Event Notification Report for September 27, 2024
U.S. Nuclear Regulatory Commission
Operations Center
EVENT REPORTS FOR
09/26/2024 - 09/27/2024
Part 21
Event Number: 57243
Rep Org: RSSC dba Marmon
Licensee:
Region: 1
City: East Granby State: CT
County:
License #:
Agreement: N
Docket:
NRC Notified By: Phillip Sargenski
HQ OPS Officer: Adam Koziol
Licensee:
Region: 1
City: East Granby State: CT
County:
License #:
Agreement: N
Docket:
NRC Notified By: Phillip Sargenski
HQ OPS Officer: Adam Koziol
Notification Date: 07/25/2024
Notification Time: 11:05 [ET]
Event Date: 07/23/2024
Event Time: 00:00 [EDT]
Last Update Date: 09/26/2024
Notification Time: 11:05 [ET]
Event Date: 07/23/2024
Event Time: 00:00 [EDT]
Last Update Date: 09/26/2024
Emergency Class: Non Emergency
10 CFR Section:
21.21(d)(3)(i) - Defects And Noncompliance
10 CFR Section:
21.21(d)(3)(i) - Defects And Noncompliance
Person (Organization):
Lilliendahl, Jon (R1DO)
Feliz-Adorno, Nestor (R3DO)
Azua, Ray (R4DO)
Part 21/50.55 Reactors, - (EMAIL)
Lilliendahl, Jon (R1DO)
Feliz-Adorno, Nestor (R3DO)
Azua, Ray (R4DO)
Part 21/50.55 Reactors, - (EMAIL)
EN Revision Imported Date: 9/27/2024
EN Revision Text: PART 21 REPORT - NON-COMPLAINT INSULATED CONDUCTOR
The following is a synopsis of information received via fax:
A reel of insulated conductor was found non-compliant due to failure of insulation tensile and elongation at break test following air oven aging. Wire from the non-compliant reel was delivered to nine plants.
Affected plants: Wolf Creek, Dresden, LaSalle, Limerick, Peach Bottom, Arkansas Nuclear One, Waterford, Susquehanna, and Davis Besse.
Reporting company point of contact:
RSSC Wire and Cable LLC
dba Marmon Industrial Energy and Infrastructure
20 Bradley Park Road
East Granby, CT 06026
Phillip Sargenski - Quality Assurance Manager
Phone: 860-653-8376
Fax: 860-653-8301
Phillip.sargenski@marmoniei.com
* * * UPDATE ON 08/23/24 AT 1315 EDT FROM PHILLIP SARGENSKI TO JOSUE RAMIREZ * * *
The vendor provided the final report for this event listing corrective actions and the estimated completion dates.
Notified R1DO (Lilliendahl), R3DO (Skokowski), R4DO (Vossmar), and Part 21 group (Email).
* * * UPDATE ON 09/04/24 AT 1044 EDT FROM PHILLIP SARGENSKI TO NESTOR MAKRIS * * *
The vendor notified the NRC that they plan to send additional finding data regarding this notification via fax and/or email within the next day or two.
Notified R1DO (Ferdas), R3DO (Hills), R4DO (Drake), and Part 21 group (Email).
* * * UPDATE ON 09/06/24 AT 1327 EDT FROM PHILLIP SARGENSKI TO ADAM KOZIOL * * *
The vendor identified an additional non-compliant shipment of insulated conductor.
Affected plant: Calvert Cliffs
Notified R1DO (Ferdas), R3DO (Hills), R4DO (Drake), and Part 21 group (Email).
* * * UPDATE ON 9/17/24 AT 1641 EDT FROM PHILLIP SARGENSKI TO ROBERT THOMPSON * * *
The vendor identified an additional non-compliant shipment of insulated conductor.
Affected customer: Curtiss-Wright Nuclear Division.
Notified R1DO (Werkheiser), R3DO (Ziolkowski), R4DO (Azua), and Part 21 group (Email).
* * * UPDATE ON 9/26/24 AT 1030 EDT FROM PHILLIP SARGENSKI TO ADAM KOZIOL * * *
The vendor is continuing to conduct inventory sampling which involves a 14 day aging test. Due to the length of testing, the vendor plans on submitting their final report the week of October 7, 2024.
Notified R1DO (Dimitriadis), R3DO (Havertape), R4DO (Young), and Part 21 group (Email).
