United States Nuclear Regulatory Commission - Protecting People and the Environment
Home > NRC Library > Document Collections > Reports Associated with Events > Event Notification Reports > 2019 > June 05

Event Notification Report for June 05, 2019

U.S. Nuclear Regulatory Commission
Operations Center

Event Reports For
6/4/2019 - 6/5/2019

** EVENT NUMBERS **


53879 54098 54099

To top of page
Agreement State Event Number: 53879
Rep Org: ARKANSAS DEPARTMENT OF HEALTH
Licensee: UNIVERSITY OF ARKANSAS FOR MEDICAL SCIENCES
Region: 4
City: LITTLE ROCK   State: AR
County:
License #: ARK-0001-02110
Agreement: Y
Docket:
NRC Notified By: ANGIE HILL
HQ OPS Officer: THOMAS KENDZIA
Notification Date: 02/15/2019
Notification Time: 17:07 [ET]
Event Date: 02/13/2019
Event Time: 07:24 [CST]
Last Update Date: 06/04/2019
Emergency Class: NON EMERGENCY
10 CFR Section:
AGREEMENT STATE
Person (Organization):
VINCENT GADDY (R4DO)
NMSS_EVENTS_NOTIFICATION (EMAIL)

Event Text



EN Revision Imported Date : 6/5/2019

EN Revision Text: AGREEMENT STATE REPORT - DOSE DELIVERED WAS LESS THAN PRESCRIBED

The following was received from the Arkansas Department of Health, Radiation Control Program (the Department) via email:

"The treatment prescribed activity was for 0.54 GBq (14.5 mCi) on February 13, 2019. The calibrated activity at projected treatment time was 0.53 GBq (14.3 mCi). The patient received a dose of 0.204 GBq (5.51 mCi) due to 61.5 percent of the dose remaining in the connector of the manufacturer tubing and the catheter Terumo-Progreat Microcatheter (2.0 French Catheter). The Department performed an on-site review and investigation on February 15, 2019 at approximately 1215 [CST].

"The Department performed exposure surveys of the connector confirming activity stuck at the connector site. The connector site read the highest and in that concentrated area, reading 430 mR/hr, on February 15, 2019, at approximately 1415 [CST].

"There were no spills and/or contamination during this event.

"The licensee notified the manufacturer and the manufacturer will be performing an investigation on the tubing and radiopharmaceutical/sealed sources. The licensee is continuing to investigate the root cause and is preparing an initial fifteen day written report.

"The Department is waiting on information from the manufacturer(s) and licensee for further investigation. The Department will update this report when the licensee provides additional information."

Arkansas Event AR-2019-001

* * * UPDATE AT 1516 EST ON 3/7/19 FROM ANGIE HALL TO JEFF HERRERA * * *

The following update was received from the Arkansas Department of Health, Radioactive Materials Program via email:

"The Department [Arkansas Department of Health] received a Y-90 TheraSphere Glass Microsphere patient therapy misadministration notification on February 14, 2019 from a medical licensee. The Department performed an on-site review and investigation on February 15, 2019 at approximately 1215 [CST]. The Department has received the required initial fifteen day report from the Licensee.

"The Y-90 TheraSphere therapy prescribed activity was for 0.54 GBq (14.6 mCi) on February 13, 2019. The Y-90 TheraSphere calibrated activity at projected treatment time was 0.53 GBq (14.3 mCi). The patient received a dose of 0.204 GBq (5.51 mCi) due to 61.5 percent of the dose remaining in the connector of the manufacturer tubing and the catheter. The catheter used was a Terumo-Progreat Microcatheter (2.0 French Catheter). This dose resulted in a 54.34 Gy exposure instead of the intended 143 Gy exposure.

"The Licensee performs Y-90 TheraSphere therapies on a regular basis. The Licensee's physician/Authorized User and colleagues state that they have never had this issue before. The Authorized User states that 54.34 Gy is still a therapeutic dose. A patient CT follow-up scan will be performed to evaluate the therapy dose effectiveness.

"The Department verified activity stuck at the connector site via exposure surveys with a Fluke ion chamber survey meter (reading 430 mR/hr) on February 15, 2019 at approximately 1415 [CST].

"The Licensee notified the Manufacturer and the Manufacturer will be performing an investigation on the tubing and on the radioactive sealed sources.

"There were no spills and/or contamination during this event.

"The Department is waiting on information from the Licensee regarding the Manufacturer's investigation. The Department will update this report when the Licensee provides additional information.

"Corrective Actions: In Process by Licensee and Manufacturer."

Notified the R4DO (Werner), NMSS Events (via email).

* * * UPDATE FROM ANGIE HILL TO HOWIE CROUCH VIA EMAIL ON 4/24/19 AT 1708 EDT * * *

"The Department received a report on April 24, 2019 (dated April 4, 2019) from the Licensee regarding the Y-90 TheraSphere misadministration.

"The Department requested additional information on April 24, 2019, regarding the information provided by the Licensee. The request includes clarification from the manufacturer's report and the Licensee's corrective actions.

"The Department will update this report when the Licensee provides additional information."

Notified R4DO (Young) and NMSS Events (via email).

