U.S. Nuclear Regulatory Commission Operations Center Event Reports For 11/26/2003 - 11/28/2003 ** EVENT NUMBERS ** | General Information or Other | Event Number: 40352 | Rep Org: ILLINOIS EMERGENCY MGMT. AGENCY Licensee: Region: 3 City: State: IL County: License #: Agreement: Y Docket: NRC Notified By: JOE KLINGER HQ OPS Officer: GERRY WAIG | Notification Date: 11/25/2003 Notification Time: 11:32 [ET] Event Date: 11/24/2003 Event Time: 14:15 [CST] Last Update Date: 11/25/2003 | Emergency Class: NON EMERGENCY 10 CFR Section: AGREEMENT STATE | Person (Organization): SONIA BURGESS (R3) JOHN GREEVES (NMSS) | Event Text AGREEMENT STATE REPORT - DOSE TO PATIENT OUTSIDE INTENDED TREATMENT SITE "[Radiation Safety Officer (RSO)] for Advocate Lutheran General Hospital called Illinois Emergency Management Agency on 11/24/03 at approximately 1415 to report an event involving a Novoste Intravascular Brachytherapy [IVB] procedure. Hospital RSO stated that at approximately 1100 on 11/24/2003 during an IVB procedure with a prescribed dose of 18.4 gray, the end of the 40mm source train was not visible at the anticipated location at the end of the catheter. The sources were stuck in an apparent kink in the catheter. The source train was immediately retracted into the safe shielded position in the unit. A second attempt was then made but the sources became stuck in the same area and were again immediately retracted. " The procedure was then terminated and an analysis of the event and dose estimates were performed. An unintended area of the heart was exposed to radiation from the source train for approximately 47 seconds in the first attempt and 10 seconds in the second. The estimated radiation dose calculated to the wrong area of the heart was estimated to be approximately 5 gray. Essentially none of the prescribed dose of 18.4 gray was delivered to the intended area of the heart as the source train was retracted before reaching the intended area. "The patient has been notified that there was a problem encountered during the procedure and the physician will notify the patient shortly of the particulars involved with the unintended dose delivered. The physicians do not expect any adverse medical effects from this event. Hospital RSO stated that they will carefully review this event and enhance training for this procedure. Hospital RSO added that he will notify Novoste regarding this event and submit the required written report within 15 days." Illinois Event Report ID: IL030078, License Number: IL -01152-01 Source Information: NOVOSTE Model #A1767, Serial # 91834, Radionuclide: Sr 90, Activity: .0484 Curies | Power Reactor | Event Number: 40357 | Facility: LASALLE Region: 3 State: IL Unit: [1] [ ] [ ] RX Type: [1] GE-5,[2] GE-5 NRC Notified By: TODD GRANLUND HQ OPS Officer: CHAUNCEY GOULD | Notification Date: 11/27/2003 Notification Time: 03:24 [ET] Event Date: 11/27/2003 Event Time: 00:52 [CST] Last Update Date: 11/27/2003 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL | Person (Organization): SONIA BURGESS (R3) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | M/R | Y | 23 | Power Operation | 0 | Hot Shutdown | Event Text REACTOR MANUALLY SCRAMMED FROM 23% DUE TO DECREASING REACTOR VESSEL WATER LEVEL A manual reactor scram was initiated due to a decreasing reactor vessel water level. The decreasing water level occurred during a feedwater transient while performing a power reduction in preparation for taking the main generator off line for maintenance. The licensee is investigating the cause of the feedwater transient, but it occurred while one turbine driven reactor feed pump was being taken off line. All rods fully inserted following the scram and no ECCS or safety relief valves actuated. Residual heat is being rejected to the condenser. The licensee notified NRC Resident Inspector. | Power Reactor | Event Number: 40358 | Facility: MILLSTONE Region: 1 State: CT Unit: [ ] [2] [ ] RX Type: [1] GE-3,[2] CE,[3] W-4-LP NRC Notified By: BRUCE FERGUSON HQ OPS Officer: CHAUNCEY GOULD | Notification Date: 11/27/2003 Notification Time: 06:51 [ET] Event Date: 11/27/2003 Event Time: 06:29 [EST] Last Update Date: 11/27/2003 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(2)(iv)(B) - RPS ACTUATION - CRITICAL | Person (Organization): ANTHONY DIMITRIADIS (R1) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 2 | M/R | Y | 20 | Power Operation | 0 | Hot Standby | Event Text PLANT HAD A MANUAL REACTOR TRIP FROM 23% POWER DUE TO TURBINE VIBRATION While rolling the turbine when at 20% power they experienced an over speed turbine trip. During a second attempt when at 23% power, the turbine had high vibration so they manually tripped the reactor. Cause for the vibration is being investigated since a new rotor had just been installed in the turbine. All rods fully inserted during the reactor trip and no ECCS injection occurred or primary relief valves lifted. The licensee notified the NRC Resident, the State of Connecticut and Local agencies | Power Reactor | Event Number: 40359 | Facility: CATAWBA Region: 2 State: SC Unit: [1] [2] [ ] RX Type: [1] W-4-LP,[2] W-4-LP NRC Notified By: JAMIE MCCONNELL HQ OPS Officer: CHAUNCEY GOULD | Notification Date: 11/28/2003 Notification Time: 01:55 [ET] Event Date: 11/27/2003 Event Time: 22:55 [EST] Last Update Date: 11/28/2003 | Emergency Class: NON EMERGENCY 10 CFR Section: 50.72(b)(3)(ii)(B) - UNANALYZED CONDITION 50.72(b)(3)(v)(B) - POT RHR INOP 50.72(b)(3)(v)(D) - ACCIDENT MITIGATION | Person (Organization): STEPHEN CAHILL (R2) | Unit | SCRAM Code | RX CRIT | Initial PWR | Initial RX Mode | Current PWR | Current RX Mode | 1 | N | N | 0 | Refueling Shutdown | 0 | Refueling Shutdown | 2 | N | Y | 100 | Power Operation | 100 | Power Operation | Event Text COMPONENT COOLING SYSTEM SURGE TANK SUPPORTS MAY FAIL DURING A SEISMIC EVENT During an ISI inspection of the component cooling system, it was discovered that several of the surge tank support stiffener plates were missing due to a design change that was never fully implemented. This condition creates a question as to the adequacy of the tanks to withstand a seismic event. This deficiency affects both trains of component cooling on Units 1 and 2. The problem will be corrected on Unit 1 while it is in its refueling outage. Work on the Unit 2 "A" train is currently ongoing, making that train of the component cooling system inoperable, therefore, putting the plant in a 72 hour LCO. When work on the "A" train is completed, they will exit the LCO, but re-enter it when work begins on the "B" train. Licensee will notify the NRC Resident Inspector, the State and local agencies | |