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Event Notification Report for August 21, 2017

U.S. Nuclear Regulatory Commission
Operations Center

Event Reports For
08/18/2017 - 08/21/2017

** EVENT NUMBERS **


52090 52895 52915 52918 52919

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Fuel Cycle Facility Event Number: 52090
Facility: WESTINGHOUSE ELECTRIC CORPORATION
RX Type: URANIUM FUEL FABRICATION
Comments: LEU CONVERSION (UF6 to UO2)
                   COMMERCIAL LWR FUEL
Region: 2
City: COLUMBIA State: SC
County: RICHLAND
License #: SNM-1107
Agreement: Y
Docket: 07001151
NRC Notified By: NANCY PARR
HQ OPS Officer: DONG HWA PARK
Notification Date: 07/14/2016
Notification Time: 18:49 [ET]
Event Date: 07/13/2016
Event Time: [EDT]
Last Update Date: 08/18/2017
Emergency Class: NON EMERGENCY
10 CFR Section:
PART 70 APP A (a)(4) - ALL SAFETY ITEMS UNAVAILABLE
PART 70 APP A (b)(1) - UNANALYZED CONDITION
Person (Organization):
DANIEL RICH (R2DO)
NMSS_EVENTS_NOTIFIC (EMAI)

Event Text

DEGRADED SAFETY ITEMS CAUSED BY URANIUM BUILDUP

"On July 13, 2016, it was determined by the Environment, Health and Safety (EH&S) department that scrubber clean-out material, found in the S-1030 scrubber transition section during the annual maintenance shutdown that occurred in late May, potentially exceeded the uranium mass limit for the scrubber transition.

"(IROFS [Items Relied on for Safety] VENT-S1030-110) requires annual inspection and removal of significant solids buildup in the transition section. Upon inspection, significant buildup was found, and the ductwork was opened to permit extensive cleanout. 36 containers of material with a total gross weight of 210.4 kg was removed from the inlet transition during the cleanout on May 28th to May 29th. Grab samples were subsequently taken from each container and analyzed for uranium concentration. On July 13th, the EH&S department was made aware that the grab sample results averaged 47.8% U. Although the exact uranium mass cannot be determined until the material is dissolved and representatively sampled, available evidence suggests that the mass limit of 29 kg U in the inlet transition was exceeded. The 29 kg U limit is based on an optimally moderated, fully reflected spherical geometry which very conservatively bounds the conditions in the inlet transition of the scrubber. IROFS remained to limit the quantity of uranium available to the scrubber (IROFS VENT-S1030-101, -102, -103 & -104), which are physical barriers designed to minimize uranium in the airflow entering the transition area. Continuous liquid spraying in the inlet transition section to limit solids accumulation (IROFS VENT-S1030-109) was also in place.

"The inlet transition and scrubber were thoroughly cleaned, and the uranium bearing solids were placed into favorable geometry containers. Also, the inspection and cleanout of the transition frequency was increased to monthly.

"Based on available but degraded IROFS, this accident sequence was unlikely. Therefore, this mass accident sequence does not meet the performance requirements of 10CFR70.61. The actual configuration remained safe at all times. Also, no external conditions affected the event.

"Immediate Corrective Actions:
NRC Region II personnel, who were onsite at the CFFF [Columbia Fuel Fabrication Facility], were made aware of the discovery.

"The Conversion area was shutdown to plan for a second extensive scrubber clean-out to validate that the accumulation of solids is a slow buildup over time. The last extensive cleanout was performed in 2009.

"An extent of condition was performed to determine if other scrubbers potentially had significant uranium buildup. Inspection data indicated that this material accumulation issue was limited to the S-1030 scrubber.

"This event has been entered into the facility Corrective Action Prevention And Learning system (CAPAL) #100397353."

* * * UPDATE PROVIDED BY NANCY PARR TO JEFF ROTTON AT 1025 EDT ON 07/26/2016 * * *

"Onsite chemical analysis confirmed that uranium mass limit for the scrubber transition piece was exceeded. The accumulated material contained 87 kgs of Uranium.

"The Criticality Safety Evaluation for this system was revised and implemented on July 20, 2016 to add Items Relied on For Safety to prevent recurrence of a mass exceedance while the causal analysis and additional corrective actions are completed."

Notified R2DO (Nease) and NMSS Events Notification Group via email.

* * * UPDATE PROVIDED BY NANCY PARR TO HOWIE CROUCH AT 1749 EDT ON 07/31/2016 * * *

"On July 31, 2016, it was determined by the Environment, Health and Safety (EH&S) department that clean-out material found in the S-1030 scrubber packing and floor also potentially exceeded the uranium mass limit for the scrubber criticality safety evaluation. Over years of operations, the same available but degraded mass prevention and inspection/clean-out IROFS did not prevent exceedance of the mass limit.

