U.S. Nuclear Regulatory Commission Operations Center Event Reports For 02/11/2013 - 02/12/2013 ** EVENT NUMBERS ** | Power Reactor | Event Number: 48740 | Facility: CLINTON Region: 3 State: IL Unit: [1] [ ] [ ] RX Type: [1] GE-6 NRC Notified By: JAMES LUCAS HQ OPS Officer: DONALD NORWOOD | Notification Date: 02/11/2013 Notification Time: 12:59 [ET] Event Date: 02/11/2013 Event Time: 07:56 [CST] Last Update Date: 02/11/2013 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.719 - FITNESS FOR DUTY | Person (Organization): PATTY PELKE (R3DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 97 | Power Operation | 97 | Power Operation | Event Text FITNESS FOR DUTY - CONFIRMED POSITIVE FFD TEST A non-licensed, supervisory employee had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been restricted. The licensee notified the NRC Resident Inspector. | Part 21 | Event Number: 48741 | Rep Org: TOPWORX Licensee: TOPWORX Region: 1 City: LOUISVILLE State: KY County: License #: Agreement: Y Docket: NRC Notified By: BRIAN HAMPTON HQ OPS Officer: DONALD NORWOOD | Notification Date: 02/11/2013 Notification Time: 15:26 [ET] Event Date: 10/12/2012 Event Time: [CST] Last Update Date: 02/11/2013 | Emergency Class: NON EMERGENCY 10 CFR Section: 21.21(d)(3)(i) - DEFECTS AND NONCOMPLIANCE | Person (Organization): ANTHONY DIMITRIADIS (R1DO) GEORGE HOPPER (R2DO) PATTY PELKE (R3DO) BOB HAGAR (R4DO) PART 21 RX GROUP (E-MA) | Event Text PART 21 REPORT - SWITCHES BUILT WITH ADHESIVE BEYOND ITS EXPIRATION DATE TopWorx discovered that switches were built and shipped using adhesive G909 that was beyond its manufacturer's recommended expiration date. Adhesion properties of the expired adhesive cannot be guaranteed against the deleterious effects of seismic events, thermal aging, and high dose radiation. The switches involved were TopWorx M8-24521-P4 shipped on 12 October 2012 and TopWorx M8-2352T-P4 shipped on 8 November 2012. Both shipments were sent to PGS Enrique Maria Hierro S.L. in Spain. If the units mentioned above are found to be installed in an environment that may expose them to the conditions of seismic events, thermal aging, and/or high dose radiation, then the units should be replaced. Per TopWorx, there were 13 switches shipped. All switches were shipped to Spain. No switches were shipped to US licensees. Technical questions or concerns should be addressed to Alex Murphy, Manager, Quality, (502) 873-4602. | Power Reactor | Event Number: 48743 | Facility: PILGRIM Region: 1 State: MA Unit: [1] [ ] [ ] RX Type: [1] GE-3 NRC Notified By: RICHARD PROBASCO HQ OPS Officer: BILL HUFFMAN | Notification Date: 02/11/2013 Notification Time: 20:34 [ET] Event Date: 02/11/2013 Event Time: 14:35 [EST] Last Update Date: 02/11/2013 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(xiii) - LOSS COMM/ASMT/RESPONSE | Person (Organization): ANTHONY DIMITRIADIS (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | N | 0 | Cold Shutdown | 0 | Cold Shutdown | Event Text LOSS OF EMERGENCY RESPONSE CAPABILITY - JOINT INFORMATION CENTER (JIC) UNAVAILABLE "On Monday, February 11, 2013 at 1435 EST with Pilgrim Nuclear Power Station (PNPS) at 0% core thermal power, the Joint Information Center (JIC) was determined to be unavailable and was declared non-operational. [Power was lost] to the facility [due] to winter storm Nemo. This facility serves as the Joint Information Center for Entergy, State, and Federal organizations during an emergency response. "Existing emergency procedures direct the responsible Emergency Plant Manager to relocate the JIC staff to the designated alternate location (Bridgewater State University) as required. It has been confirmed that the alternate location is available for use. "The Emergency Response Organization has been informed to establish the JIC at the Moakley Center at Bridgewater State University in the event of a declared emergency classification requiring activation of this Emergency Response Facility. "The licensee has notified the NRC Senior Resident Inspector and the Commonwealth of Massachusetts. "This eight-hour notification is being made in accordance with 10 CFR 50.72(b)(3)(xiii) due to the loss of an emergency offsite response facility. "An update will be provided when power has been restored to the JIC and the facility is available to be activated if called upon." | Power Reactor | Event Number: 48744 | Facility: TURKEY POINT Region: 2 State: FL Unit: [3] [ ] [ ] RX Type: [3] W-3-LP,[4] W-3-LP NRC Notified By: TIM JONES HQ OPS Officer: JOHN SHOEMAKER | Notification Date: 02/12/2013 Notification Time: 00:45 [ET] Event Date: 02/11/2013 Event Time: 22:36 [EST] Last Update Date: 02/12/2013 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL 50.72(b)(3)(iv)(A) - VALID SPECIF SYS ACTUATION | Person (Organization): GEORGE HOPPER (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 3 | A/R | Y | 100 | Power Operation | 0 | Hot Standby | Event Text AUTOMATIC REACTOR TRIP DUE TO TURBINE TRIP ON LOSS OF CONDENSER VACUUM "This is a non-emergency event notification to the NRCOC [Nuclear Regulatory Commission Operations Center] in accordance with 10 CFR 50.72(b)(2)(iv)(B) for a valid actuation of the Reactor Protection System (RPS) (four hour notification) and 10 CFR 50.72(b)(3)(iv)(A) for a valid Engineered Safeguards (ESF) actuation due to Auxiliary Feedwater (AFW) initiation (eight hour notification). "On 2/11/2013 at 2236 EST Unit 3 experienced a loss of condenser vacuum. An automatic Turbine Trip signal was generated which initiated a Reactor Trip signal. The reactor tripped as required on the automatic trip signal. Auxiliary feedwater water actuated automatically based on low steam generator levels following the trip. Unit 3 is currently in Mode 3 and stable. Steam generator levels have been returned to normal levels . The loss of vacuum is under investigation at this time. All other plant systems are working as designed." The reactor trip was uncomplicated. All control rods fully inserted. The plant is stable at normal temperature and pressure. AFW has been secured and main feedwater is being used for Steam Generator water level control. The main condenser is unavailable and decay heat removal is to atmosphere via the atmospheric steam dumps. There are no indications of primary to secondary leakage. Unit 3 is in a normal offsite power electrical alignment. There is no impact on Unit 4. The licensee has notified the NRC Resident Inspector. | |