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Event Notification Report for September 09, 2022

U.S. Nuclear Regulatory Commission
Operations Center

EVENT REPORTS FOR
09/08/2022 - 09/09/2022

Fuel Cycle Facility
Event Number: 55220
Facility: Bwx Technologies
RX Type: Uranium Fuel Fabrication
Comments: Heu Fabrication & Scrap Recovery
Naval Reactor Fuel
Region: 2
City: Lynchburg   State: VA
County: Campbell
License #: SNM-42
Docket: 07000027
NRC Notified By: Chris Terry
HQ OPS Officer: Ossy Font
Notification Date: 04/29/2021
Notification Time: 09:07 [ET]
Event Date: 04/28/2021
Event Time: 12:30 [EDT]
Last Update Date: 09/08/2022
Emergency Class: Non Emergency
10 CFR Section:
Person (Organization):
NMSS_EVENTS_NOTIFICATION (EMAIL)
MILLER, MARK (R2DO)
FUELS GROUP, - (EMAIL)
Event Text
CONCURRENT REPORT FOR OFFSITE NOTIFICATION

"BWXT is making a concurrent report to the NRC for an OSHA [(Occupational Safety and Health Administration)] reportable event under 29 CFR 1904.39(b)(2). The report of a workplace injury requiring the hospitalization of an employee was made to OSHA at 1230 EDT on 4/28/2021. At this time the incident is under investigation. While repositioning a component on a cart, the cart shifted causing the component to pinch the operators thumb and index finger. The employee was transported and admitted to Lynchburg General Hospital by BWXT's emergency team for treatment."

It was determined that the individual did not have contamination.

The licensee notified the NRC Resident Inspector.


Non-Agreement State
Event Number: 55994
Rep Org: West Virginia University
Licensee: West Virginia University
Region: 1
City: Morgantown   State: WV
County:
License #: 47-23066-02
Agreement: N
Docket:
NRC Notified By: Stephen Root
HQ OPS Officer: Lloyd Desotell
Notification Date: 07/15/2022
Notification Time: 14:00 [ET]
Event Date: 06/22/2022
Event Time: 00:00 [EDT]
Last Update Date: 09/08/2022
Emergency Class: Non Emergency
10 CFR Section:
20.2201(a)(1)(ii) - Lost/Stolen LNM>10x
Person (Organization):
Bickett, Brice (R1DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
ILTAB, (EMAIL)
Event Text
MISSING I-125 SEED

The following information was provided by the licensee via email:

"On June 22, 2022, West Virginia University Radiation Safety Department discovered that one Iodine-125 seed (Isoaid Model IAl-125A, titanium capsule sealed source, seed lot number 202280796) used in a Radioactive Seed Localization procedure was missing. The seed, with an activity of 268 microCi, was implanted into a lesion in the patient's right breast on June 16, 2022. A second seed, with the same activity, was implanted into the same lesion in the patient's right breast on the same day. A third seed, with the same activity, was implanted into a lesion in the patient's left breast on the same day. The surgery to remove the lesions was completed on the same day. On June 21, 2022, a Radiation Safety specialist picked up 2 seeds from the patient in question along with 7 seeds from different patients. At this time the Radiation Safety specialist did not have seed implantation records for all the seeds retrieved as they were not available at the Breast Care Center. On June 22, 2022, the specialist retrieved the seed implantation records and noted that the patient in question had a total of three seeds implanted and reported the seed as missing to the Radiation Safety Department Manager. An investigation determined that the seed arrived in the Pathology Gross Room but was likely inadvertently discarded in the trash or flushed down the sink."

THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL

Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf


!!!!! THIS EVENT HAS BEEN RETRACTED !!!!!
!!!!! THIS EVENT HAS BEEN RETRACTED !!!!!
Power Reactor
Event Number: 56054
Facility: Fermi
Region: 3     State: MI
Unit: [2] [] []
RX Type: [2] GE-4
NRC Notified By: Greg Miller
HQ OPS Officer: Brian Lin
Notification Date: 08/18/2022
Notification Time: 01:20 [ET]
Event Date: 08/17/2022
Event Time: 21:08 [EDT]
Last Update Date: 09/08/2022
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(3)(v)(D) - Accident Mitigation
Person (Organization):
Orth, Steve (R3DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
2 N Y 100 Power Operation 100 Power Operation
Event Text
EN Revision Imported Date: 9/8/2022

EN Revision Text: SAFETY SYSTEM INOPERABILITY

The following information was provided by the licensee via email:

"At 2108 EDT on August 17, 2022 the Division 2 Mechanical Draft Cooling Tower (MDCT) fans were declared inoperable due to failure of the over speed fan brake inverter. The brakes prevent fan over speed from a design basis tornado. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system. The Division 2 EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) room cooler and Division 2 Control Center HVAC (CCHVAC) chiller. An unplanned HPCI inoperability occurred based on a loss of the HPCI Room Cooler. At the time of the event, Division I CCHVAC was inoperable for maintenance (but was running for a maintenance run) and the event caused an inoperability of Division 2 CCHVAC. This resulted in an inoperability of both divisions of CCHVAC. Failure of the Division 2 MDCT Fan brake inverter occurred due to a trip of the DC input breaker. The breaker was reset at 2128 EDT restoring Division 2 UHS Operability. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfilment of the safety function of structures or systems that are needed to mitigate the consequences of an accident based on a loss of a single train safety system and loss of both divisions of a safety system.

"The Senior NRC Resident Inspector has been notified"

* * * RETRACTION ON 09/08/2022 AT 0856 EDT FROM JEFF MYERS TO MIKE STAFFORD * * *

The following information was provided by the licensee via email:

"On 8/17/22 at 2108 EDT the Division 2 (Div. 2) mechanical draft cooling tower (MDCT) brake inverter input breaker tripped for an unknown cause. The result of the loss of power was the inoperability of the MDCT fan brakes which impacts the ultimate heat sink (UHS) (TS 3.7.2). The UHS cascades to the EECW (emergency equipment cooling water) (TS 3.7.2) which is a support system for Div. 2 CCHVAC (Control Cell) Chiller A/C system (TS 3.7.4). This resulted in the inoperability of the Div. 2 CCHVAC Chiller.

"The cause for the breaker to trip is an intermittent electrical transient. Immediate corrective action was to reset the breaker, and the long-term action is to implement a modification to mitigate susceptibility to voltage variations. Div. 1 has implemented this long-term mod and no unexpected trips have occurred to date.

"Div. 1 CCHVAC Chiller was previously inoperable from equipment issues which was repaired, and the unit was in service for a 24-hour confidence run. Although licensed personnel had not completed the administrative actions for documenting operability during the 24-hour confidence run to monitor parameters, the (post maintenance test) PMT related to the maintenance was already completed, which included a 4-hour run in accordance with surveillance 24.413.01, Div. 1 and Div. 2 Chilled Water Pump and Valve, to verify normal operation and motor current. These PMT's were completed prior to the identified inoperability of the Div. 2 UHS due to the tripped breaker on the brake power supply.

"At the time of the MDCT brake inverter trip, the Operations' Senior License and the Night Shift Manager were aligned that, although still operating as part of the 24-hour confidence run, the unit was in service and capable of performing its safety function, but the administrative tasks were not completed, the Limited Condition of Operation (LCO) sheet had not been cleared, and no log entries were made. Since the Div. 1 Chiller was, in fact, operable at the time of the trip of the breaker on the inverter, this would allow the use of Technical Specification (TS) 3.0.9 'Barriers'. Per Operations Department Expectation (ODE)-12 `LCOs' (standard guidance and expectations for preparing and implementing an LCO), Operations determined that the MDCT brakes are barriers to a tornado event and TS 3.0.9 could be utilized. By invoking TS 3.0.9, as long as all other supported systems in the other division are operable, Div. 2 supported systems relying upon the UHS can remain operable and the Automatic Depressurization System (ADS) and Reactor Core Isolation Cooling (RCIC) system can be used as backup to the High Pressure Coolant Injection (HPCI) system. Based on this information, there was no loss of safety function with CCHVAC A/C system or HPCI. Therefore, the NRC non-emergency 10CFR50.72(b)(3)(v)(D) report was not required and the NRC report 56054 can be retracted."