EN Revision Text: PART 21 REPORT - NON-COMPLAINT INSULATED CONDUCTOR
The following is a synopsis of information received via fax:
A reel of insulated conductor was found non-compliant due to failure of insulation tensile and elongation at break test following air oven aging. Wire from the non-compliant reel was delivered to nine plants.
Affected plants: Wolf Creek, Dresden, LaSalle, Limerick, Peach Bottom, Arkansas Nuclear One, Waterford, Susquehanna, and Davis Besse.
Reporting company point of contact:
RSSC Wire and Cable LLC
dba Marmon Industrial Energy and Infrastructure
20 Bradley Park Road
East Granby, CT 06026
Phillip Sargenski - Quality Assurance Manager
Phone: 860-653-8376
Fax: 860-653-8301
Phillip.sargenski@marmoniei.com
* * * UPDATE ON 08/23/24 AT 1315 EDT FROM PHILLIP SARGENSKI TO JOSUE RAMIREZ * * *
The vendor provided the final report for this event listing corrective actions and the estimated completion dates.
Notified R1DO (Lilliendahl), R3DO (Skokowski), R4DO (Vossmar), and Part 21 group (Email).
* * * UPDATE ON 09/04/24 AT 1044 EDT FROM PHILLIP SARGENSKI TO NESTOR MAKRIS * * *
The vendor notified the NRC that they plan to send additional finding data regarding this notification via fax and/or email within the next day or two.
Notified R1DO (Ferdas), R3DO (Hills), R4DO (Drake), and Part 21 group (Email).
* * * UPDATE ON 09/06/24 AT 1327 EDT FROM PHILLIP SARGENSKI TO ADAM KOZIOL * * *
The vendor identified an additional non-compliant shipment of insulated conductor.
Affected plant: Calvert Cliffs
Notified R1DO (Ferdas), R3DO (Hills), R4DO (Drake), and Part 21 group (Email).
* * * UPDATE ON 9/17/24 AT 1641 EDT FROM PHILLIP SARGENSKI TO ROBERT THOMPSON * * *
The vendor identified an additional non-compliant shipment of insulated conductor.
Affected customer: Curtiss-Wright Nuclear Division.
Notified R1DO (Werkheiser), R3DO (Ziolkowski), R4DO (Azua), and Part 21 group (Email).
* * * UPDATE ON 9/26/24 AT 1030 EDT FROM PHILLIP SARGENSKI TO ADAM KOZIOL * * *
The vendor is continuing to conduct inventory sampling which involves a 14 day aging test. Due to the length of testing, the vendor plans on submitting their final report the week of October 7, 2024.
Notified R1DO (Dimitriadis), R3DO (Havertape), R4DO (Young), and Part 21 group (Email).
Power Reactor
Event Number: 57338
Facility: Grand Gulf
Region: 4 State: MS
Unit: [1] [] []
RX Type: [1] GE-6
NRC Notified By: Joshua Hubbard
HQ OPS Officer: Bill Nytko
Region: 4 State: MS
Unit: [1] [] []
RX Type: [1] GE-6
NRC Notified By: Joshua Hubbard
HQ OPS Officer: Bill Nytko
Notification Date: 09/25/2024
Notification Time: 02:06 [ET]
Event Date: 09/24/2024
Event Time: 22:04 [CDT]
Last Update Date: 09/25/2024
Notification Time: 02:06 [ET]
Event Date: 09/24/2024
Event Time: 22:04 [CDT]
Last Update Date: 09/25/2024
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
Person (Organization):
Young, Cale (R4DO)
Young, Cale (R4DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | N | Y | 100 | Power Operation | 100 | Power Operation |
HIGH PRESSURE CORE SPRAY INOPERABLE
The following information was provided by the licensee via phone or email:
"On September 24, 2024, at 2204 CDT, Grand Gulf Nuclear Station (GGNS) was conducting surveillance testing on the high pressure core spray (HPCS) division III diesel generator. During testing, the HPCS pump breaker unexpectedly tripped after the HPCS diesel generator started and powered the safety bus. The breaker performed its motor protection function and tripped due to an over-frequency indication.
"The event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function.
"Troubleshooting is in progress. HPCS, a single-train system, will remain inoperable until the condition is corrected.
