U.S. Nuclear Regulatory Commission Operations Center Event Reports For 01/06/2014 - 01/07/2014 ** EVENT NUMBERS ** | Agreement State | Event Number: 49680 | Rep Org: ARKANSAS DEPARTMENT OF HEALTH Licensee: DEL-TIN FIBER, LLC Region: 4 City: EL DORADO State: AR County: License #: ARK-0874-0312 Agreement: Y Docket: NRC Notified By: TAMMY KRIESEL HQ OPS Officer: DONG HWA PARK | Notification Date: 12/30/2013 Notification Time: 12:04 [ET] Event Date: 12/27/2013 Event Time: [CST] Last Update Date: 12/30/2013 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): GEOFFREY MILLER (R4DO) FSME EVENTS RESOURCE (EMAI) | Event Text AGREEMENT STATE REPORT - GAUGE SHUTTER FAILURE The following information was received via email from Arkansas Department of Health: "The licensee notified the [Arkansas] Department [of Health] on December 27, 2013 via email that a Ronan source holder model SA1-F37 shutter failed. The source holder serial number is M4785, and the source contains 100 mCi of Cesium-137. The problem was discovered during shutter checks. [According to the licensee], it appears the shutter handle is spinning on the shaft that rotates [to] open [and] close the shutter. [This] may be a result of a sheared pin that connects the handle to the shaft. Per the RSO, the gauge is still in use, and there have been no exposures to employees or members of the public. The RSO has notified applicable facility personnel. "The licensee indicated the manufacturer was contacted on December 27, 2013 and repairs should be performed the week of January 6th-13th. "The State of Arkansas is awaiting a written report after repairs. The State's event number is ARK-2013-013." | Power Reactor | Event Number: 49692 | Facility: WOLF CREEK Region: 4 State: KS Unit: [1] [ ] [ ] RX Type: [1] W-4-LP NRC Notified By: JIM KURAS HQ OPS Officer: CHARLES TEAL | Notification Date: 01/06/2014 Notification Time: 06:56 [ET] Event Date: 01/06/2014 Event Time: 03:30 [CST] Last Update Date: 01/06/2014 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): GEOFFREY MILLER (R4DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text LOSS OF THREE EMERGENCY PLAN SIRENS "While operating in Mode 1 at 100% rated thermal power, the City of Burlington Kansas emergency dispatch center notified Wolf Creek Nuclear Operating Corporation (WCNOC) Security that two emergency plan sirens in Burlington, Kansas and one emergency plan siren in New Strawn, Kansas failed to function when they were actuated to call out a local fire response . These three sirens also function as part of the Emergency Plan Alert and Notification System. WCNOC Emergency Plan personnel have been notified of the three siren failures and the cause is under investigation. "Wolf Creek Generating Station (WCGS) remains at 100% rated thermal power. "The WCGS NRC Resident [Inspector] has been notified and local government." * * * UPDATE AT 1408 EST ON 01/06/14 FROM PIERCE MOORE III TO JEFF ROTTON * * * "At 0922 CST, the three sirens were returned service. "WCGS NRC Resident has been notified. " Notified R4DO (Hagar). | Power Reactor | Event Number: 49693 | Facility: MILLSTONE Region: 1 State: CT Unit: [ ] [ ] [3] RX Type: [1] GE-3,[2] CE,[3] W-4-LP NRC Notified By: TODD FISHER HQ OPS Officer: CHARLES TEAL | Notification Date: 01/06/2014 Notification Time: 10:09 [ET] Event Date: 01/06/2014 Event Time: 08:51 [EST] Last Update Date: 01/06/2014 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): WAYNE SCHMIDT (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 3 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text RADIATION MONITOR TAKEN OUT OF SERVICE FOR PLANNED MAINTENANCE "The Supplementary Leakage Collection and Release System ventilation process flow radiation monitor 3HVR*RE19A has been removed from service for pre-planned maintenance. The monitor will be returned to service after maintenance is complete." The NRC Resident Inspector, state, and local agencies have been informed. | Power Reactor | Event Number: 49694 | Facility: COOPER Region: 4 State: NE Unit: [1] [ ] [ ] RX Type: [1] GE-4 NRC Notified By: BRIAN HASSELBRING HQ OPS Officer: CHARLES TEAL | Notification Date: 01/06/2014 Notification Time: 10:31 [ET] Event Date: 01/06/2014 Event Time: 02:45 [CST] Last Update Date: 01/06/2014 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(C) - POT UNCNTRL RAD REL 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): BOB HAGAR (R4DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text SECONDARY CONTAINMENT DIFFERENTIAL PRESSURE EXCEEDED TECHNICAL SPECIFICATION "At 0245 CST secondary containment differential pressure exceeded the Technical Specifications limit due to a personnel error manipulating an incorrect component. This caused entry into LCO 3.6.4.1 for secondary containment inoperability. An event or condition that could have prevented fulfillment of a safety function requires an 8 hour report per 10CFR50.72(b)(3)(v)(C) for Control of Rad Release and 10CFR50.72(b)(3)(v)(D) for Accident Mitigation. The error was corrected and secondary containment pressure was restored to greater than or equal to 0.25 inch vacuum water gauge and secondary containment was declared operable at 0302 CST. The NRC Resident has been informed of this condition." | Power Reactor | Event Number: 49697 | Facility: BEAVER VALLEY Region: 1 State: PA Unit: [1] [ ] [ ] RX Type: [1] W-3-LP,[2] W-3-LP NRC Notified By: DAVE GIBSON HQ OPS Officer: JEFF ROTTON | Notification Date: 01/06/2014 Notification Time: 19:09 [ET] Event Date: 01/06/2014 Event Time: 16:59 [EST] Last Update Date: 01/06/2014 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): WAYNE SCHMIDT (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | A/R | Y | 100 | Power Operation | 0 | Hot Standby | Event Text AUTOMATIC REACTOR TRIP DUE TO MAIN TRANSFORMER FAULT "At 1659 EST hours on January 6, 2014, Beaver Valley Power Station Unit 1 automatically tripped from 100% power. The cause of the reactor trip was a main transformer differential trip. All rods fully inserted into the core and the plant is stable in Mode 3. All three auxiliary feedwater pumps automatically started as expected. Normal and Emergency Busses are being powered by Offsite Power. The cause of the main transformer differential trip is being investigated. All other equipment functioned as expected. At 1757 EST hours the Emergency Operating Procedures were exited. "Resident inspector has been notified." Decay heat is being removed via the turbine bypass valves to the condenser. No primary or secondary safety valves lifted. Unit 2 was unaffected. Licensee notified the States of Pennsylvania, Ohio, and West Virginia and the Counties of Beaver, PA, Hancock, OH, and Columbiana, OH. | Power Reactor | Event Number: 49698 | Facility: INDIAN POINT Region: 1 State: NY Unit: [ ] [3] [ ] RX Type: [2] W-4-LP,[3] W-4-LP NRC Notified By: GEORGE KELLER HQ OPS Officer: STEVE SANDIN | Notification Date: 01/06/2014 Notification Time: 21:55 [ET] Event Date: 01/06/2014 Event Time: 21:15 [EST] Last Update Date: 01/06/2014 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): WAYNE SCHMIDT (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 3 | A/R | Y | 100 | Power Operation | 0 | Hot Standby | Event Text AUTOMATIC REACTOR TRIP ON LOW STEAM GENERATOR WATER LEVEL DUE TO A FAILED MAIN FEEDWATER REG VALVE "On January 6th, 2014 at 2115 EST Indian Point Unit 3 experienced an Automatic Reactor Trip due to '33 Steam Generator Steam flow/Feed flow Mismatch.' Operators entered emergency procedure E-0, Reactor Trip or Safety Injection. All control rods fully inserted, all safety systems responded as expected, and off-site power remained in-service. No primary or secondary safety valves actuated due to the trip. This is reportable under 10CFR50.72(b)(2)(iv)(B). The main condenser is being used for heat sink. Unit 2 remains stable at 100% power. The Auxiliary Feedwater System actuated following the automatic trip as expected. This is reportable under 10CFR50.72(b)(3)(iv)(A). "Investigation is underway to determine the cause of the 33 Steam Generator Mismatch condition." The licensee will inform local and other government agencies and issue a press release. The licensee has informed the State of New York and the NRC Resident Inspector. | |