Event Notification Report for August 15, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 08/14/2003 - 08/15/2003 ** EVENT NUMBERS ** 39941 40055 40056 40060 40061 40063 40064 40065 40066 40067 40068 40069 40070 40071 40072 40073 40074 40075 +------------------------------------------------------------------------------+ |Hospital |Event Number: 39941 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: GUTHRIE HEALTH CARE |NOTIFICATION DATE: 06/16/2003| |LICENSEE: GUTHRIE HEALTH CARE |NOTIFICATION TIME: 09:20[EDT]| | CITY: SAYRE REGION: 1 |EVENT DATE: 06/12/2003| | COUNTY: STATE: PA |EVENT TIME: [EDT]| |LICENSE#: 37-01893-01 AGREEMENT: N |LAST UPDATE DATE: 08/14/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |RAYMOND LORSON R1 | | |DOUG BROADDUS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JOON PARK | | | HQ OPS OFFICER: FANGIE JONES | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |LDIF 35.3045(a)(1) DOSE <> PRESCRIBED DOSA| | |LOTH 35.3045(a)(3) DOSE TO OTHER SITE > SP| | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DISCOVERY THAT PART OF THE IMPLANTED SEEDS WERE NOT IN THE PROPER SITE | | | | A patient was referred for treatment, due to reoccurring prostate cancer, to | | the hospital where he had previously had treatment. Seeds were implanted | | around May 2001. A scan of the previous treatment of implanted seeds | | determined that many of the seeds were not located in the prostate, but in | | adjacent tissue where they would have been ineffective in treatment. Also, | | a review of the records indicated a scan was performed in early 2002, but | | was not followed up on. The patient and referring physician have been | | informed. The hospital is conducting an investigation into the event and | | also developing a plan to provide appropriate treatment for the patient. | | | | * * * UPDATE ON 07/18/03 AT 1638 FROM JOON PARK TO ARLON COSTA * * * | | | | Post-op dosimetry on one patient was determined to be a misadministration. | | The dose that covered the prostate was more than 20 percent different from | | the prescription as well as the penile bulb dose being close to 50 percent | | of the prescription dose. Efforts are being made to contact the affected | | patient. The licensee will continue efforts to obtain post-op dosimetry on | | the rest of the patients related to this incident so that evaluations for | | misadministration can be performed. | | | | Notified R1DO (Della Greca) and NMSS EO (Pierson). | | | | * * * UPDATE ON 07/25/03 AT 0921 EDT FROM JOON PARK TO JOHN MACKINNON * * * | | | | Post-op dosimetry for two patients were determined to be a | | misadministration. The patients had their prostates treated some time in | | the year 2001. The iodine-125 seeds were placed 2 to 3 centimeters below | | the area where they were supposed to be located. The improper location of | | the iodine-125 seeds caused more than 50% of the prescribed dose to be | | delivered to an un-intended organ. The patients will be notified. | | | | Notified R1DO (Dan Holody) and NMSS EO (Trish Holahan). | | | | * * * UPDATE ON 07/30/03 AT 0911 EDT FROM JOON PARK TO ARLON COSTA * * * | | | | Two additional patients of a group of seven were identified as having | | received a misadministration of iodine-125 to an unintended organ. The | | patients will be notified of this misadministration. The licensee is in the | | process of clarifying and document the issues related to this incident. | | | | Notified R1DO (James Moorman) and NMSS EO (Tom Essig). | | | | * * * UPDATE ON 08/07/03 AT 1535 EDT FROM CHARLES LEE TO NATHAN SANFILIPPO * | | * * | | | | Another patient has been identified who received a misadministration of | | iodine-125 to the prostate. The prescribed dose was 144 Gy, and it was | | delivered using 76 seeds and 27 needles as planned prior to the implant | | date. After reviewing the CT, which was done on Feb. 27, 2001, the V100 of | | the prostate received 29% of the prescribed dose. The penile bulb at 72 Gy | | received 44.8%. The licensee indicated that they have looked into 8 | | patients who may have been misadministered, of which, one was not declared a | | misadministration. The other seven appear in this notification. There are | | 23 total patients that the licensee intends to review. | | | | Notified R1DO (Clifford Anderson) and NMSS EO (Fred Brown). | | | | * * * FINAL UPDATE ON 08/14/03 AT 1150 EDT BY CHARLES LEE TO JOHN MACKINNON | | * * * | | | | Twelve more patients have