' due to less than two of the required subsystems operable, to within 1 hour restore at least two subsystems to operable status or apply the requirements of the CRMP, or be in at least hot standby within the next 6 hours and in hot shutdown within the following 6 hours.

"On 09/25/2025 at 1329 CDT, STP-1 entered the CRMP based on two ECCS subsystems remaining inoperable longer than 1 hour. These subsystems are used for accident mitigation. Unit 1 remains in mode 1."

* * * RETRACTION ON 10/20/2025 AT 1636 EDT FROM MARC HILL TO JOSUE RAMIREZ * * *

The following information was provided by the licensee via phone and email:

"The purpose of this notification is to retract EN 57952, which was made on September 25, 2025, at 1736 EDT. [The] notification was initially made due to two of three trains of emergency core cooling system (ECCS) being declared inoperable. After the notification was made, South Texas Project determined using an engineering evaluation, that one of the two inoperable ECCS trains was operable because the elevated chilled water outlet temperature of the associated essential chiller (Train A) did not impact the technical specification specified function.
"Therefore, this event was not a condition that could have prevented fulfillment of a safety function.
"The NRC Resident Inspector has been notified."

Notified R4DO (Vossmar)


Power Reactor
Event Number: 57963
Facility: South Texas
Region: 4     State: TX
Unit: [1] [] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Long Han
HQ OPS Officer: Jordan Wingate
Notification Date: 10/02/2025
Notification Time: 20:55 [ET]
Event Date: 10/02/2025
Event Time: 16:52 [CDT]
Last Update Date: 10/20/2025
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
Person (Organization):
Vossmar, Patricia (R4DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 100 100
Event Text
EN Revision Imported Date: 10/21/2025

EN Revision Text: TWO TRAINS OF ECCS INOPERABLE

The following information was provided by the licensee via phone and email:

"On October 2, 2025, at 1651 CDT, essential cooling water pump '1C' tripped. Essential chiller '1C' and cascading equipment, including emergency core cooling system (ECCS) train '1C,' was declared inoperable.

"Essential chiller '12A' and cascading equipment, including ECCS train '1A,' was concurrently inoperable for ongoing maintenance.

"This condition resulted in an inoperable condition on 2 out of 3 safety trains for the accident mitigating functions, including the train 'A' and train 'C' high head safety injection (SI), low head SI, containment spray, electrical auxiliary building heating ventilation and air conditioning (HVAC), and essential chilled water. All 'B' train safety related equipment remains operable. There was no impact on the health and safety of the public or plant personnel.

"The repair timeline is unknown. We have already entered the configuration risk management program to mitigate additional maintenance induced risk with a risk informed completion time of October 19, 2025, at 1140 CDT. We are limited by TS 3.7.7.C to restore 1 train of control room HVAC by October 5, 2025, at 1651 CDT.

"This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D).

"The NRC Resident Inspector has been notified."

The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:

The 'C' emergency diesel generator is unavailable due to the loss of cooling water. Maintenance on the ECCS train '1A' is partially complete and operators are working to restore the train to an operable status prior to the technical specification deadline. The essential cooling water pump trip was due to a hot spot causing the pump to overheat. The cause of the hot spot is still under investigation.

* * * RETRACTION ON 10/20/2025 AT 1636 EDT FROM MARC HILL TO JOSUE RAMIREZ * * *

The following information was provided by the licensee via phone and email:

"The purpose of this notification is to retract EN 57963, which was made on October 2, 2025, at 2055 EDT. [The] notification was initially made due to two of three trains of emergency core cooling system (ECCS) being declared inoperable. After the notification was made, South Texas Project determined, using an engineering evaluation, that one of the two inoperable ECCS trains was operable because the elevated chilled water outlet temperature of the associated essential chiller (Train A) did not impact the technical specification specified function.
"Therefore, this event was not a condition that could have prevented fulfillment of a safety function.
"The NRC Resident Inspector has been notified."

Notified R4DO (Vossmar)


Agreement State
Event Number: 57965
Rep Org: Arkansas Department of Health
Licensee: Domtar AW LLC
Region: 4
City: Ashdown   State: AR
County:
License #: ARK-0354-03120
Agreement: Y
Docket:
NRC Notified By: Hunter Broadaway
HQ OPS Officer: Robert A. Thompson
Notification Date: 10/03/2025
Notification Time: 13:56 [ET]
Event Date: 10/02/2025
Event Time: 00:00 [CDT]
Last Update Date: 10/20/2025
Emergency Class: Non Emergency
10 CFR Section:
Agreement State
Person (Organization):
Vossmar, Patricia (R4DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
Event Text
EN Revision Imported Date: 10/21/2025

EN Revision Text: AGREEMENT STATE REPORT - STUCK OPEN GAUGE SHUTTER

The following information is a summary of information provided by the Arkansas Department of Health (the Department) via email:

During routine gauge shutter checks conducted by the licensee on October 2, 2025, the licensee found the shutters of three Berthold Technologies model LB300L fixed gauges stuck in the open position. The licensee has flagged the gauges, placed barriers around the gauges, and suspended any work in the area. The licensee is arranging for a Berthold field representative to perform maintenance on the gauges to attempt to close the gauges.

