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Event Notification Report for July 08, 2024

U.S. Nuclear Regulatory Commission
Operations Center

EVENT REPORTS FOR
07/07/2024 - 07/08/2024

EVENT NUMBERS
57217572155721357214
Agreement State
Event Number: 57217
Rep Org: NV Div of Rad Health
Licensee: Nevada Gold Mines, LLC - Goldstrike
Region: 4
City: Elko   State: NV
County:
License #: 05-11-13549-01
Agreement: Y
Docket:
NRC Notified By: Corey Creveling
HQ OPS Officer: Howie Crouch
Notification Date: 07/09/2024
Notification Time: 08:40 [ET]
Event Date: 07/08/2024
Event Time: 00:00 [PDT]
Last Update Date: 07/09/2024
Emergency Class: Non Emergency
10 CFR Section:
Agreement State
Person (Organization):
Gepford, Heather (R4DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
Event Text
AGREEMENT STATE REPORT - STUCK OPEN SHUTTER
The following information was received from the state of Nevada via email:

"Nevada Gold Mines LLC - Goldstrike, [Nevada license] 05-11-13545-01, reported a stuck open shutter on a Berthold LB 7440, serial number 1459. The fixed gauge remains installed pending the arrival of a contractor to replace the failed shutter. Radiation surveys of the installed gauges are as expected for a gauge in service giving 0.11 mR/hour 1 foot back from the gauge (in walkway). Gauge is installed in a location where there is occasional foot traffic, providing no additional exposure mine/mill staff until it can be repaired. Licensee [was] reminded to report the failure to the manufacturer in accordance with the operations and maintenance manual for the gauge."

The gauge contains 50 mCi of Cs-137. The state of Nevada considers this event closed.

Nevada Item Number: NV240005


Power Reactor
Event Number: 57215
Facility: Vogtle 3/4
Region: 2     State: GA
Unit: [3] [] []
RX Type: [3] W-AP1000,[4] W-AP1000
NRC Notified By: Tommie Sweat
HQ OPS Officer: Ernest West
Notification Date: 07/09/2024
Notification Time: 01:11 [ET]
Event Date: 07/08/2024
Event Time: 21:25 [EDT]
Last Update Date: 07/09/2024
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(2)(iv)(A) - ECCS Injection 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
Suggs, LaDonna (R2DO)
Grant, Jeffery (IR)
Felts, Russell (NRR EO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
3 M/R Y 100 Power Operation 0 Safe Shutdown
Event Text
MANUAL REACTOR TRIP AND AUTOMATIC SAFEGUARDS ACTUATION

The following information was provided by the licensee via email:

"At 2125 EDT on 07/08/2024, with Unit 3 in Mode 1 at 100 percent power, the reactor was manually tripped due to main feedwater pump `A' miniflow valve failing open, which resulted in lowering steam generator water level. Additionally, an automatic safeguards actuation occurred due to the cooldown of the reactor coolant system. The trip was not complex, with all safety systems responding normally post-trip.

"Operations responded and stabilized the plant. Decay heat is being removed by the passive residual heat removal heat exchanger. Units 1, 2, and 4 are not affected.

"Due to the core makeup tank actuation, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). The reactor protection system actuation while critical is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, this event is reportable per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid containment isolation actuation and a valid passive residual heat removal heat exchanger actuation.

"There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."

The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:

The cause of the main feedwater pump 'A' miniflow valve failing open was unknown and under investigation at the time of the notification of this event to the NRC.


Power Reactor
Event Number: 57213
Facility: Harris
Region: 2     State: NC
Unit: [1] [] []
RX Type: [1] W-3-LP
NRC Notified By: Trent Plummer
HQ OPS Officer: Ernest West
Notification Date: 07/08/2024
Notification Time: 11:04 [ET]
Event Date: 07/08/2024
Event Time: 07:48 [EDT]
Last Update Date: 07/08/2024
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(xi) - Offsite Notification
Person (Organization):
Suggs, LaDonna (R2DO)
Grant, Jeffery (IR)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 100 Power Operation 100 Power Operation
Event Text
INADVERTENT SIREN ACTIVATION

The following information was provided by the licensee via fax and email:

"On July 8, 2024, at 0748 EDT, six emergency response sirens were inadvertently actuated. Four sirens are located in Chatham County and two sirens are in Wake County. The first notification was made to Wake County at 0754. Investigation is ongoing to determine the cause of the actuation. Duke Energy notified the state and all counties within the emergency planning zone (EPZ). A press release was issued by Wake and Chatham Counties.

"This is a four-hour notification, non-emergency for the notification of another government agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi).

"There was no impact to the health and safety of the public or plant personnel.

"The NRC resident inspector has been notified."



Power Reactor
Event Number: 57214
Facility: Watts Bar
Region: 2     State: TN
Unit: [1] [] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: Paul Blakely
HQ OPS Officer: Sam Colvard
Notification Date: 07/08/2024
Notification Time: 18:24 [ET]
Event Date: 07/08/2024
Event Time: 15:21 [EDT]
Last Update Date: 07/08/2024
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS Actuation - Critical 50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation
Person (Organization):
Suggs, LaDonna (R2DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 A/R Y 100 Power Operation 0 Hot Standby
Event Text
AUTOMATIC REACTOR TRIP

The following information was provided by the licensee via phone and email:

"At 1521 EDT on July 8, 2024, with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main turbine trip. The [reactor] trip was not complex with all systems responding normally post trip.

"Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser using the steam dump system and the auxiliary feedwater (AFW) system. Unit 2 is not affected.

"Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the AFW system (an engineered safety feature) is being reported as an eight-hour report under 10 CFR 50.72(b)(3)(iv)(A).

"There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified."

The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:

The specific cause of the turbine trip is under investigation by the licensee.