"All sources of offsite power are available. No other safety systems are inoperable. Reactor core isolation cooling was verified to be operable per GGNS Technical Specification 3.5.1.B.1.
"The NRC Senior Resident has been notified."
The following information was provided by the licensee via phone or email:
"On September 24, 2024, at 2204 CDT, Grand Gulf Nuclear Station (GGNS) was conducting surveillance testing on the high pressure core spray (HPCS) division III diesel generator. During testing, the HPCS pump breaker unexpectedly tripped after the HPCS diesel generator started and powered the safety bus. The breaker performed its motor protection function and tripped due to an over-frequency indication.
"The event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function.
"Troubleshooting is in progress. HPCS, a single-train system, will remain inoperable until the condition is corrected.
"All sources of offsite power are available. No other safety systems are inoperable. Reactor core isolation cooling was verified to be operable per GGNS Technical Specification 3.5.1.B.1.
"The NRC Senior Resident has been notified."
Fuel Cycle Facility
Event Number: 57339
Facility: Global Nuclear Fuel - Americas
Region: 2 State: NC
Unit: [] [] []
RX Type: Uranium Fuel Fabrication
Comments: Leu Conversion (Uf6 To Uo2)
Leu Fabrication
Lwr Commerical Fuel
NRC Notified By: Phillip Ollis
HQ OPS Officer: Tenisha Meadows
Region: 2 State: NC
Unit: [] [] []
RX Type: Uranium Fuel Fabrication
Comments: Leu Conversion (Uf6 To Uo2)
Leu Fabrication
Lwr Commerical Fuel
NRC Notified By: Phillip Ollis
HQ OPS Officer: Tenisha Meadows
Notification Date: 09/25/2024
Notification Time: 15:07 [ET]
Event Date: 09/25/2024
Event Time: 11:10 [EDT]
Last Update Date: 09/25/2024
Notification Time: 15:07 [ET]
Event Date: 09/25/2024
Event Time: 11:10 [EDT]
Last Update Date: 09/25/2024
Emergency Class: Non Emergency
10 CFR Section:
PART 70 APP A (c) - Offsite Notification/News Rel
10 CFR Section:
PART 70 APP A (c) - Offsite Notification/News Rel
Person (Organization):
Suber, Gregory (R2DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
Suber, Gregory (R2DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
CONCURRENT REPORT FOR FIRE DOOR IMPAIRMENT
The following information was provided by the licensee via phone and email:
"At approximately 1110 EDT, on September 25, 2024, the New Hanover County Deputy Fire Marshall was notified that a non-IROFS (Item Relied On For Safety) fire door was damaged and incapable of fulfilling its function. Specifically, the door will not close properly and seal with the opposing door. A fire watch was initiated and a replacement door is being obtained. Because the New Hanover County Deputy Fire Marshall was notified, a concurrent notification to the NRC Operations Center is being made per 10 CFR 70, Appendix A(c)."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The licensee plans to notify the NRC Region 2 office and the state of North Carolina concerning this event report.
The following information was provided by the licensee via phone and email:
"At approximately 1110 EDT, on September 25, 2024, the New Hanover County Deputy Fire Marshall was notified that a non-IROFS (Item Relied On For Safety) fire door was damaged and incapable of fulfilling its function. Specifically, the door will not close properly and seal with the opposing door. A fire watch was initiated and a replacement door is being obtained. Because the New Hanover County Deputy Fire Marshall was notified, a concurrent notification to the NRC Operations Center is being made per 10 CFR 70, Appendix A(c)."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The licensee plans to notify the NRC Region 2 office and the state of North Carolina concerning this event report.
Agreement State
Event Number: 57335
Rep Org: New Mexico Rad Control Program
Licensee: Acme Environmental, Inc.
Region: 4
City: Albuquerque State: NM
County: Bernalillo
License #: PA 526-02
Agreement: Y
Docket:
NRC Notified By: Victor Diaz
HQ OPS Officer: Jon Lilliendahl
Licensee: Acme Environmental, Inc.
