Event Notification Report for June 13, 2019
U.S. Nuclear Regulatory Commission Event Reports For ** EVENT NUMBERS ** |
54100 | 54112 | 54113 | 54116 |
Agreement State | Event Number: 54100 |
Rep Org: LOUISIANA RADIATION PROTECTION DIV Licensee: BLUE CUBE SOLUTIONS, LLC Region: 4 City: PLAQUEMINE State: LA County: License #: LA-13286-L01 Agreement: Y Docket: NRC Notified By: JOSEPH NOBLE HQ OPS Officer: HOWIE CROUCH | Notification Date: 06/04/2019 Notification Time: 14:18 [ET] Event Date: 06/03/2019 Event Time: 00:00 [CDT] Last Update Date: 06/04/2019 |
Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): RAY KELLAR (R4DO) NMSS_EVENTS_NOTIFICATION (EMAIL) |
Event Text
AGREEMENT STATE REPORT - STUCK SHUTTER ON PROCESS GAUGE The following information was received from the state of Louisiana via email: "On 06/03/2019, BCS [Blue Cube Solutions] detected a malfunction of an internal shutter of a gauge installed on a process. The gauge shutter would not function as designed by the manufacturer due to a rotor tip on an internal shutter. BCS called a service contractor, BBP Sales, to evaluate the situation and determine the best course of action to correct the problem. "The source and device with will remain installed on the process until the repairs are completed. This is not a radiation exposure hazard and does not pose a health and safety situation for the BCS employees or the general public. "This event is being reported to the NRC OP CENTER as required by Regulatory Requirement 10 CFR Part 30.50 (b)(2) & LAC 33:XV 340.B. "The Level Gauge is an OHMART, Model SHF-1, S/N M 6989, loaded with an approximately 120 mCi Cs-137 source, Model # A-2102." Louisiana Report ID No.: LA-190008 |
Power Reactor | Event Number: 54112 |
Facility: WATTS BAR Region: 2 State: TN Unit: [1] [2] [] RX Type: [1] W-4-LP,[2] W-4-LP NRC Notified By: MATTHEW MILLER HQ OPS Officer: MICHAEL BLOODGOOD | Notification Date: 06/12/2019 Notification Time: 11:55 [ET] Event Date: 06/12/2019 Event Time: 08:49 [EDT] Last Update Date: 06/12/2019 |
Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): ERIC MICHEL (R2DO) |
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | |||||||
1 | N | Y | 100 | Power Operation | 100 | Power Operation | |||||||
2 | N | Y | 100 | Power Operation | 100 | Power Operation |
Event Text
LOSS OF CONTROL ROOM EMERGENCY AIR TEMPERATURE CONTROL SYSTEM "At 0849 (EDT), a significant air leak on an inline air filter was identified. At 0908, the leak on the filter was isolated. A subsequent review of this situation determined that this air leak impacted operation of the A Train of the Control Room Emergency Air Temperature Control System (CREATCS) which is required to be operable in accordance with Technical Specification 3.7.10. At the time of this event, the B Train of CREATCS was out of service for planned maintenance. "With both trains of CREATCS out of service, both Watts Bar Units entered a condition that could have prevented fulfillment of a safety function. This condition was terminated when the leaking air filter was isolated. This event is being reported pursuant to 10 CFR 50.72(b)(3)(v)(D). "NRC Resident Inspector has been notified." |
Power Reactor | Event Number: 54113 |
Facility: COLUMBIA GENERATING STATION Region: 4 State: WA Unit: [2] [] [] RX Type: [2] GE-5 NRC Notified By: QUOC VO HQ OPS Officer: MICHAEL BLOODGOOD | Notification Date: 06/12/2019 Notification Time: 12:17 [ET] Event Date: 06/11/2019 Event Time: 20:04 [PDT] Last Update Date: 06/12/2019 |
Emergency Class: NON EMERGENCY 10 CFR Section: 26.719 - FITNESS FOR DUTY | Person (Organization): GREG WARNICK (R4DO) FFD GROUP (EMAIL) |
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | |||||||
2 | N | N | 0 | Refueling | 0 | Refueling |
Event Text
FITNESS FOR DUTY - CONTRACT EMPLOYEE SUPERVISOR CONFIRMED POSITIVE FOR ALCOHOL A contract employee supervisor had a confirmed positive test for alcohol during a random fitness-for-duty test. The employee's access to the plant had been terminated. The NRC Resident Inspector has been notified. |
Power Reactor | Event Number: 54116 |
Facility: BRUNSWICK Region: 2 State: NC Unit: [] [2] [] RX Type: [1] GE-4,[2] GE-4 NRC Notified By: LUCAS HOGGARD HQ OPS Officer: HOWIE CROUCH | Notification Date: 06/13/2019 Notification Time: 03:59 [ET] Event Date: 06/12/2019 Event Time: 21:27 [EDT] Last Update Date: 06/13/2019 |
Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): ERIC MICHEL (R2DO) |
Unit | SCRAM Code | RX Crit | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | |||||||
2 | N | Y | 100 | Power Operation | 100 | Power Operation |
Event Text
HIGH PRESSURE COOLANT INJECTION (HPCI) INOPERABLE "At 2127 EDT on June 12, 2019, during routine testing, the HPCI turbine experienced an overspeed trip and then subsequently restarted and ramped to the required speed. As a result, the response time of the system exceeded the 60-second acceptance criteria, thereby rendering the system inoperable. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The Reactor Core Isolation Cooling (RCIC) System and Automatic Depressurization System (ADS) are operable. "The safety significance of this event is minimal. Troubleshooting activities are in progress. "There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified." |
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021