been added to the number of patients. Patients are | | identified by a six digit number. | | | | Patient# [deleted]- On this date, March 21, 2001, the former physician, | | prescribed a dose of 144Gy to the prostate using 1-125 seeds. The prescribed | | dose was delivered using 77 seeds and 26 needles as planned prior to the | | implant, The V 100 of the prostate received 39% of the prescribed dose and | | the V50 of the penile bulb received 88%. | | Patient# [deleted]- On this date, May 23, 2001, the former physician, | | prescribed a dose of 144Gy to the prostate using 1-125 seeds. The prescribed | | close was delivered using 53 seeds and 18 needles as planned prior to the | | implant. The V100 of the prostate received 62% of the prescribed dose and | | the V50 of the penile bulb received 57%, | | Patient# [deleted]- On this date, December. 13, 2001, the former physician, | | prescribed a dose of 144Gy to the prostate using 1-125 seeds. The prescribed | | dose was delivered using 86 seeds and 21 needles as planned prior to the | | implant. The V 100 of the prostate received 70% of the prescribed dose and | | the V50 of the penile bulb received 99%. | | Patient# [deleted]- On this date, February 22, 2001, the former physician, | | prescribed a dose of 144Gy to the prostate using 1-125 seeds. The prescribed | | dose was delivered using 77 seeds and 25 needles as planned prior to the | | implant. The V100 of the prostate received 52.5% of the prescribed dose and | | the V50 of the penile bulb received 80%. | | Patient# [deleted]- On this date, March 15, 2001, the former physician, | | prescribed a dose of 144Gy to the prostate using 1-125 seeds. The prescribed | | dose was delivered using 67 seeds and 27 needles as planned prior to the | | implant. The V 100 of the prostate received 59% of the prescribed dose and | | the V50 of the penile bulb received 86.5%. | | Patient# [deleted]- On this date, July 5, 2001, the former physician, | | prescribed a dose of 144Gy to the prostate using 1-125 seeds. The prescribed | | dose was delivered using 62 seeds and 21 needles as planned prior to the | | implant. The VI 00 of the prostate received 49% of the prescribed dose. | | Patient# [deleted]- On this date, February 8, 2001, the former physician, | | prescribed a dose of 144-Gy to the prostate using 1-125 seeds. The | | prescribed dose was delivered using 45 seeds and 18 needles as planned prior | | to the implant. The V 100 of the prostate received 68% of the prescribed | | dose. | | Patient# [deleted]- On this date, September 5, 2001, the former physician, | | prescribed a dose of 144Gy to the prostate using 1-125 seeds. The prescribed | | dose was delivered using 58 seeds and 20 needles as planned prior to the | | implant. The V100 of the prostate received 59.5% of the prescribed dose. | | Patient# [deleted]- On this date, May 31, 2001, the former physician, | | prescribed a dose of 14-4Gy to the prostate using 1-125 seeds. The | | prescribed dose was delivered using 60 seeds and 17 needles as planned prior | | to the implant. The V1 00 of the prostate received 68% of the prescribed. | | Dose. | | Patient# [deleted]- On this date, January 22, 2001, the former physician, | | prescribed a dose of 144Gy to the prostate using I-125 seeds. The prescribed | | dose was delivered using 54 seeds and 3, 8 needles as planned prior to the | | implant. The V100 of the prostate received 73% of the prescribed dose, | | Patient# [deleted]- On this date, January 10, 2001, the former physician, | | prescribed a dose of 144Gy to the prostate using I-125 seeds. The prescribed | | dose was delivered using 58 seeds and 19 needles as planned prior to the | | implant. The VI 00 of the prostate received 54% of the prescribed dose. | | Patient# [deleted]- On this date, June 21, 2001, the former physician, | | prescribed a dose of 144Gy to the prostate using 1-125 seeds, The prescribed | | dose was delivered using 82 seeds 28 needles as planned prior to the | | implant, The V 100 of the prostate received 73% of the prescribed dose. | | | | Notified R1DO (Glenn Meyer) & NMSS EO (Linda Psyk). