U.S. Nuclear Regulatory Commission Operations Center Event Reports For 10/04/2017 - 10/05/2017 ** EVENT NUMBERS ** | Agreement State | Event Number: 52993 | Rep Org: KALISPELL REGIONAL MEDICAL CENTER Licensee: KALISPELL REGIONAL MEDICAL CENTER Region: 4 City: KALISPELL State: MT County: License #: 25-15463-01 Agreement: N Docket: 3009152 NRC Notified By: ANDRE VANTERPOOL HQ OPS Officer: VINCE KLCO | Notification Date: 09/26/2017 Notification Time: 15:39 [ET] Event Date: 05/01/2017 Event Time: [MDT] Last Update Date: 09/27/2017 | Emergency Class: NON EMERGENCY 10 CFR Section: 35.3045(a)(1) - DOSE <> PRESCRIBED DOSAGE | Person (Organization): DAVID PROULX (R4DO) NMSS_EVENTS_NOTIFICA (EMAI) | Event Text MEDICAL EVENT WRITTEN DOSE DIRECTIVE IS DIFFERENT THAN PRESCRIBED DOSE An endocrinologist specified a therapy dose of 20 milliCuries of I-131. An authorized dose directive was incorrectly written for 30 milliCuries of I-131. The patient was administered the initially determined dose of 20 milliCuries of I-131. Medical personnel determined that there was no impact on the patient. Hospital supervision notified the on-site Authorized User, the Radiation Safety Officer and the Medical Physicist. A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient. * * * UPDATE AT 1345 EDT ON 9/27/17 FROM ANDRE VANTERPOOL TO RICHARD L. SMITH * * * The actual event date was May 1, 2017, and the discovery date was September 25, 2017, at approximately 1500 MDT. Notified R4DO (Proulx) and NMSS Events Notification (via email). | Agreement State | Event Number: 52994 | Rep Org: OK DEQ RAD MANAGEMENT Licensee: CENTURY GEOPHYSICAL CORP Region: 4 City: TULSA State: OK County: License #: OK-04017-05 Agreement: Y Docket: NRC Notified By: KEVEN SAMPSON HQ OPS Officer: RICHARD SMITH | Notification Date: 09/27/2017 Notification Time: 12:38 [ET] Event Date: 09/27/2017 Event Time: 09:07 [CDT] Last Update Date: 09/27/2017 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): DAVID PROULX (R4DO) NMSS_EVENTS_NOTIFICA (EMAI) | Event Text AGREEMENT STATE REPORT - STUCK WELL LOGGING TOOL The following information was received from the State of Oklahoma via email and a follow-up phone call: Oklahoma Department of Environmental Quality notified us that they were notified on September 27, 2017, at 0907 CDT, by Century Geophysical Corp. (OK-04017-05) that a well logging tool was stuck at approximately 14 feet in a cased borehole. The tool contains a 1 Ci Am/Be source. They will provide more details on the source as soon as they are available. The initial plan is to dig the tool out. | Power Reactor | Event Number: 53000 | Facility: PERRY Region: 3 State: OH Unit: [1] [ ] [ ] RX Type: [1] GE-6 NRC Notified By: ALEX HALLMARK HQ OPS Officer: STEVE SANDIN | Notification Date: 10/04/2017 Notification Time: 05:53 [ET] Event Date: 10/04/2017 Event Time: 02:50 [EDT] Last Update Date: 10/04/2017 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(i) - PLANT S/D REQD BY TS 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION 50.72(b)(3)(v)(B) - POT RHR INOP 50.72(b)(3)(v)(C) - POT UNCNTRL RAD REL | Person (Organization): DAVID HILLS (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 82 | Power Operation | Event Text PERRY COMMENCED TECHNICAL SPECIFICATION REQUIRED SHUTDOWN "On October 4, 2017, at 0250 hours [EDT], the Perry Nuclear Power Plant commenced a Technical Specification (TS) shutdown by lowering reactor power from 100 percent rated thermal power to 98 percent to comply with TS LCO 3.0.3. Reactor power was further reduced to 82 percent rated thermal power at 0430 hours [EDT]. "The plant had entered TS 3.0.3 at 0155 hours [EDT] upon loss of MCC [Motor Control Center], Switchgear, and Miscellaneous Electrical Equipment Areas HVAC System train A while train B was removed from service for maintenance. MCC switchgear ventilation train A was declared inoperable based on excessive belt noise and a dropped belt on MCC switchgear supply fan A. This also constitutes a loss of safety function. "This event is being reported in accordance with 10 CFR 50.72(b)(2)(i) and 10 CFR 50.72(b)(3)(v)(D). "The NRC Resident Inspector was notified." * * * UPDATE ON 10/04/17 AT 0926 EDT FROM DAN HARTIGAN TO STEVEN VITTO * * * "Due to the loss of both trains of MCC, Switchgear, and Miscellaneous Electrical Equipment Areas HVAC, actions were taken in LCO 3.8.7 for AC and DC Distribution Systems, LCO 3.8.4 for DC Sources, LCO 3.8.1 for AC Sources, and the associated support systems, the High Pressure Core Spray system was also declared inoperable, which is a single train safety system and therefore, an additional loss of safety function. "This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(B), 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72 (b)(3)(v)(D). "At 0620 hours [EDT] the A train of MCC, Switchgear, and Miscellaneous Electrical Equipment Areas HVAC and High Pressure Core Spray was declared operable and LCO 3.0.3 was exited. The plant was restored to 100% [percent] power at 0804 [EDT]. "The NRC Resident Inspector was notified." Notified R3DO(Hills). | |