"This report is being upgraded to a 1 Hour Event Notification based on 10CFR70 Appendix A(a)(4).

"There was no consequence to the public, the workers or the environment.

"The scrubber process will remain in a safe shutdown mode until further investigation and corrective actions are completed."

Notified R2DO (Rose), IRD (Grant), NMSS EO (Kotzalas) and NMSS Events Notification via email.

* * * UPDATE FROM JOHN HOWELL TO VINCE KLCO AT 1620 EDT ON 8/7/2016 * * *

"On August 6, 2016 at 1700, it was reported to the Environment, Health and Safety (EH&S) department that residual material located within the abandoned S-1056 scrubber was sampled and confirmed to contain Uranium.

"24 Hour Event Notification based on 10CFR70 Appendix A(b)(1) 'Any event or condition that results in the facility being in a state that was not analyzed, was improperly analyzed, or is different from that analyzed in the Integrated Safety Analysis, and which results in failure to meet the performance requirements of 10CFR70.61.'

"The S-1056 is an out-of-service scrubber. When operational, it scrubbed the acid fumes from the Conversion area. It currently is an unanalyzed system without IROFS or controls. The reported volume of approximately 15 kg is well within safety margins.

"It was taken out of service in 2002, when the S-1030 scrubber replaced it. The material in the S-1056 was discovered as an extent of condition for the S-1030 event.

"The discovery and sampling were documented in Redbook 71409. At no time was there any actual or potential health and safety consequence to the workers, the public, or the environment."

The licensee notified the NRC Regional Inspector (Lopez).

Notified the R2DO (Suggs), R2RA (Haney) and NMSS Events Notification Group via email.

* * * UPDATE AT 1546 EDT ON 8/23/16 FROM NANCY PARR TO JEFF HERRERA * * *

"On August 23, 2016, during the extent of condition for this S-1030 scrubber system event, a review of inspection video for the S-1030 ductwork in Conversion identified material accumulation in an elbow which potentially could exceed the uranium mass limit for the elbow section (36.5 kgU).

"This report is being updated based on a potential to meet the 10 CFR 70 Appendix A(a)(4) in the ductwork.

"There was no consequence to the public, the workers or the environment.

"The scrubber process will remain in a safe shutdown mode until further investigation and corrective actions are completed."

The Region IV Project Managers were notified.

Notified the R2DO (Michel), IRDMOC (Stapleton) and NMSS Events Notification Group (via email).

* * * UPDATE AT 1810 EDT ON 9/15/16 FROM NANCY PARR TO DANIEL MILLS * * *

"24-Hour Event Notification based on 10 CFR 70 Appendix A(b)(1) 'Any event or condition that results in the facility being in a state that was not analyzed, was improperly analyzed, or is different from that analyzed in the Integrated Safety Analysis, and which results in failure to meet the performance requirements of 10 CFR 70.61.'

"On September 15, 2016 at 1204 EDT, it was reported to the Environment, Health and Safety (EH&S) department that residual material was located within the abandoned 3A/3B ventilation system. Based on gamma radiation surveys, the material contains Uranium.

"The 3A/3B system was taken out of service in 2002, when the S-1030 scrubber replaced it. When operational, it removed chemical fumes and particulate matter from the Conversion area. The material in the system was discovered as an extent of condition for the S-1030 event.

"When taken out of service, the system was isolated from the introduction of any additional material and/or moderator. However, because the system is out of service, it is considered an unanalyzed system without IROFS or controls. The reported depth of material in the duct appears well within analyzed safety margins for similar systems.

"At no time was there any actual or potential health and safety consequence to the workers, the public, or the environment.

"UPDATED INFORMATION FROM AUGUST 23, 2016 NOTIFICATION:
This notification also serves to update previously reported information provided on August 23, 2016 where a review of inspection video for the S-1030 ductwork in Conversion identified material accumulation in an elbow which potentially could exceed the uranium mass limit for the elbow section (36.5 kg U). This report was made based on a potential to meet the 10 CFR 70 Appendix A(a)(4) in the ductwork. The material was removed from the ductwork and weighed. The total weight of the material removed was 5.5 kgs in the elbow and 3.0 kgs in a horizontal section of the duct, which is well below the mass limit in the safety basis. Therefore, the information from the August 23, 2016 potential report is retracted."

Notified the R2DO (Walker) and NMSS Events Notification Group (via email).