The NRC Resident Inspector has been notified.

Notified R3DO (Orlikowski)


Agreement State
Event Number: 56083
Rep Org: Illinois Emergency Mgmt. Agency
Licensee: Bard Brachytherapy
Region: 3
City: Carol Stream   State: IL
County:
License #: IL-02062
Agreement: Y
Docket:
NRC Notified By: Gary Forsee
HQ OPS Officer: Ian Howard
Notification Date: 09/01/2022
Notification Time: 17:36 [ET]
Event Date: 08/31/2022
Event Time: 00:00 [CDT]
Last Update Date: 09/01/2022
Emergency Class: Non Emergency
10 CFR Section:
Agreement State
Person (Organization):
Hills, David (R3DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
ILTAB, (EMAIL)
Event Text
AGREEMENT STATE REPORT - LOST I-125 BRACHYTHERAPY SEEDS

The following information was provided by Illinois Emergency Management Agency, Radioactive Materials Branch (the Agency) via email:

"The Agency received a partial report via email from the licensee on September 1, 2022, indicating the potential loss of two brachytherapy seeds, accounting for a maximum estimated activity of 1.05 millicuries. The licensee has conducted an investigation and although the package appeared undamaged; believes the seeds may have been lost in transit from Atlanta Medical Center in Atlanta, GA. Requests for clarification and the nuclide (either I-125 or Pd-103) have not yet been returned. The amount and form of radioactivity would not be useful for illicit intent and there is no indication of intentional theft or diversion. While incomplete, this incident has the potential to be reportable and will be communicated to the United States Nuclear Regulatory Commission Headquarters Operations Officers today.

"On August 8, 2022, Bard Brachytherapy received a package from the Atlanta Medical Center. The package contained sources that were outside of the primary container and were lodged in the packaging foam. The shipping box looked undamaged from the outside, but three of the four primary containers were loose or open inside. The licensee counted the sources in the package and found 28. The return sticker included in the box from Atlanta Medical Center listed that 30 sources should have been returned. Surveys were conducted of the packaging material, the receiving and returns processing areas, and the path between to verify that the unaccounted-for sources were not in the Illinois facility. The counts were verified with the shipper and the licensee confirms two brachytherapy seeds (likely I-125) were most likely lost in transit."

Illinois Incident Number: IL220031

THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL

Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf


Agreement State
Event Number: 56084
Rep Org: Colorado Dept of Health
Licensee: CTC-Geotek, Inc.
Region: 4
City: Lakewood   State: CO
County: Jefferson
License #: CO 552-01
Agreement: Y
Docket:
NRC Notified By: Will Hageman
HQ OPS Officer: Karen Cotton-Gross
Notification Date: 09/01/2022
Notification Time: 15:19 [ET]
Event Date: 08/31/2022
Event Time: 04:15 [MDT]
Last Update Date: 09/01/2022
Emergency Class: Non Emergency
10 CFR Section:
Agreement State
Person (Organization):
Josey, Jeffrey (R4DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
ILTAB, (EMAIL)
Event Text
AGREEMENT STATE REPORT - STOLEN PORTABLE GAUGE
The following information was provided by the Colorado Department of Public Health and Environment via email:
"A call was received on 9/1/2022, at approximately 1200 MST from the RSO [Radiation Safety Officer] for CTC-Geotek, Inc. reporting a theft of a portable nuclear gauge, Instrotek model 3430, serial number 32097, containing 10 mCi of Cesium -137 and 40 mCi of Americium - 241:Beryllium. The gauge was stolen from the back of an employee's truck that was parked at their residence. The truck was in the parking lot of their apartment complex. Bolt cutters broke the chains used to secure the gauge transport case to the truck. Local law enforcement was informed."

