INVALID SPECIFIED SYSTEM ACTUATION
"This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system.
"On March 16, 2020, at approximately 0102 CDT, Browns Ferry Nuclear Plant (BFN), Unit 3 received motor trip-out alarms and diagnosed Group 2 and 3 Primary Containment Isolation System (PCIS) Isolations, 3C Residual Heat Removal (RHR) Pump tripping and Reactor Water Cleanup (RWCU) system isolating. All affected safety systems responded as expected. BFN, Unit 3, was nearing the end of the U3R19 refueling outage at the time of the event, and was still dependent on the Shutdown Cooling (SDC) system. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. At the time of the event, these conditions did not exist: therefore, the PCIS actuation was invalid.
"The event was determined to have been caused by clearance restoration activities in an unprotected control panel. A fuse re-installation inadvertently created a fault condition between two different plant 120 VAC power sources when the fuse holder's lower spring clip contacted a different fuse. This was a result of age-related degradation of the fuse holder, its close proximity to other fuses, and the lack of insulating isolation barriers between fuses.
"There were no safety consequences or impact to the health and safety of the public as a result of this event.
"This event was entered into the Corrective Action Program as Condition Report 1594925.
"The NRC Resident Inspector has been notified of this event." |