U.S. Nuclear Regulatory Commission Operations Center Event Reports For 12/29/2014 - 12/30/2014 ** EVENT NUMBERS ** | Agreement State | Event Number: 50695 | Rep Org: PA BUREAU OF RADIATION PROTECTION Licensee: TRICAN WELL SERVICE Region: 1 City: MILL HALL State: PA County: License #: PA-G0076 Agreement: Y Docket: NRC Notified By: JOSEPH MELNIC HQ OPS Officer: DONG HWA PARK | Notification Date: 12/19/2014 Notification Time: 12:19 [ET] Event Date: 12/18/2014 Event Time: [EST] Last Update Date: 12/19/2014 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): DONNA JANDA (R1DO) NMSS EVENTS NOTIFICA (EMAI) | Event Text AGREEMENT STATE REPORT - SHUTTER FAILURE The following was received via email from the Commonwealth of Pennsylvania: "Notifications: The [Pennsylvania] Department [Bureau of Radiation Protection] was notified on 12/18/2014 of a shutter malfunction. This event is reportable within 24-hours per 10 CFR 30.50(b)(2). "Event Description: An operator tried to open the shutter handle, and it was hard to move. When the shutter did move, it spun freely and was put in the open position but no activity was observed. However, when the shutter was placed in the closed position activity was seen, thus verifying a malfunction. "Manufacturer: Berthold Technologies Model: LB8010 Serial Number: 10204 Isotope: Cs-137 Activity: 20 mCi "Cause of the event: Unknown at this time, possible sheared roll pin. "Action: Berthold, the manufacturer, was called to fix the damaged shutter handle. The [Pennsylvania] Department [Bureau of Radiation Protection] plans to follow-up with the licensee and the manufacturer. More information will be provided when received. "Event Report ID No: PA140024" | Agreement State | Event Number: 50698 | Rep Org: KENTUCKY DEPT OF RADIATION CONTROL Licensee: BIG RIVERS ELECTRIC CORPORATION Region: 1 City: WEST CENTERTOWN State: KY County: License #: 201-277-56 Agreement: Y Docket: NRC Notified By: ERIC PERRY HQ OPS Officer: HOWIE CROUCH | Notification Date: 12/22/2014 Notification Time: 13:05 [ET] Event Date: 11/24/2014 Event Time: [CST] Last Update Date: 12/22/2014 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): MARC FERDAS (R1DO) NMSS EVENTS NOTIFICA (EMAI) | Event Text KENTUCKY AGREEMENT STATE REPORT - FAILURE OF FIXED GAUGE ACTUATORS The following information was obtained from the Commonwealth of Kentucky via facsimile: "Failure of on/off mechanisms on three fixed gauges to function as designed. Failure discovered during routine testing of on/off mechanism by [the] licensee. The licensee has contacted the manufacturer to schedule removal/repair." The fixed gauges are in a normally inaccessible area and don't present a personnel exposure concern. The gauges contain Cs-137 with 100 mCi, 25 mCi, and 10 mCi respectively and are used at a coal fired facility. Kentucky Event Report ID: KY-14-0005 | Non-Agreement State | Event Number: 50699 | Rep Org: DASSAULT AIRCRAFT SERVICE Licensee: DASSAULT AIRCRAFT SERVICE Region: 1 City: NEW CASTLE State: DE County: License #: GL Agreement: N Docket: NRC Notified By: KEN HEAVLOW HQ OPS Officer: HOWIE CROUCH | Notification Date: 12/22/2014 Notification Time: 15:15 [ET] Event Date: 12/03/2014 Event Time: [EST] Last Update Date: 12/22/2014 | Emergency Class: NON EMERGENCY 10 CFR Section: 20.2201(a)(1)(i) - LOST/STOLEN LNM>1000X | Person (Organization): MARC FERDAS (R1DO) NMSS EVENTS NOTIFICA (EMAI) | This material event contains a "Less than Cat 3 " level of radioactive material. | Event Text LOST STATIC ELIMINATOR "Dassault Falcon Jet Wilmington Corp. has lost a leased piece of equipment that contains radioactive materials. The tool in question is an air blow gun leased from NRD, LLC. The blow gun model number is P-2021-1000, Serial number A2JT781 and was on lease number 055641 shipped on 12/03/2013. The blow gun [contains] 1.7 mCi (61 MBq) [of Po-210]. "The tool was used to remove static from aircraft interior windows and also to remove static from interior wood paneling between decorative