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 40055 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 08/11/2003| |LICENSEE: ARIAS & KEZAR, INC. |NOTIFICATION TIME: 16:32[EDT]| | CITY: AUSTIN REGION: 4 |EVENT DATE: 08/08/2003| | COUNTY: STATE: TX |EVENT TIME: [CDT]| |LICENSE#: L04964-001 AGREEMENT: Y |LAST UPDATE DATE: 08/11/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |PHIL HARRELL R4 | | |M. WAYNE HODGES NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JIM OGDEN | | | HQ OPS OFFICER: HOWIE CROUCH | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT - TEXAS | | | | "On Friday, August 11, 2003, the Licensee was transporting the gauge in a | | Nissan Pickup truck that had a defective tailgate. The Type 7A package was | | locked to the pickup with a chain but was held in place with a very small | | and cheap padlock. Also in the truck were concrete samples being | | transported for analysis. While transiting FM 471, the tailgate failed to | | the open position when the concrete samples shifted and pushed the gauge | | (Troxler Model 3430, Serial No. 28510, with two sealed sources - Am-241 /Be, | | nominal 40 millicuries, Serial No. 47-25576; and Cs-137, nominal 8 | | millicuries, Serial No. 750-2732) out of the bed and broke the lock allowing | | the gauge to become detached from the truck. The gauge was found by a | | member of the public laying in the middle of Highway FM471 being swerved | | around by traffic. The member of the public stopped and picked up the | | package and placed in his vehicle and transported it to his residence at | | [address deleted], Helotes, Texas. He opened the package which was not | | secured by a locking device. There is no indication that the member of the | | public exposed the sources. He made notification to the Helotes Fire | | Department who in turn notified the Texas Department of Health's Public | | Health Region 8, Radiation Control Office in San Antonio. The Public Health | | Region responded with a Radioactive Materials Inspector who determined that | | the gauge was intact and appeared to have no damage. The Licensee was | | notified and retrieved the gauge." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 40056 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: KENTUCKY DEPT OF RADIATION CONTROL |NOTIFICATION DATE: 08/12/2003| |LICENSEE: UNIVERSITY OF KENTUCKY |NOTIFICATION TIME: 14:10[EDT]| | CITY: LEXINGTON REGION: 2 |EVENT DATE: 06/23/2003| | COUNTY: FAYETTE STATE: KY |EVENT TIME: 15:30[CDT]| |LICENSE#: 203-021-72 AGREEMENT: Y |LAST UPDATE DATE: 08/12/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |DAVID AYRES R2 | | |TOM ESSIG NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ROB GRESHAM | | | HQ OPS OFFICER: ERIC THOMAS | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT | | | | "On June 23, 2003 at 3:30 PM the [University of Kentucky] radiation safety | | office received a call from an AU [Authorized User] in the Dept. of Biology, | | because a shipment of I-125, triiodothyronine, 100 microcuries, had not been | | received. Upon review of the records it was found that the package had | | arrived on June 18, 2003, and had measured 10 [millirem]/hr at the surface, | | 0.1 [millirem]/hr @ 1meter, and no external contamination. The Radiation | | Safety Office shipping paper record shows the I-125 package was included for | | delivery to room 109, Research Building 3, on June 19. The required | | signature of receipt for the package was not obtained. With the DOT | | shipping labels removed, the greatest likelihood is that the package was put | | into the ordinary trash. A thorough search of the Radiation Safety Office | | facilities and vehicles was conducted on June 23. On June 24, the | | authorized user's lab was searched, including use of a low energy NAI (Tl) | | detector, as well as all labs where deliveries were made on June 19. No | | trace of the package or contents has been found. It was concluded that the | | highest probability was that the package entered the normal waste stream and | | went to a landfill. Once in a landfill, the I-125 will be sequestered from | | any contact, and will be essentially non-radioactive in 1.65 years. | | Assuming worst case scenarios, the dose rate to the torso would be about 10 | | [millirem]/hr or less, and would have to be held against the body | | continuously by a single individual for 10 hours to produce a dose in excess | | of 100 [millirem]. Additionally there is no indication or likelihood of | | intentional or accidental ingestion of the contents since this is not | | intended for human use. However, if the entire 100 microcuries were | | ingested by a single individual, as sodium iodide, the thyroid dose would be | | 78 rem, and the effective dose would be 2.4 rem. While no thyroid dose | | information has been found for the triiodothyronine form, the effective | | dose from ingestion of 100 microcuries would be 17 [millirem]. Surveys are | | conducted on a continual basis, if the package did not go to a landfill it | | would likely be found during monthly use area surveys or quarterly | | supervisory surveys. No NOV was issued based on the corrective actions | | taken by licensee to correct deficiencies prior to report completion." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 40060 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: UNIVERSITY OF PENNSYLVANIA |NOTIFICATION DATE: 08/14/2003| |LICENSEE: UNIVERSITY OF PENNSYLVANIA |NOTIFICATION TIME: 09:00[EDT]| | CITY: PHILADELPHIA REGION: 1 |EVENT DATE: 07/01/2003| | COUNTY: STATE: PA |EVENT TIME: [EDT]| |LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 08/14/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GLENN MEYER R1 | | |JOHN HICKEY NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: ROBERT FORREST | | | HQ OPS OFFICER: RICH LAURA | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BLO2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING SOURCE AT UNIVERSITY OF PENNSYLVANIA | | | | "During a routine sealed source inventory in July 2003, a technician from | | the University of Pennsylvania's Office of Environmental Health and | | Radiation Safety (EHRS) found that a Hewlett-Packard 6890 gas chromatograph | | (GC) containing a generally licensed 15 millicuries source of Ni-63 was | | missing from a laboratory undergoing renovations. EHRS contacted faculty and | | staff associated with the laboratory trying to locate the instrument. After | | an extensive search, it was determined that the GC was most likely sent to a | | scrap metal dealer. According to NUREG-1717, Systematic Radiological | | Assessment of Exemptions for Source and Byproduct Materials, the dose to any | | individual from a scrapped Ni-63 gas chromatograph source would be less than | | 0.01 millisievert (1 millirem)" | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40061 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: KEWAUNEE REGION: 3 |NOTIFICATION DATE: 08/14/2003| | UNIT: [1] [] [] STATE: WI |NOTIFICATION TIME: 10:57[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 09:10[CDT]| | NRC NOTIFIED BY: ETHAN TREPTOW |LAST UPDATE DATE: 08/14/2003| | HQ OPS OFFICER: RICH LAURA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |SONIA BURGESS R3 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EP SIRENS OUT OF SERVICE IN KEWAUNEE COUNTY | | | | "At 0910 on August 14, It was reported to the Control Room that all thirteen | | Kewaunee County sirens had a communications problem that rendered them out | | of service. The percent siren coverage population lost is 68.52%. The State | | and County have been notified of the siren failures. The siren vendor has | | been contacted to begin troubleshooting the problem. | | | | "This is being reported under 10 CFR 50.72(b)(3)(xiii) as any event that | | results in a major loss of emergency assessment capability, offsite response | | capability, or offsite communications capability (loss of greater than 50% | | of emergency sirens). It is also being reported under 10 CFR 50.72(b)(2)(xi) | | as any event or situation, related to the health and safety of the public or | | onsite personnel, or protection of the environment, for which a news release | | is planned or notification to other government agencies has been or will be | | made." | | | | The NRC resident inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40063 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 08/14/2003| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 16:33[EDT]| | RXTYPE: [1] GE-6 |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:10[EDT]| | NRC NOTIFIED BY: JOE KOTAR |LAST UPDATE DATE: 08/14/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |SONIA BURGESS R3 | |10 CFR SECTION: |STUART RICHARDS NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |HYMAN FEMA | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO LOSS OF OFFSITE POWER GREATER THAN 15 | | MINUTES. | | | | Automatic reactor scram due to a loss of offsite power. All rods fully | | inserted. Supplying power to vital buses via emergency diesel generators. | | All system operating properly. | | | | NRC Resident Inspector was notified of the event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40064 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALISADES REGION: 3 |NOTIFICATION DATE: 08/14/2003| | UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 17:10[EDT]| | RXTYPE: [1] CE |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:07[EDT]| | NRC NOTIFIED BY: VANDENALLE |LAST UPDATE DATE: 08/14/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |SONIA BURGESS R3 | |10 CFR SECTION: | | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | POWER GRID DISTURBANCE OCCURRED RESULTING IN A MOMENTARY DROP IN VOLTAGE | | | | At 1607 EDT a significant electrical power grid disturbance occurred | | resulting in a momentary drop in voltage at the site, including both 2400 | | VAC safety busses 1C and 1D. The reduced voltage on the 2400VAC safety | | busses caused both emergency diesel generators to auto start, but not load. | | The plant is stable at pre-event conditions. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40065 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: OYSTER CREEK REGION: 1 |NOTIFICATION DATE: 08/14/2003| | UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 18:16[EDT]| | RXTYPE: [1] GE-2 |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:11[EDT]| | NRC NOTIFIED BY: CIGANIK |LAST UPDATE DATE: 08/14/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |GLENN MEYER R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR SCRAM FROM 100% POWER DUE TO OFF SITE ELECTRICAL GRID INSTABILITY | | | | Reactor scram from 100% due to off site electrical grid instability, but did | | not lose off site power. Reactor conditions at 1730 are normal reactor | | water level, reactor pressure 850-1000psig, MSIV's closed and all recirc | | pumps are off and reactor is in hot shutdown with all rods inserted. | | | | The NRC Resident Inspector | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40066 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 08/14/2003| | UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 17:34[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 17:00[EDT]| | NRC NOTIFIED BY: MORAN |LAST UPDATE DATE: 08/14/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |GLENN MEYER R1 | |10 CFR SECTION: |HYMAN FEMA | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |STUART RICHARDS NRR | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | NOUE WAS DECLARED AT 1700 DUE TO LOSS OF OFFSITE POWER | | | | The plant lost off site power due to grid disturbance which resulted in a | | reactor trip from 100% power. The NOUE was declared because of loss of off | | site power was greater than 15 minutes. | | | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40067 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 08/14/2003| | UNIT: [2] [] [] STATE: NY |NOTIFICATION TIME: 16:39[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:25[EDT]| | NRC NOTIFIED BY: MARK COX |LAST UPDATE DATE: 08/15/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |GLENN MEYER R1 | |10 CFR SECTION: |STUART RICHARDS NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |HYMAN FEMA | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO LOSS OF OFFSITE POWER GREATER THAN 15 | | MINUTES. | | | | Automatic reactor scram due to a loss of offsite power. All rods fully | | inserted. Supplying power to vital buses via emergency diesel generators. | | All systems operating properly. | | | | NRC Resident Inspector was notified of the event by the licensee. | | | | * * * UPDATE 2340EDT ON 8/14/03 FROM ANDY MIHALIK TO S.SANDIN * * * | | | | The following information was provided as an update: | | | | "RPS Actuation (loss of flow) due to loss of offsite power. Auto actuation | | of AFW in response to the unit trips. Auto start & load of Emergency Diesel | | Generators in response to the loss of offsite power." | | | | The licensee informed the state/local authorities and the NRC resident | | inspector. Notified R1IRC. | | | | *****UPDATE ON 8/15/03 AT 0226 FROM CELENTANO TO GOTT***** | | | | The licensee exited the Unusual Event at 0210 upon confirmation of a stable | | off-site power. | | | | Notified R1 IRC and FEMA(Heyman). