U.S. Nuclear Regulatory Commission Operations Center Event Reports For 10/25/2010 - 10/26/2010 ** EVENT NUMBERS ** | General Information or Other | Event Number: 46351 | Rep Org: TEXAS DEPARTMENT OF HEALTH Licensee: INTERNATIONAL PAPER COMPANY Region: 4 City: QUEEN CITY State: TX County: License #: 01686 Agreement: Y Docket: NRC Notified By: ANNIE BACKHAUS HQ OPS Officer: JOE O'HARA | Notification Date: 10/21/2010 Notification Time: 17:58 [ET] Event Date: 10/21/2010 Event Time: [CDT] Last Update Date: 10/21/2010 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): VIVIAN CAMPBELL (R4DO) KEITH McCONNELL (FSME) | Event Text AGREEMENT STATE REPORT - PROCESS GAUGE SHUTTER INOPERABLE The following was received from the State of Texas via e-mail: "On October 21, 2010, the Agency [State of Texas] received a 'Notice of reciprocity' from Berthold Technologies. The notice stated that a Berthold Technologies service representative would be replacing the shutters on two gauges at the licensee's (International Paper Company) facility on October 22, 2010. The Agency contacted the licensee and asked to speak with the Radiation Safety Officer (RSO). The Agency was forwarded to the RSO's voicemail box and left a message. The Agency then contacted one of the licensee's employees whose information was obtained from the 'Notice of Reciprocity.' The employee then reported that the licensee had experienced a shutter failure. "The licensee stated that on Monday, October 18, 2010, another licensee properly authorized by the Agency [State of Texas] to remove the gauges came to the licensee's facility to remove the gauge from the pipe it was fixed to. The gauge was manufactured by Berthold Technologies (Model: LB7440; Serial Number: 1335) and it houses a 30 milliCurie Cesium (Cs) 137 source (Serial Number: 1335- 5-89). The gauge was removed so that the licensee could perform maintenance on the pipe. The licensee stated that the shutter was hard to turn at that time, but the shutter properly closed prior to the authorized person removing the gauge. On Wednesday, October 20, 2010, the authorized person returned to reattach the gauge and attempted to open the shutter, and the shutter would not open. The licensee then stated that they contacted Berthold Technologies to repair the shutter that failed, as well as another shutter on different gauge that was difficult to operate. The shutters are scheduled to be repaired on Friday, October 22, 2010. The RSO was later contacted and he agreed to submit a written report to the Agency within thirty days." TX Incident No. I-8794 | Power Reactor | Event Number: 46360 | Facility: BEAVER VALLEY Region: 1 State: PA Unit: [1] [ ] [ ] RX Type: [1] W-3-LP,[2] W-3-LP NRC Notified By: KEN TIEFENTHAL HQ OPS Officer: VINCE KLCO | Notification Date: 10/25/2010 Notification Time: 12:04 [ET] Event Date: 10/25/2010 Event Time: 07:00 [EDT] Last Update Date: 10/25/2010 | Emergency Class: NON EMERGENCY 10 CFR Section: 26.719 - FITNESS FOR DUTY | Person (Organization): JOHN CARUSO (R1DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | N | 0 | Refueling | 0 | Refueling | Event Text CONTRACT NON-LICENSED SUPERVISOR TESTED POSITIVE FOR A CONTROLLED SUBSTANCE A non-licensed contract employee supervisor had a confirmed positive for a controlled substance during a random fitness for duty test. The employee's unescorted access to the plant has been terminated. Contact the Headquarters Operations Officer for additional details. The licensee has notified the NRC Resident Inspector. | Power Reactor | Event Number: 46362 | Facility: TURKEY POINT Region: 2 State: FL Unit: [3] [ ] [ ] RX Type: [3] W-3-LP,[4] W-3-LP NRC Notified By: KEITH MAESTAS HQ OPS Officer: VINCE KLCO | Notification Date: 10/25/2010 Notification Time: 22:30 [ET] Event Date: 10/25/2010 Event Time: 22:00 [EDT] Last Update Date: 10/25/2010 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(ii)(A) - DEGRADED CONDITION | Person (Organization): RANDY MUSSER (R2DO) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 3 | N | N | 0 | Cold Shutdown | 0 | Cold Shutdown | Event Text CONTAINMENT LINER CORROSION DEGRADATION "This report is made in accordance with 10 CFR 50.72(b)(3)(ii) as a condition resulting in a serious degradation of the Containment liner. During a visual inspection on 10/22/10, corrosion was found in the containment sump liner on Unit 3, A more detailed inspection was performed on 10/24/10 after the corroded area was cleaned. Evaluation of the inspection results has determined that the corrosion is greater than allowed by the ASME Code, including through wall areas, and requires repair. At this time, it is not known whether any leakage caused by the through-wall condition would have resulted in exceeding the containment allowed leakage limit. Unit 3 is currently in Mode 5 preparing to return to service following refueling. The corroded areas will be repaired prior to entering Mode 4." The licensee notified the NRC Resident Inspector | |