* * * UPDATE FROM ANGIE MORGAN HILL TO HOWIE CROUCH VIA EMAIL ON 6/4/19 AT 1150 EDT * * *

The following information was obtained from the state of Arkansas via email:

"The Licensee has submitted to the Department the Manufacturer's Report, possible Root Cause and Corrective Actions.

"According to the Manufacturer's Report, it states 'the most likely cause of this event is insufficient flow rate due to high backpressure associated with the microcatheter.' 'BTG [the manufacturer] recommends following the TheraSphere package insert guidance for the selection of a microcatheter with an inner diameter that is equal or larger than 0.020 inch.' The Manufacturer's Report also states, in part, 'A review of the manufacturing records confirmed there were no device defects.'

"It is noted by the Licensee that the Authorized User prescribed a different size microcatheter from the Manufacturer Recommendations and Manufacturer's package insert.

"The Licensee states regarding the root cause, 'After testing the tubing and catheter, it was determined that the event was caused by insufficient flow through the microcatheter possibly caused by overall length and inner diameter of the microcatheter, septum fragments from the dose vial, and possible changes in the condition of materials during the time from treatment to inspection (e.g. dried saline, coiled in tight bends for extended time.' 'Having several potential causes and contributing factors, the root cause is still not known.'

The Licensee states that their corrective actions to prevent reoccurrence are '(1) continue to abide by our standard operating procedure of performing three flushes, ensuring the electronic dosimeter, or rados, is reading zero, and surveying the patient; (2) Flush an additional time with 20 mL of saline after the rados reads zero; (3) Will use a catheter with a diameter greater than or equal to 0.02 inches. A smaller catheter will only be used if the patient would otherwise be unable to receive the treatment due to small vessels.'

The Department did not issue any Items of Noncompliance for this medical event.

The Department considers this event closed.

Notified R4DO (Kellar) and NMSS Events Notification (email).

A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.

To top of page
Power Reactor Event Number: 54098
Facility: LIMERICK
Region: 1     State: PA
Unit: [] [2] []
RX Type: [1] GE-4,[2] GE-4
NRC Notified By: STEVEN BARCZYK
HQ OPS Officer: OSSY FONT
Notification Date: 06/04/2019
Notification Time: 04:10 [ET]
Event Date: 06/04/2019
Event Time: 01:45 [EDT]
Last Update Date: 06/04/2019
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
Person (Organization):
ERIN CARFANG (R1DO)
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
2 M/R Y 100 Power Operation 0 Hot Shutdown

Event Text

MANUAL SCRAM DURING RAPID PLANT SHUTDOWN

"At 0145 EDT, on 6/4/19, Unit 2 was manually scrammed during a Rapid Plant Shutdown. At 64 percent reactor power, a Rapid Plant Shutdown was initiated due to lowering Main Condenser vacuum as a result of the loss of a plant electrical panel that powers Offgas System controls.

"The shutdown was normal and the plant is stable in Hot Shutdown with normal pressure control via the Main Turbine Bypass Valves to the Main Condenser and normal level control using Feedwater and Condensate. Main Condenser Vacuum has been restored."

The licensee notified the NRC Resident Inspector. Additionally, State and local government agencies were notified.

Prior to restarting Unit 2, an evaluation needs to be done due to the Unit 1 Diesel currently out of service for maintenance. The Unit 1 Diesel is a power supply for some of the common systems under the Unit 2 Technical Specifications and therefore required.

To top of page
Power Reactor Event Number: 54099
Facility: COOPER
Region: 4     State: NE
Unit: [1] [] []
RX Type: [1] GE-4
NRC Notified By: TERRELL HIGGINS
HQ OPS Officer: JEFFREY WHITED
Notification Date: 06/04/2019
Notification Time: 11:39 [ET]
Event Date: 06/04/2019
Event Time: 08:15 [CDT]
Last Update Date: 06/04/2019
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(xi) - OFFSITE NOTIFICATION
Person (Organization):
RAY KELLAR (R4DO)
Unit SCRAM Code RX Crit Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 100 Power Operation 100 Power Operation

Event Text

ISSUANCE OF PRESS RELEASE DUE TO SPURIOUS ACTUATION OF EMERGENCY SIRENS

"On 06/04/2019, Nebraska Public Power District will issue a press release concerning the spurious actuation of emergency sirens near Cooper Nuclear Station and Indian Cave State Park.

"This is a four hour report per 10 CFR 50.72(b)(2)(xi) for any event or situation for which a news release is planned or notification to other government agencies has been or will be made which is related to heightened public or government concern."

The cause of the siren actuation is still under investigation.

The licensee notified the NRC Resident Inspector.

* * * UPDATE FROM TERRELL HIGGINS TO HOWIE CROUCH AT 1301 EDT ON 6/4/19 * * *

"During this event, State & local government agencies (Nemaha County, Atchison County, Richardson County, and Indian Cave State Park) were contacted regarding the spurious actuation of emergency sirens. This is an update to the original Event Notification # 54099."

Notified R4DO (Kellar).


Page Last Reviewed/Updated Wednesday, June 05, 2019
Wednesday, June 05, 2019