U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/23/2018 - 03/26/2018 ** EVENT NUMBERS ** | !!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!! | Power Reactor | Event Number: 53192 | Facility: RIVER BEND Region: 4 State: LA Unit: [1] [ ] [ ] RX Type: [1] GE-6 NRC Notified By: Timothy Gates HQ OPS Officer: VINCE KLCO | Notification Date: 02/01/2018 Notification Time: 14:23 [ET] Event Date: 02/01/2018 Event Time: 10:57 [CST] Last Update Date: 03/23/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL | Person (Organization): RICK DEESE (R4DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | M/R | Y | 27 | Power Operation | 0 | Hot Shutdown | Event Text MANUAL REACTOR SCRAM "At 1057 CST on February 1, 2018 with the unit in Mode 1 at approximately 27% power, a manual actuation of the Reactor Protection System (RPS) was initiated due to an unexpected trip of the B Recirc Pump with A Recirc Pump in fast speed. B Recirc Pump tripped during transfer from slow to fast speed resulting in single loop operation. Operators were unable to reconcile differing indications of core flow. This resulted in a conservative decision to initiate a manual scram. The cause of the B Recirc Pump trip and the apparent issues with core flow indication are under investigation. The plant is currently stable in Mode 3. "The plant response to the scram was as expected. All control rods [fully] inserted as expected; the feedwater system is maintaining reactor vessel water level in the normal control band and reactor pressure is being maintained with steam line drains and main turbine bypass valves. "The NRC Senior Resident [Inspector] has been notified." * * * RETRACTION AT 1015 EDT ON 03/22/2018 FROM DAVID DABADIE TO OSSY FONT * * * "This event was initially reported under 10 CFR 72(b)(2)(iv)(B) as a manual actuation of the RPS due to an unexpected trip of the B Reactor Recirculation Pump with the A Reactor Recirculation Pump running in fast speed (Single Loop Operations). Operations was unable to reconcile differing indications of core flow and made the conservative decision to perform a planned shutdown in accordance with normal operating procedures. Therefore, this event 'resulted from and was part of a pre-planned sequence during testing or reactor operation' as specified in 10 CFR 50.72(b)(2)(iv)(B), 10 CFR 50.73(a)(2)(iv)(A) and NUREG-1022 Section 3.2.6. Consequently, this event is not reportable as an actuation of RPS. "The NRC Resident Inspector has been notified." R4DO (Groom) has been notified. | Non-Agreement State | Event Number: 53264 | Rep Org: TUV SUD AMERICA Licensee: TUV SUD AMERICA Region: 4 City: PASADENA State: TX County: License #: 42-32507-01 Agreement: Y Docket: NRC Notified By: MATTHIAS KRANEISS HQ OPS Officer: DAVID AIRD | Notification Date: 03/15/2018 Notification Time: 15:57 [ET] Event Date: 02/19/2018 Event Time: [CDT] Last Update Date: 03/15/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 30.50(b)(2) - SAFETY EQUIPMENT FAILURE | Person (Organization): JESSE ROLLINS (R4DO) NMSS_EVENTS_NOTIFICA (EMAI) | Event Text RADIOGRAPHY SOURCE STUCK IN SOURCE TUBE On 2/19/2018, a crew was performing work at the Phillips 66 Refinery in Billings, Montana. While moving the source into the open position, a loud noise was heard originating from the exposure set up area. The crew immediately attempted to crank the source back into the fully shielded position, but the attempt was unsuccessful. It was determined that the part to be inspected had tipped over and fallen onto the source tube, resulting in a crimp which prevented the source from being retracted into the fully shielded position. The source was shielded with lead plates, the crimp reduced, and the source successfully retracted into the fully shielded position. No members of the general public were exposed to any radiation and no workers received a dose exceeding the limit for personnel working with radiation sources. The source tube involved in this incident has been removed from service and destroyed. The exposure device involved in this incident has been