Event Notification Report for September 11, 2006
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 09/08/2006 - 09/11/2006 ** EVENT NUMBERS ** | Power Reactor | Event Number: 42835 | Facility: DUANE ARNOLD Region: 3 State: IA Unit: [1] [ ] [ ] RX Type: [1] GE-4 NRC Notified By: ELLIS VANN HQ OPS Officer: MARK ABRAMOVITZ | Notification Date: 09/08/2006 Notification Time: 10:30 [ET] Event Date: 09/08/2006 Event Time: 04:01 [CDT] Last Update Date: 09/08/2006 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): BRUCE BURGESS (R3) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | Y | 96 | Power Operation | 96 | Power Operation | Event Text CONTAINMENT ATMOSPHERIC DILUTION (CAD) SYSTEM INOPERABLE "On September 8, 2006 at 04:01, DAEC declared CAD inoperable after determining SV-4332B, UPPER DRYWELL SPRAY CAD N2 OUTBOARD ISOLATION was inoperable while SV-4331B, LOWER DRYWELL SPRAY CAD N2 OUTBOARD ISOLATION was also inoperable. Actions to isolate both of these injection pathways as required by Technical Specifications made CAD injection into the Drywell unavailable. Day 1 of a 7 day LCO for Technical Specification 3.6.3.1 Condition A was entered. Per DAEC Technical Specifications bases, CAD is considered to be inoperable when both injection pathways into either the drywell or torus are not available. Since CAD is a single train safety system, this event is reportable as an 8 hour non-emergency event under 50.72(b)(3)(v)(D), any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident." The licensee notified the NRC Resident Inspector. | |
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021