* * * UPDATE AT 1701 EDT ON 10/05/16 FROM NANCY PARR TO JEFF HERRERA * * *

"On October 4, 2016 at approximately 1700 EDT, while performing housekeeping and cleanout activities on the out of service 3A and 3B ductwork, degradation was discovered in an area not routinely or readily accessed in the bottom of the out of service filter house system. This discovery was made while performing clean-out activities covered under a Radiation Work Permit (RWP).

"The work was stopped, and Health Physics (HP) performed contamination surveys of the area. The degraded area was sealed and isolated. No additional radiological controls were needed, and access to the area was not restricted.

"No degradation was found in other out of service systems on the roof. A comprehensive extent of condition is ongoing.

"There was no actual or potential health and safety consequence to the workers, the public, or to the environment during this time."

Notified the R2DO (Bonser) and NMSS Event Notification Group (via email).

* * * UPDATE AT 1113 EDT ON 08/18/17 FROM NANCY PARR TO BETHANY CECERE * * *

"On August 17, 2017 at 11:17 a.m., it was reported to the Environment, Health and Safety (EH&S) department that additional residual material located within the out of service S-1056 scrubber was found. Material in this out of service system was previously reported on August 7, 2016. The material was removed and placed into favorable geometry storage. The material has been quantified and determined to contain less than 80 grams of uranium, which is well within safety margins.

"This information is being reported in accordance with the 24 Hour Event Notification criterion: 10 CFR 70 Appendix A(b)(1), 'Any event or condition that results in the facility being in a state that was not analyzed, was improperly analyzed, or is different from that analyzed in the Integrated Safety Analysis, and which results in failure to meet the performance requirements of 10 CFR 70.61.'

"The buildup was not visible until dismantling the abandoned equipment for removal from the roof. Demolition and removal has already been completed for ventilation system filter houses 2A, 2B, 3A, 3B and 7A.

"The discovery and sampling were documented in Redbook 72846 and in CAPAL 100488919. At no time was there any actual or potential health and safety consequence to the workers, the public, or the environment."

The licensee discussed this report with NRC Region 2 (Vukovinsky and Michel).

Notified the R2DO (Sykes) and NMSS Event Notification Group (via email).

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Agreement State Event Number: 52895
Rep Org: TEXAS DEPT OF STATE HEALTH SERVICES
Licensee: PASADENA REFINING SYSTEM INC
Region: 4
City: PASADENA State: TX
County:
License #: 0134
Agreement: Y
Docket:
NRC Notified By: IRENE CASARES
HQ OPS Officer: JEFF HERRERA
Notification Date: 08/10/2017
Notification Time: 14:48 [ET]
Event Date: 08/09/2017
Event Time: [CDT]
Last Update Date: 08/10/2017
Emergency Class: NON EMERGENCY
10 CFR Section:
AGREEMENT STATE
Person (Organization):
HEATHER GEPFORD (R4DO)
NMSS_EVENTS_NOTIFICA (EMAI)

Event Text

AGREEMENT STATE REPORT - SHUTTER FAILURE DUE TO WATER INTRUSION

The following report was received from the Texas Department of State Health Services via email:

"On August 10, 2017, the licensee's radiation safety officer notified the Agency [Texas Department of State Health Services] that a fixed gauge (Ohmart Vega, SHLG-2, SN 8551CM, 3000 milliCuries, Cs-137) had a stuck shutter. A repair company was called and the technician completed repairs on the gauge within one day. Shutter failure was from water intrusion in the slide channel causing the shutter to rust and reduce movement. The gauge was cleaned and lubricated. A monthly maintenance procedure will be placed in effect to reduce or eliminate this issue."

Texas Incident: I-9503

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Power Reactor Event Number: 52915
Facility: RIVER BEND
Region: 4 State: LA
Unit: [1] [ ] [ ]
RX Type: [1] GE-6
NRC Notified By: DAN JAMES
HQ OPS Officer: BETHANY CECERE
Notification Date: 08/18/2017
Notification Time: 23:41 [ET]
Event Date: 08/18/2017
Event Time: 20:55 [CDT]
Last Update Date: 08/18/2017
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
Person (Organization):
THOMAS FARNHOLTZ (R4DO)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
1 A/R Y 100 Power Operation 0 Hot Shutdown

Event Text

AUTOMATIC SCRAM WHILE AT 100 PERCENT POWER

"At 2055 CDT on August 18, 2017, an automatic actuation of the reactor protection system occurred while the plant was operating at 100 percent power. No plant parameters requiring the actuation of the emergency diesel generators or the emergency core cooling system were exceeded. The main feedwater system remained in service following the scram to maintain reactor water level, and the main condenser remained available as the normal heat sink.

