U.S. Nuclear Regulatory Commission Operations Center Event Reports For 06/19/2015 - 06/22/2015 ** EVENT NUMBERS ** | Power Reactor | Event Number: 51165 | Facility: QUAD CITIES Region: 3 State: IL Unit: [1] [2] [ ] RX Type: [1] GE-3,[2] GE-3 NRC Notified By: JAMES COX HQ OPS Officer: JEFF HERRERA | Notification Date: 06/19/2015 Notification Time: 10:03 [ET] Event Date: 06/19/2015 Event Time: 01:53 [CDT] Last Update Date: 06/19/2015 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(C) - POT UNCNTRL RAD REL | Person (Organization): PATTY PELKE (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text SECONDARY CONTAINMENT INTERLOCK DOORS OPEN SIMULTANEOUSLY "On June 19, 2015, at 0153 CDT, two Secondary Containment interlock doors (1/2 EDG [Emergency Diesel Generator] room door and the Unit 1 reactor building door) were open simultaneously. The doors were immediately closed and secondary containment pressure remained negative. "This condition represents a failure to meet surveillance requirement 3.6.4.1.2 given two doors in a single access opening were open simultaneously. As a result entry into Technical Specification 3.6.4.1, Condition A, was made momentarily due to secondary containment being inoperable. "This event is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function. "The NRC Resident Inspector has been notified. "The door has been posted to notify to restrict access. "The State of Illinois Emergency Management has been notified." | Power Reactor | Event Number: 51168 | Facility: LIMERICK Region: 1 State: PA Unit: [ ] [2] [ ] RX Type: [1] GE-4,[2] GE-4 NRC Notified By: DAN WILLIAMSON HQ OPS Officer: STEVE SANDIN | Notification Date: 06/21/2015 Notification Time: 20:25 [ET] Event Date: 06/21/2015 Event Time: 16:25 [EDT] Last Update Date: 06/21/2015 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): BRICE BICKETT (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text MANUAL SECONDARY CONTAINMENT ISOLATION "In response to a trip of Unit 2 reactor enclosure HVAC [Heating, Ventilation and Air Conditioning], subsequent loss of reactor enclosure delta-p and rising reactor enclosure room temperatures, a Unit 2 manual secondary containment isolation was initiated per station procedures. This manual isolation also resulted in an isolation signal to containment atmosphere control (CAC) system valves and primary containment instrument gas (PCIG) system valves. System responses were as expected. "Unit 2 secondary containment delta-p and room temperatures were restored via the standby gas treatment system (SGTS), and Unit 2 secondary containment integrity remains intact and operable. "Investigation of the trip of Unit 2 reactor enclosure HVAC is ongoing. "This is being reported under 50.72(b)(3)(iv)(A) for containment isolation signal affecting containment isolation valves in more than one system." The licensee informed the NRC Resident Inspector. | |