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Event Notification Report for November 27, 2021

U.S. Nuclear Regulatory Commission
Operations Center

EVENT REPORTS FOR
11/26/2021 - 11/27/2021

EVENT NUMBERS
55612
Power Reactor
Event Number: 55612
Facility: Oconee
Region: 2     State: SC
Unit: [2] [] []
RX Type: [1] B&W-L-LP,[2] B&W-L-LP,[3] B&W-L-LP
NRC Notified By: Will Beekman
HQ OPS Officer: Howie Crouch
Notification Date: 11/27/2021
Notification Time: 13:16 [ET]
Event Date: 11/27/2021
Event Time: 05:19 [EST]
Last Update Date: 11/27/2021
Emergency Class: Non Emergency
10 CFR Section:
50.72(b)(3)(iv)(A) - Valid Specif Sys Actuation 50.72(b)(3)(v)(B) - Pot Rhr Inop
Person (Organization):
Miller, Mark (R2)
Power Reactor Unit Info
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
2 N N 0 Cold Shutdown 0 Cold Shutdown
Event Text
EN Revision Imported Date: 12/27/2021

EN Revision Text: AUTOMATIC ACTUATION OF THE EMERGENCY AC ELECTRICAL POWER SYSTEM

"At 0519 EST on November 27, 2021, with Unit 2 in Mode 5 at zero percent power, an actuation of the Emergency AC Electrical Power System occurred. The reason for the Emergency AC Electrical Power System auto-start was a lockout of the CT-2 transformer; causing a temporary loss of AC power to the main feeder bus. The Keowee Hydroelectric Units 1 and 2 automatically started as designed when a main feeder bus undervoltage signal was received.

"This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Emergency AC Electrical Power System.

"Additionally, the temporary loss of AC power resulted in a loss of Decay Heat Removal (DHR) that was restored upon power restoration to the main feeder bus. Therefore, this condition is also being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v) for an event or condition that could have prevented fulfillment of a safety function.

"There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified."

The loss of the CT-2 transformer is under investigation. Main feeder bus power was restored within a minute so no plant heat up occurred as a result of the loss of the decay heat removal system.