"The scram occurred after a planned swap of the main feedwater master controller channels in preparation for scheduled surveillance testing. When the channel swap was actuated, the feedwater regulating valves moved to the fully open position. The scram signal originated in the high-flux detection function of the average power range monitors, apparently from the rapid increase in feedwater flow.

"The cause of the apparent feedwater controller malfunction is under investigation. The NRC Resident Inspector has been notified."

No safety relief valves opened. Decay heat is being removed via steam to the main condenser using the bypass valves and steam drains. The licensee intends to go to Cold Shutdown to investigate the malfunction.

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Power Reactor Event Number: 52918
Facility: COLUMBIA GENERATING STATION
Region: 4 State: WA
Unit: [2] [ ] [ ]
RX Type: [2] GE-5
NRC Notified By: RICK KERRONE
HQ OPS Officer: DONALD NORWOOD
Notification Date: 08/20/2017
Notification Time: 22:46 [ET]
Event Date: 08/20/2017
Event Time: 16:05 [PDT]
Last Update Date: 08/20/2017
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL
Person (Organization):
THOMAS FARNHOLTZ (R4DO)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
2 M/R Y 100 Power Operation 0 Hot Shutdown

Event Text

MANUAL REACTOR SCRAM DUE TO A RISE IN MAIN CONDENSER BACK PRESSURE

"On August 20, 2017 at 1605 PDT, Columbia Generating Station was manually scrammed from 100 percent power due to a rise of Main Condenser back pressure. Manual scram of the unit is procedurally required upon a loss of Main Condenser back pressure. Preliminary investigations indicate that the Main Condenser air removal suction valve (AR-V-1) closed, resulting in the Condenser back pressure rising to within 1.0 inch Hg of the setpoint with reactor power greater than 25 percent. Further investigations continue. All control rods fully inserted.

"In addition to the closure of the air removal suction valve, one of two Reactor Feedwater startup flow control valves did not adequately operate to control Reactor vessel level and resulted in a high-level (Level-8) actuation tripping the Reactor Feedwater System. All other systems operated as expected. Reactor water level is currently being controlled manually with the start-up level control isolation valve. AR-V-1 has been manually opened with a jumper and temporary air supply. Reactor decay heat is being removed via bypass valves to the Main Condenser.

"This event is being reported under the following: 10 CFR 50.72(b)(2)(iv)(B), which requires a four-hour notification for any event or condition that results in actuation of the Reactor Protection System when the reactor is critical."

The licensee notified the NRC Resident Inspector.

The licensee plans to issue a press release.

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Power Reactor Event Number: 52919
Facility: BYRON
Region: 3 State: IL
Unit: [1] [2] [ ]
RX Type: [1] W-4-LP,[2] W-4-LP
NRC Notified By: ED SMITH
HQ OPS Officer: BETHANY CECERE
Notification Date: 08/21/2017
Notification Time: 05:30 [ET]
Event Date: 08/20/2017
Event Time: 21:08 [CDT]
Last Update Date: 08/21/2017
Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE
Person (Organization):
AARON McCRAW (R3DO)

Unit SCRAM Code RX CRIT Initial PWR Initial RX Mode Current PWR Current RX Mode
1 N Y 100 Power Operation 100 Power Operation
2 N Y 100 Power Operation 100 Power Operation

Event Text

LOSS OF EMERGENCY ASSESSMENT CAPABILITY DUE TO NON-FUNCTIONAL TSC VENTILATION

"On August 20, 2017 at 2108 hours CDT, Byron Station Technical Support Center (TSC) ventilation system supply fan (0VV23C) was identified as non-functional. This failure affects the ability of the TSC ventilation system to maintain adequate radiological habitability in the event of an emergency with an airborne radiological release. All other capabilities of the TSC are unaffected by this emergent condition. Currently troubleshooting/investigation is being performed. This condition is considered a major loss of emergency assessment capability and is reportable under 10CFR50.72(b)(3)(xiii). If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures. If the TSC becomes uninhabitable, the Station Emergency Director will relocate the TSC staff to an alternate TSC location in accordance with applicable procedures.

"This notification is being made in accordance with 10CFR50.72(b)(3)(xiii) due to the potential loss of an emergency response facility because of the unavailability of the ventilation system. An update will be provided once the TSC ventilation has been restored to normal operation.

"The NRC Resident Inspector has been notified."

Page Last Reviewed/Updated Thursday, March 25, 2021