Region: 4
City: Albuquerque State: NM
County: Bernalillo
License #: PA 526-02
Agreement: Y
Docket:
NRC Notified By: Victor Diaz
HQ OPS Officer: Jon Lilliendahl
Notification Date: 09/23/2024
Notification Time: 14:56 [ET]
Event Date: 09/23/2024
Event Time: 00:00 [CDT]
Last Update Date: 09/23/2024
Notification Time: 14:56 [ET]
Event Date: 09/23/2024
Event Time: 00:00 [CDT]
Last Update Date: 09/23/2024
Emergency Class: Non Emergency
10 CFR Section:
Agreement State
10 CFR Section:
Agreement State
Person (Organization):
Young, Cale (R4DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
ILTAB, (EMAIL) (EMAIL)
CNSNS (Mexico), - (EMAIL)
Young, Cale (R4DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
ILTAB, (EMAIL) (EMAIL)
CNSNS (Mexico), - (EMAIL)
AGREEMENT STATE REPORT - STOLEN SOURCE
The following is a summary of information that was provided by the New Mexico Radiation Control Program via phone and email:
During the weekend, Acme Environmental, Inc. (the licensee) was burglarized. An XRF lead paint analyzer, model Heuresis Pb200i, containing 5 mCi of Co-57 was stolen, along with numerous other items. The licensee notified the police, and the police are actively investigating.
THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL
Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
The following is a summary of information that was provided by the New Mexico Radiation Control Program via phone and email:
During the weekend, Acme Environmental, Inc. (the licensee) was burglarized. An XRF lead paint analyzer, model Heuresis Pb200i, containing 5 mCi of Co-57 was stolen, along with numerous other items. The licensee notified the police, and the police are actively investigating.
THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL
Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
Power Reactor
Event Number: 57343
Facility: Hatch
Region: 2 State: GA
Unit: [1] [] []
RX Type: [1] GE-4,[2] GE-4
NRC Notified By: David Hutto
HQ OPS Officer: Adam Koziol
Region: 2 State: GA
Unit: [1] [] []
RX Type: [1] GE-4,[2] GE-4
NRC Notified By: David Hutto
HQ OPS Officer: Adam Koziol
Notification Date: 09/27/2024
Notification Time: 07:02 [ET]
Event Date: 09/27/2024
Event Time: 03:46 [EDT]
Last Update Date: 09/27/2024
Notification Time: 07:02 [ET]
Event Date: 09/27/2024
Event Time: 03:46 [EDT]
Last Update Date: 09/27/2024
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
Suber, Gregory (R2DO)
Suber, Gregory (R2DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | M/R | N | 54 | Power Operation | 0 | Hot Shutdown |
MANUAL REACTOR TRIP ON LOWERING CONDENSER VACUUM
The following information was provided by the licensee via phone:
"At 0346 EDT on 9/27/24, with Unit 1 in mode 1 at 54 percent power, the reactor was manually tripped due to degrading condenser vacuum secondary to environmental conditions. The trip was not complex with all systems responding normally post trip. Closure of containment isolation valves (CIVs) in multiple systems occurred. Operations responded and stabilized the plant.
"The reactor protection system actuation while critical event is being reported as a 4-hour non-emergency notification per 10 CFR 52.72(b)(2)(iv)(B). Additionally, it is reportable under 10 CFR 52.72(b)(3)(iv)(a) as an event that results in a valid actuation of the CIVs.
"There was no impact on the health and safety of the public or plant personnel.
"The NRC Resident Inspector has been notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
Decay heat removal is via steam bypass to the main condenser. Unit 2 was not affected.
The following information was provided by the licensee via phone:
"At 0346 EDT on 9/27/24, with Unit 1 in mode 1 at 54 percent power, the reactor was manually tripped due to degrading condenser vacuum secondary to environmental conditions. The trip was not complex with all systems responding normally post trip. Closure of containment isolation valves (CIVs) in multiple systems occurred. Operations responded and stabilized the plant.
"The reactor protection system actuation while critical event is being reported as a 4-hour non-emergency notification per 10 CFR 52.72(b)(2)(iv)(B). Additionally, it is reportable under 10 CFR 52.72(b)(3)(iv)(a) as an event that results in a valid actuation of the CIVs.
"There was no impact on the health and safety of the public or plant personnel.
"The NRC Resident Inspector has been notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
Decay heat removal is via steam bypass to the main condenser. Unit 2 was not affected.