Gauge 1: 0.2 mCi Co-60
Gauge 2: 0.5 mCi Co-60
Gauge 3: 1.8 mCi Co-60

Arkansas event: AR-2025-013


* * * UPDATE ON 10/20/2025 AT 1617 EDT FROM HUNTER BROADAWAY TO JOSUE RAMIREZ * * *

The following information is a summary of information provided by the Arkansas Department of Health (the Department) via email:

On October 20, 2025, a response from DOMTAR A.W. LLC, Arkansas Licensee ARK-0354-03120, reports that under the direction of a Berthold Technologies representative, the three shutters were able to be cycled and are once again functional. Maintenance and leak testing were performed on the three gauges.
Arkansas event AR-2025-013 is considered closed by the Department.


Power Reactor
Event Number: 57994
Facility: Wolf Creek
Region: 4     State: KS
Unit: [1] [] []
RX Type: [1] W-4-LP
NRC Notified By: Michael J. Payne
HQ OPS Officer: Josue Ramirez
Notification Date: 10/21/2025
Notification Time: 14:37 [ET]
Event Date: 10/21/2025
Event Time: 06:10 [CDT]
Last Update Date: 10/21/2025
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
Person (Organization):
Vossmar, Patricia (R4DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N N 0 0
Event Text
BOTH TRAINS OF CONTROL ROOM EMERGENCY VENTILATION SYSTEM INOPERABLE

The following is a summary of information provided by the licensee via phone and email:

On October 21, 2025, at 0610 CDT, while reloading fuel to the reactor vessel, an electrical perturbation initiated a control room ventilation isolation signal (CRVIS). The control room air conditioning system (CRACS) 'A' train A/C unit did not start upon the CRVIS due to a blown fuse. The 'B' CRACS A/C unit was out of service for planned maintenance at the time. At 1020 CDT, the 'A' train CRACS A/C unit was returned to service. Both trains of the control room emergency ventilation system (CREVS) were inoperable for 10 minutes. Due to both trains of CRACS and CREVS being inoperable, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v).

This condition caused entry into technical specification (TS) limiting condition for operation (LCO) 3.7.10 condition `E' and 3.7.11 condition `D'. Upon discovery of the condition, fuel movement and core alterations were suspended in accordance with the TS LCO required actions.

There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector was notified.


Power Reactor
Event Number: 57996
Facility: Palisades
Region: 3     State: MI
Unit: [1] [] []
RX Type: [1] CE
NRC Notified By: Scott Moore
HQ OPS Officer: Josue Ramirez
Notification Date: 10/21/2025
Notification Time: 16:52 [ET]
Event Date: 10/21/2025
Event Time: 16:32 [EDT]
Last Update Date: 10/21/2025
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(3)(xii) - Offsite Medical
Person (Organization):
Edwards, Rhex (R3DO)
Grant, Jeffery (IRMOC)
Phil McKenna (NRR EO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N N 0 0
Event Text
TRANSPORT OF CONTAMINATED PERSON OFFSITE

The following information was provided by the licensee via phone and email:

"On 10/21/2025 at 0930 EDT an individual fell into the reactor cavity. The reactor cavity is full of water. They ingested some amount of cavity water. The individual was decontaminated by radiation protection personnel but had 300 counts per minute detected in their hair. At 1632 EDT they were sent off site to seek medical attention.

"This is an eight-hour notification, non-emergency, for the transportation of a contaminated person offsite. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xii).

"The NRC Resident Inspector has been notified."


Power Reactor
Event Number: 57997
Facility: North Anna
Region: 2     State: VA
Unit: [1] [] []
RX Type: [1] W-3-LP,[2] W-3-LP,[3] M-4-LP
NRC Notified By: Nick Wilson
HQ OPS Officer: Josue Ramirez
Notification Date: 10/21/2025
Notification Time: 23:10 [ET]
Event Date: 10/21/2025
Event Time: 21:08 [EDT]
Last Update Date: 10/21/2025
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
Mckown, Louis J (R2DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 A/R Y 74 0
Event Text
AUTOMATIC REACTOR TRIP

The following information was provided by the licensee via email and phone:

"On October 21, 2025, at 2108 EDT, Unit 1 automatically tripped from 74 percent power due to a negative rate trip. The unit has been stabilized in mode 3 at normal operating temperature and pressure. The reactor trip was uncomplicated, and all control rods fully inserted into the core. This reactor protection system actuation is reportable per 10 CFR 50.72(b)(2)(iv)(B). The auxiliary feedwater pumps actuated as designed because of the reactor trip and is reportable per 10 CFR 50.72(b)(3)(iv)(A) for a valid engineered safety feature (ESF) actuation. Decay heat is being removed via the steam generator power-operated relief valves and Unit 1 is in a normal shutdown electrical lineup. Unit 2 was not affected by this event."

The NRC Resident Inspector has been notified.