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40068 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 08/14/2003| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 16:46[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:12[EDT]| | NRC NOTIFIED BY: PAUL HARRIS |LAST UPDATE DATE: 08/14/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |GLENN MEYER R1 | |10 CFR SECTION: |STUART RICHARDS NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |HYMAN FEMA | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO LOSS OF OFFSITE POWER GREATER THAN 15 | | MINUTES. | | | | Automatic reactor trip due to a loss of offsite power. All rods fully | | inserted into the core. All emergency systems operated as expected. | | | | NRC Resident Inspector was of this event by the licensee. | | | | * * * UPDATE 0510EDT ON 8/15/03 FROM McCOY TO S.SANDIN * * * | | | | Unit exited the UE at 2108EDT on 8/14/03 after restoration of offsite power. | | The licensee informed state.local agencies and the NRC resident inspector. | | Notified R1IRC and FEMA(Heyman). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40069 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 08/14/2003| | UNIT: [] [3] [] STATE: NY |NOTIFICATION TIME: 16:50[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:23[EDT]| | NRC NOTIFIED BY: MESSINA |LAST UPDATE DATE: 08/15/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |GLENN MEYER R1 | |10 CFR SECTION: |STUART RICHARDS NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |HYMAN FEMA | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | |ASHU 50.72(b)(2)(i) PLANT S/D REQD BY TS | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |3 A/R Y 100 Power Operation |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO LOSS OF OFFSITE POWER GREATER THAN 15 | | MINUTES. | | | | Automatic reactor scram due to a loss of offsite power. All rods fully | | inserted. Supplying power to vital buses via emergency diesel generators. | | All systems operating properly. | | | | NRC Resident Inspector was notified of the event by the licensee. | | | | * * * UPDATE 2340EDT ON 8/14/03 FROM ANDY MIHALIK TO S.SANDIN * * * | | | | The following information was provided as an update: | | | | "RPS Actuation (loss of flow) due to loss of offsite power. Auto actuation | | of AFW in response to the unit trips. Auto start & load of Emergency Diesel | | Generators in response to the loss of offsite power. Unit 3 also | | experienced a second AFW auto start during the event. Unit 3 also entered | | Tech Spec LCO 3.0.3 for loss of two offsite circuits and one EDG inoperable. | | #31 EDG was declared inoperable when its associated Fuel oil storage tank | | inventory decreased below required." | | | | The licensee informed the state/local authorities and the NRC resident | | inspector. Notified R1IRC. | | | | *****UPDATE ON 8/15/03 AT 0226 FROM CELENTANO TO GOTT***** | | | | The licensee exited the Unusual Event at 0210 upon confirmation of a stable | | off-site power. | | | | Notified R1 IRC and FEMA(Heyman). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40070 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DAVIS BESSE REGION: 3 |NOTIFICATION DATE: 08/14/2003| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 16:54[EDT]| | RXTYPE: [1] B&W-R-LP |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:10[EDT]| | NRC NOTIFIED BY: DON BONDY |LAST UPDATE DATE: 08/14/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |SONIA BURGESS R3 | |10 CFR SECTION: |STUART RICHARDS NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |HYMAN FEMA | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO A LOSS OF OFFSITE POWER. | | | | All systems operated as expected. Decay Heat pumps are available if | | needed. | | | | NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40071 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 08/14/2003| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 17:15[EDT]| | RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:35[EDT]| | NRC NOTIFIED BY: HELKER |LAST UPDATE DATE: 08/15/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |GLENN MEYER R1 | |10 CFR SECTION: |STUART RICHARDS NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |HYMAN FEMA | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO LOSS OF OFFSITE POWER GREATER THAN 15 MINUTES. | | | | | | Automatic reactor scram due to a loss of offsite power. All rods fully | | inserted into the core. All emergency core cooling systems are operating | | properly and the emergency diesel generators are operating properly. | | | | NRC Resident Inspector was notified of this event by the licensee. | | | | *****UPDATE 8/15/03 AT 0145 TO LAURA***** | | | | Offsite electrical power was restored. The licensee exited the Unusual Event | | at 0123. Notified R1IRC and FEMA(Heyman). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40072 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 08/14/2003| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 17:17[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:11[EDT]| | NRC NOTIFIED BY: TIM PAGE |LAST UPDATE DATE: 08/15/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |GLENN MEYER R1 | |10 CFR SECTION: |STUART RICHARDS NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |HYMAN FEMA | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT DECLARED DUE TO A LOSS OF OFFSITE POWER. | | | | Automatic reactor scram due to a loss of offsite power. All rods fully | | inserted into the core. All emergency core cooling systems and the | | emergency diesel generators are operating properly. | | | | NRC Resident Inspector was notified of this event by the licensee. | | | | *****UPDATE ON 8/15/03 AT 0035 FROM PAGE TO LAURA***** | | | | Reactor vessel pressure is 93 psig. Plant electrical loads have been | | shifted back to offsite power and the EDGs were secured. The licensee exited | | the Unusual Event at 0039. The licensee tentatively plans to remain shutdown | | for a brief period to do some maintenance work. | | | | Notified R1IRC and FEMA(Heyman). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40073 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: INDIAN POINT REGION: 1 |NOTIFICATION DATE: 08/14/2003| | UNIT: [2] [3] [] STATE: NY |NOTIFICATION TIME: 18:49[EDT]| | RXTYPE: [2] W-4-LP,[3] W-4-LP |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:25[EDT]| | NRC NOTIFIED BY: FINUCAH |LAST UPDATE DATE: 08/14/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |GLENN MEYER R1 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 N N 0 Hot Shutdown |0 Hot Shutdown | |3 N N 0 Hot Shutdown |0 Hot Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | EMERGENCY SIRENS LOST IN FOUR COUNTIES | | | | Emergency sirens lost in four counties due to a loss of power. At | | approximately 1830 hours power starting to be returned to the sirens. | | | | NRC Resident Inspector notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40074 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 08/14/2003| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 20:07[EDT]| | RXTYPE: [1] W-2-LP |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:11[EDT]| | NRC NOTIFIED BY: Roy Gillow |LAST UPDATE DATE: 08/14/2003| | HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |GLENN MEYER R1 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR TRIP/AUXILIARY FEEDWATER ACTUATION | | | | Received grid disturbance that caused reactor trip at 1611. The trip | | occurred due to over temperature delta set point being reached from load | | swings experienced on the generator. Subsequently in the recovery process, | | the Auxiliary Feedwater Pumps auto started from a signal from the Main | | Feedwater Pumps being secured. As a result of grid problems it was noted | | that Ginna did not meet the required number of emergency sirens (greater | | than 25% of sirens without power). | | | | | | NRC Resident Inspector was notified of this event by the licensee. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 40075 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FERMI REGION: 3 |NOTIFICATION DATE: 08/14/2003| | UNIT: [2] [] [] STATE: MI |NOTIFICATION TIME: 20:08[EDT]| | RXTYPE: [2] GE-4 |EVENT DATE: 08/14/2003| +------------------------------------------------+EVENT TIME: 16:10[EDT]| | NRC NOTIFIED BY: KEVIN DAHM |LAST UPDATE DATE: 08/14/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |SONIA BURGESS R3 | |10 CFR SECTION: |STUART RICHARDS NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |HYMAN FEMA | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |2 A/R Y 100 Power Operation |0 Hot Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | PLANT ENTERED AN NOUE DUE TO THE LOSS OF OFF SITE POWER | | | | The reactor scrammed from 100% power due to fluctuations occurring on the | | main generator and a loss of off site power. All rods fully inserted and | | all MSIV's closed. Reactor level is being maintained in the normal band of | | 173 to 214 inches using RCIC. Reactor pressure is being controlled via | | SRV's in lo-lo set mode between 905 and 1017 psig. Isolations occurred as | | expected for level 2 and level 3. HPCI and RCIC started on level 2 signal. | | HPCI has been shutdown but is available. All 4 EDG's started and loaded. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Wednesday, March 24, 2021
Page Last Reviewed/Updated Wednesday, March 24, 2021