inspected, checked for proper functionality, found to be in working order, and returned to service. The device was a QSA 880D exposure device containing an Iridium-192 source. | Power Reactor | Event Number: 53285 | Facility: MONTICELLO Region: 3 State: MN Unit: [1] [ ] [ ] RX Type: [1] GE-3 NRC Notified By: LT. LORI KIFFMEYER HQ OPS Officer: ANDREW WAUGH | Notification Date: 03/23/2018 Notification Time: 21:07 [ET] Event Date: 03/23/2018 Event Time: 12:30 [CDT] Last Update Date: 03/23/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): ERIC DUNCAN (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text LOSS OF EMERGENCY ASSESSEMENT CAPABILITY "This report is made for a loss of Emergency Assessment Capability associated with Emergency Action Levels for Toxic and Flammable Gas and is reportable under 10 CFR 50.72(b)(3)(xiii). During an emergency equipment inventory, it was identified that methods were not available to detect levels of toxic or flammable gas at the IDLH (Immediately Dangerous to Life and Health) level for a number of substances due to the detector having an unsuitable range. The IDLH is used to assess the Emergency Action Level Alert Range. "The ability of the Control Room Staff to detect and respond to the presence of toxic or flammable gas is unaffected. "Because there have been no chemical spills or releases that would require sampling to be performed, the health and safety of the public was not affected. "The resident NRC Inspector has been notified." The licensee will be notifying the state of Minnesota. | Power Reactor | Event Number: 53286 | Facility: PRAIRIE ISLAND Region: 3 State: MN Unit: [1] [2] [ ] RX Type: [1] W-2-LP,[2] W-2-LP NRC Notified By: DON HARTINGER HQ OPS Officer: STEVEN VITTO | Notification Date: 03/24/2018 Notification Time: 01:09 [ET] Event Date: 03/23/2018 Event Time: 16:35 [CDT] Last Update Date: 03/24/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): ERIC DUNCAN (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text LOSS OF EMERGENCY ASSESSMENT CAPABILITY "This report is made for a loss of Emergency Assessment Capability associated with Emergency Action Levels for Toxic and Flammable Gas and is reportable under 10 CFR 50.72 (b)(3)(xiii). During an emergency equipment inventory it was identified that methods were not available to detect levels of toxic or flammable gas at the IDLH (Immediately Dangerous to Life and Health) level for a number of substances. The IDLH is used to assess the Alert Emergency Action Level. "The ability of the Control Room Staff to detect and respond to the presence of toxic or flammable gas is unaffected. "Because there have been no chemical spills or releases that would require sampling to be performed, the health and safety of the public was not affected. "The NRC Resident Inspector has been notified." The State of Minnesota will be notified. | Power Reactor | Event Number: 53287 | Facility: PILGRIM Region: 1 State: MA Unit: [1] [ ] [ ] RX Type: [1] GE-3 NRC Notified By: JOSEPH FRATTASIO HQ OPS Officer: VINCE KLCO | Notification Date: 03/25/2018 Notification Time: 23:43 [ET] Event Date: 03/25/2018 Event Time: 16:16 [EDT] Last Update Date: 03/26/2018 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(ii)(A) - DEGRADED CONDITION 50.72(b)(3)(ii)(B) - UNANALYZED CONDITION | Person (Organization): RAY MCKINLEY (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | N | 0 | Cold Shutdown | 0 | Cold Shutdown | Event Text CONTROL ROD DRIVE PIPING POTENTIALLY INOPERABLE "On March 25, 2018 at 1616 hours [EDT], with the reactor in cold shutdown condition, two control rod drive piping lines were determined to be potentially inoperable in the event of a design basis earthquake due to support defects. The control rod drive piping forms a portion of the reactor coolant pressure boundary and primary containment boundary. "The supports will be repaired prior to plant startup. "This event had no impact on the health and/or safety of the public. "The NRC Resident Inspector has been notified." The licensee will notify the Commonwealth of Massachusetts. | |