Power Reactor
Event Number: 57344
Facility: Catawba
Region: 2 State: SC
Unit: [1] [2] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Tom Chandler
HQ OPS Officer: Adam Koziol
Region: 2 State: SC
Unit: [1] [2] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Tom Chandler
HQ OPS Officer: Adam Koziol
Notification Date: 09/27/2024
Notification Time: 11:25 [ET]
Event Date: 09/27/2024
Event Time: 07:46 [EDT]
Last Update Date: 09/27/2024
Notification Time: 11:25 [ET]
Event Date: 09/27/2024
Event Time: 07:46 [EDT]
Last Update Date: 09/27/2024
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation 50.72(b)(3)(v)(B) - Pot RHR Inop
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation 50.72(b)(3)(v)(B) - Pot RHR Inop
Person (Organization):
Suber, Gregory (R2DO)
Suber, Gregory (R2DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | N | Y | 95 | Power Operation | 33 | Power Operation |
2 | M/R | Y | 100 | Power Operation | 0 | Hot Standby |
MANUAL REACTOR TRIP DUE TO LOSS OF CONDENSER VACUUM
The following information was provided by the licensee via phone and email:
"At 0748 EDT on 9/27/24, Catawba Unit 2 was manually tripped due to loss of condenser vacuum. The Unit 2 auxiliary feedwater (AFW) system started automatically as expected. Decay heat is being removed by the steam generators and discharging to the condenser.
"Due to the Unit 2 reactor protection system actuation while critical, this event is being reported as a four-hour, nonemergency notification per 10 CFR 50.72(b)(2)(iv)(B). The automatic start of the Unit 2 AFW system is being reported as an eight-hour, nonemergency notification per 10 CFR 50.72(b)(3)(iv)(A).
"On Unit 1, it was determined that at 0746, all trains of the Unit 1 AFW were inoperable when the Unit 1 hotwell temperature exceeded the operability limit for the AFW system. Therefore, this condition is being reported as an eight-hour, nonemergency notification per 10 CFR 50.72(b)(3)(v). The affected safety function was restored on 9/27/24 at 0851 EDT when the Unit 1 hotwell temperature returned below the operability limit for the AFW system.
"There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The loss of vacuum for both Unit 1 and Unit 2 was due to loss of power to cooling tower fans. The suspected cause of loss of cooling tower fans was due to water intrusion due to Hurricane Helene.
The following information was provided by the licensee via phone and email:
"At 0748 EDT on 9/27/24, Catawba Unit 2 was manually tripped due to loss of condenser vacuum. The Unit 2 auxiliary feedwater (AFW) system started automatically as expected. Decay heat is being removed by the steam generators and discharging to the condenser.
"Due to the Unit 2 reactor protection system actuation while critical, this event is being reported as a four-hour, nonemergency notification per 10 CFR 50.72(b)(2)(iv)(B). The automatic start of the Unit 2 AFW system is being reported as an eight-hour, nonemergency notification per 10 CFR 50.72(b)(3)(iv)(A).
"On Unit 1, it was determined that at 0746, all trains of the Unit 1 AFW were inoperable when the Unit 1 hotwell temperature exceeded the operability limit for the AFW system. Therefore, this condition is being reported as an eight-hour, nonemergency notification per 10 CFR 50.72(b)(3)(v). The affected safety function was restored on 9/27/24 at 0851 EDT when the Unit 1 hotwell temperature returned below the operability limit for the AFW system.
"There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The loss of vacuum for both Unit 1 and Unit 2 was due to loss of power to cooling tower fans. The suspected cause of loss of cooling tower fans was due to water intrusion due to Hurricane Helene.
Power Reactor
Event Number: 57345
Facility: Prairie Island
Region: 3 State: MN
Unit: [1] [2] []
RX Type: [1] W-2-LP,[2] W-2-LP
NRC Notified By: Timothy Thomas
HQ OPS Officer: Ernest West
Region: 3 State: MN
Unit: [1] [2] []
RX Type: [1] W-2-LP,[2] W-2-LP
NRC Notified By: Timothy Thomas
HQ OPS Officer: Ernest West
Notification Date: 09/27/2024
Notification Time: 11:43 [ET]
Event Date: 09/17/2024
Event Time: 17:00 [CDT]
Last Update Date: 09/27/2024
Notification Time: 11:43 [ET]
Event Date: 09/17/2024
Event Time: 17:00 [CDT]
Last Update Date: 09/27/2024
Emergency Class: Non Emergency
10 CFR Section:
26.719 - Fitness For Duty
10 CFR Section:
26.719 - Fitness For Duty
Person (Organization):
Havertape, Joshua (R3DO)
FFD Group, (EMAIL)
Havertape, Joshua (R3DO)
FFD Group, (EMAIL)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | N | Y | 100 | Power Operation | 0 | Refueling |
2 | N | Y | 100 | Power Operation | 100 | Power Operation |
FITNESS FOR DUTY
The following information was provided by the licensee via email:
"On September 17, 2024, the site identified that an individual assigned to perform fitness for duty (FFD) program duties, who should have been part of the fitness for duty program random testing pool, had been inadvertently removed during a recent computer system upgrade. The individual was reprocessed and placed back into the FFD program on September 18, 2024. This was determined to be an isolated incident as it was confirmed that no other individuals required to be in the program were removed."