finish coats. It was used primarily in the cabinet department of the company for the purposes described above. The tool was believed to last be used in June of 2014. "Since discovering the tool was lost, every effort has been made to locate it by posting lost tool messages throughout the company and searching all tool storage locations and employee tool boxes. To prevent this from happening again, the company has placed tools like this into our inventory tool control program where employees will be required to sign out tools and return them after jobs are complete." The tool was in use at the company's New Castle, DE facility. Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf | Power Reactor | Event Number: 50705 | Facility: MONTICELLO Region: 3 State: MN Unit: [1] [ ] [ ] RX Type: [1] GE-3 NRC Notified By: WILLIAM STANG HQ OPS Officer: JEFF ROTTON | Notification Date: 12/29/2014 Notification Time: 03:40 [ET] Event Date: 12/28/2014 Event Time: 20:23 [CST] Last Update Date: 12/29/2014 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(A) - POT UNABLE TO SAFE SD 50.72(b)(3)(v)(B) - POT RHR INOP 50.72(b)(3)(v)(C) - POT UNCNTRL RAD REL 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): BILLY DICKSON (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 93 | Power Operation | 93 | Power Operation | Event Text TWO INOPERABLE EMERGENCY DIESEL GENERATORS "While the 12 Emergency Diesel Generator (EDG) was inoperable for performance of the monthly surveillance, adjustments were inadvertently made to 11 EDG which made it inoperable. As a result, Technical Specification [TS] 3.8.1 Condition E, for both EDG's inoperable was entered. Monticello has subsequently restored 12 EDG to an operable status within the 2 hour TS LCO [Limiting Condition for Operation] completion timer requirement. The station remained in a safe condition during this discovery with 12 EDG available at all times. The plant continues to operate in a normal condition with no initiating events present. The health and safety of the public was not impacted as a result of this condition. "The NRC Resident Inspector has been notified." EDG 12 was restored to operable status at 2214 CST and EDG 11 will remain inoperable until a surveillance test is performed to start the EDG and restore the local governor control idle speed to the correct setting. The licensee will be notifying the Minnesota State Duty Officer. | Power Reactor | Event Number: 50707 | Facility: LASALLE Region: 3 State: IL Unit: [ ] [2] [ ] RX Type: [1] GE-5,[2] GE-5 NRC Notified By: MARK SMITH HQ OPS Officer: JEFF ROTTON | Notification Date: 12/30/2014 Notification Time: 03:51 [ET] Event Date: 12/29/2014 Event Time: 23:30 [CST] Last Update Date: 12/30/2014 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): JAMNES CAMERON (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text HIGH PRESSURE CORE SPRAY DECLARED INOPERABLE DUE TO LEAK ON DIVISION 3 DIESEL GENERATOR COOLING WATER PUMP "This report is being made pursuant to 10CFR50.72(b)(3)(v)(D), Event or Condition that could have prevented fulfillment of a Safety Function needed to Mitigate the Consequences of an Accident. During routine surveillance testing of the Unit 2 Division 3 Emergency Diesel Generator (LOS-DG-M3) a small pinhole leak was identified in the pump casing of the Division 3 Diesel Generator Cooling Water Pump. This condition has been evaluated and the Division 3 Diesel Generator Cooling Water Pump has been declared inoperable. The Division 3 Diesel Generator Cooling Water Pump is a support system for the Division 3 Emergency Diesel Generator and the High Pressure Core Spray System (HPCS). The required actions of Technical Specification (TS) 3.5.1 were entered on 12/29/14 at 2330 [CST] when the HPCS system was determined to be inoperable. This condition could have prevented the High Pressure Core Spray System (HPCS), a single train safety system, from performing its design function." The licensee notified the NRC Resident Inspector. | |