Colorado Event Report ID No.: CO220030



THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL

Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf


Agreement State
Event Number: 56086
Rep Org: NJ Dept of Environmental Protection
Licensee: Bristol Meyers Squibb
Region: 1
City: Lawrenceville   State: NJ
County:
License #: 691580
Agreement: Y
Docket:
NRC Notified By: Debbie Wenke
HQ OPS Officer: Thomas Herrity
Notification Date: 09/02/2022
Notification Time: 16:33 [ET]
Event Date: 09/02/2022
Event Time: 16:49 [EDT]
Last Update Date: 09/02/2022
Emergency Class: Non Emergency
10 CFR Section:
Agreement State
Person (Organization):
Gray, Mel (R1DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)
ILTAB, (EMAIL)
Event Text
AGREEMENT STATE REPORT - LOST EXIT SIGN

The following was received from the New Jersey, Dept. of Environmental Protection (NJDEP) via email:

"At 1300 hours on September 1, 2022, the Radiation Safety Officer of Bristol Meyers Squibb (BMS) was in the process of disposing of all their radioactive exit signs when they went to a storage room and found one to be missing. NJDEP was notified immediately. The Exit sign in question is manufactured by SRBT, S/N 152299, originally containing 20 Ci of H-3 and had an expiration date of 2010. BMS will forward a written report within 30 days concerning the loss and their investigation."

NJ incident number: Not applicable at this time.


THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL

Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf


Power Reactor
Event Number: 56094
Facility: South Texas
Region: 4     State: TX
Unit: [1] [] []
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: William Herzog
HQ OPS Officer: Michael Bloodgood
Notification Date: 09/07/2022
Notification Time: 15:06 [ET]
Event Date: 07/28/2022
Event Time: 17:05 [CDT]
Last Update Date: 09/07/2022
Emergency Class: Non Emergency
10 CFR Section:
50.73(a)(1) - Invalid Specif System Actuation
Person (Organization):
Pick, Greg (R4DO)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 100 Power Operation 100 Power Operation
Event Text
INVALID SYSTEM ACTUATION

The following information was provided by the licensee via fax:

"Auxiliary Feedwater Pump #12 actuation and isolation of the Steam Generator Blowdown for 'A', 'B' and 'C' Steam Generators.

"Per 10 CFR 50.73(a)(1), the telephone notification is made under 10 CFR 50.73(a)(2)(iv)(A) for an invalid actuation. On 7/28/2022 at 1705 CDT, the Unit 1 Control Room received alarm SPQD0183 'SG LO-LO LVL TRN B ACT' and actuation of the Auxiliary Feedwater Pump #12 and isolation of the Steam Generator Blowdown for 'A', 'B' and 'D' Steam Generators. This event was classified as an unplanned entry into Technical Specification Shutdown LCO equal to or less than 24 hours 'Simple Restoration', due to the availability of CRMP.

"This alarm occurred several times and with each occurrence the alarm was short lived (1 second or less). Operations placed Auxiliary Feedwater Pump #12 in the Pull-To-Lock position to prevent starting of the pump with each alarm occurrence. During troubleshooting it was determined that SSPS Logic 'R' train was generating the intermittent alarm condition. A Logic board and a Safeguard Driver board were replaced which was identified as the possible cause. Operations performed applicable sections of the Logic test to ensure SSPS 'R' train operable.

"The event had no effects/consequences on the unit. The Logic board and Safeguard Driver board in SSPS 'R' train were both replaced as the possible causes, and therefore both boards were sent to Westinghouse to determine which board was at fault."

The NRC Resident Inspector has been notified.


Power Reactor
Event Number: 56095
Facility: Surry
Region: 2     State: VA
Unit: [1] [2] []
RX Type: [1] W-3-LP,[2] W-3-LP
NRC Notified By: Alan Bialowas
HQ OPS Officer: Michael Bloodgood
Notification Date: 09/07/2022
Notification Time: 15:06 [ET]
Event Date: 09/07/2022
Event Time: 09:22 [EDT]
Last Update Date: 09/07/2022
Emergency Class: Non Emergency
10 CFR Section:
26.719 - Fitness For Duty
Person (Organization):
Miller, Mark (R2DO)
FFD Group, (EMAIL)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 100 Power Operation 100 Power Operation
2 N Y 100 Power Operation 100 Power Operation
Event Text
FITNESS FOR DUTY REPORT

A licensed employee had a confirmed positive for alcohol during a random fitness-for-duty test. Unescorted access for the individual has been denied at all Dominion Energy sites.