The following information was provided by the licensee via email:
"On September 17, 2024, the site identified that an individual assigned to perform fitness for duty (FFD) program duties, who should have been part of the fitness for duty program random testing pool, had been inadvertently removed during a recent computer system upgrade. The individual was reprocessed and placed back into the FFD program on September 18, 2024. This was determined to be an isolated incident as it was confirmed that no other individuals required to be in the program were removed."
Power Reactor
Event Number: 57346
Facility: Monticello
Region: 3 State: MN
Unit: [1] [] []
RX Type: [1] GE-3
NRC Notified By: Brandon Kent
HQ OPS Officer: Ernest West
Region: 3 State: MN
Unit: [1] [] []
RX Type: [1] GE-3
NRC Notified By: Brandon Kent
HQ OPS Officer: Ernest West
Notification Date: 09/27/2024
Notification Time: 12:10 [ET]
Event Date: 09/17/2024
Event Time: 17:00 [CDT]
Last Update Date: 09/27/2024
Notification Time: 12:10 [ET]
Event Date: 09/17/2024
Event Time: 17:00 [CDT]
Last Update Date: 09/27/2024
Emergency Class: Non Emergency
10 CFR Section:
26.719 - Fitness For Duty
10 CFR Section:
26.719 - Fitness For Duty
Person (Organization):
Havertape, Joshua (R3DO)
FFD Group, (EMAIL)
Havertape, Joshua (R3DO)
FFD Group, (EMAIL)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | N | Y | 100 | Power Operation | 100 | Power Operation |
FITNESS FOR DUTY
The following information was provided by the licensee via email:
"On September 17, 2024, the site identified that an individual assigned to perform fitness for duty (FFD) program duties, who should have been part of the fitness for duty program random testing pool, had been inadvertently removed during a recent computer system upgrade. The individual was reprocessed and placed back into the FFD program on September 18, 2024. This was determined to be an isolated incident as it was confirmed that no other individuals required to be in the program were removed."
The following information was provided by the licensee via email:
"On September 17, 2024, the site identified that an individual assigned to perform fitness for duty (FFD) program duties, who should have been part of the fitness for duty program random testing pool, had been inadvertently removed during a recent computer system upgrade. The individual was reprocessed and placed back into the FFD program on September 18, 2024. This was determined to be an isolated incident as it was confirmed that no other individuals required to be in the program were removed."
Power Reactor
Event Number: 57349
Facility: Grand Gulf
Region: 4 State: MS
Unit: [1] [] []
RX Type: [1] GE-6
NRC Notified By: Mike Riehl
HQ OPS Officer: Natalie Starfish
Region: 4 State: MS
Unit: [1] [] []
RX Type: [1] GE-6
NRC Notified By: Mike Riehl
HQ OPS Officer: Natalie Starfish
Notification Date: 09/28/2024
Notification Time: 00:35 [ET]
Event Date: 09/27/2024
Event Time: 18:22 [CDT]
Last Update Date: 09/28/2024
Notification Time: 00:35 [ET]
Event Date: 09/27/2024
Event Time: 18:22 [CDT]
Last Update Date: 09/28/2024
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
Person (Organization):
Young, Cale (R4DO)
Young, Cale (R4DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | N | Y | 100 | Power Operation | 100 | Power Operation |
HIGH PRESSURE COOLANT INJECTION INOPERABLE
The following information was provided by the licensee via phone and email:
"At 1822 CST on September 27, 2024, Grand Gulf Nuclear Station (GGNS) was conducting surveillance testing on the high pressure core spray (HPCS) division Ill diesel generator. Following initiation of the test signal, the HPCS pump room cooler start time exceeded the surveillance procedure allowance of less than or equal to 20 seconds. The HPCS pump room cooler started in 26.2 seconds. HPCS was already inoperable for performance of the surveillance testing.
"The event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function.
"Troubleshooting is in progress. HPCS, a single-train system, will remain inoperable until the condition is corrected.
"All sources of offsite power are available. No other safety systems are inoperable. Reactor core isolation cooling was verified to be operable per GGNS Technical Specification 3.5.1.B.1.
"The NRC Senior Resident Inspector has been notified."
The following information was provided by the licensee via phone and email:
"At 1822 CST on September 27, 2024, Grand Gulf Nuclear Station (GGNS) was conducting surveillance testing on the high pressure core spray (HPCS) division Ill diesel generator. Following initiation of the test signal, the HPCS pump room cooler start time exceeded the surveillance procedure allowance of less than or equal to 20 seconds. The HPCS pump room cooler started in 26.2 seconds. HPCS was already inoperable for performance of the surveillance testing.
"The event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function.
"Troubleshooting is in progress. HPCS, a single-train system, will remain inoperable until the condition is corrected.
"All sources of offsite power are available. No other safety systems are inoperable. Reactor core isolation cooling was verified to be operable per GGNS Technical Specification 3.5.1.B.1.
"The NRC Senior Resident Inspector has been notified."
Power Reactor
Event Number: 57351
Facility: Sequoyah
Region: 2 State: TN
Unit: [1] [] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Timothy Wood
HQ OPS Officer: Natalie Starfish
Region: 2 State: TN
Unit: [1] [] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Timothy Wood
HQ OPS Officer: Natalie Starfish
Notification Date: 09/29/2024
Notification Time: 08:40 [ET]
Event Date: 09/29/2024
Event Time: 05:56 [EDT]
Last Update Date: 09/29/2024
Notification Time: 08:40 [ET]
Event Date: 09/29/2024
Event Time: 05:56 [EDT]
Last Update Date: 09/29/2024
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
Suber, Gregory (R2DO)
Suber, Gregory (R2DO)
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode |
---|---|---|---|---|---|---|
1 | A/R | Y | 100 | Power Operation | 0 | Hot Standby |
AUTOMATIC REACTOR TRIP DUE TO TURBINE TRIP
The following information was provided by the licensee via phone and email:
"At 05:56 EDT on 09/29/2024, with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped due to a turbine trip. The motor driven auxiliary feedwater (MDAFW) level control valves (LCV) for loop 1 failed to respond from the main control room. All others systems responded normally post-trip.
"Operations responded and stabilized the plant. Decay heat is being removed by the auxiliary feedwater (AFW) and steam dump systems. Unit 2 is currently stable in Mode 6 for a maintenance outage and was not affected.
"Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour, non-emergency notification per 10 CFR 50.72 (b)(3)(iv)(A) as an event that results in a valid actuation of the AFW system. The AFW system started automatically and is operating as designed with the exception of the MDAFW LCVs for loop 1.
"There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The facility is in a 72 hour technical specification related to the auxiliary feedwater system. Sequoyah does not consider this to be a complex trip. The turbine trip is due to an electrical failure, and is still under investigation. Offsite power is qualified with no abnormalities.
The following information was provided by the licensee via phone and email:
"At 05:56 EDT on 09/29/2024, with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped due to a turbine trip. The motor driven auxiliary feedwater (MDAFW) level control valves (LCV) for loop 1 failed to respond from the main control room. All others systems responded normally post-trip.
"Operations responded and stabilized the plant. Decay heat is being removed by the auxiliary feedwater (AFW) and steam dump systems. Unit 2 is currently stable in Mode 6 for a maintenance outage and was not affected.
"Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour, non-emergency notification per 10 CFR 50.72 (b)(3)(iv)(A) as an event that results in a valid actuation of the AFW system. The AFW system started automatically and is operating as designed with the exception of the MDAFW LCVs for loop 1.
"There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The facility is in a 72 hour technical specification related to the auxiliary feedwater system. Sequoyah does not consider this to be a complex trip. The turbine trip is due to an electrical failure, and is still under investigation. Offsite power is qualified with no abnormalities.