Event Notification Report for May 19, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/16/2003 - 05/19/2003 ** EVENT NUMBERS ** 39849 39851 39853 39854 39855 39856 39857 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39849 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 05/15/2003| | UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 05:27[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/15/2003| +------------------------------------------------+EVENT TIME: 02:52[CDT]| | NRC NOTIFIED BY: HALL |LAST UPDATE DATE: 05/16/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WILLIAM JOHNSON R4 | |10 CFR SECTION: |MICHAEL CASE NRR | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA|RICHARD WESSMAN IRO | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 100 Power Operation |0 Hot Standby | |2 A/R Y 100 Power Operation |0 Hot Standby | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | REACTOR TRIP FROM 100% POWER ON BOTH UNITS DUE TO TURBINE TRIP ON BOTH | | UNITS | | | | The licensee reported that a loss of power on the 345KV grid caused a | | turbine trip on both units which resulted in a reactor trip from 100% on | | both units. All rods fully inserted and no ECCS was actuated. Both units | | are currently at Mode 3 in natural circulation and stable. The auxiliary | | feed water systems started on both units to maintain steam generator levels. | | The reactor coolant temperature is being controlled by using the steam | | generator atmospheric relief valves. Since the safety systems were powered | | by an alternate offsite power supply, the 4 emergency diesels did not auto | | start, but they are operable. The licensee is investigating why they lost | | the 345KV grid. | | | | | | The NRC Resident Inspector was notified. | | | | *****UPDATE ON 5/16/03 AT 1500 EST FROM D. BUTLER TO R. LAURA***** | | | | "Status as of 10:30, 05/16/03 - Sequence of Events | | | | 1. Parker line experiences a `B' phase to ground fault at 02:52. | | 2. CPSES [Comanche Peak Steam Electric Station] Parker feeder breaker 8040 | | fails to trip as required. | | | | Primary and backup ground relaying do not actuate. No trip signal is sent to | | the Parker breaker. | | Should normal tripping have occurred, fault would likely have cleared and | | event ended. | | | | East Bus backup timers are not initiated due to lack of Parker Breaker 8040 | | trip signal. Operation of the | | backup timers would have isolated the East bus. CPSES impact would likely | | have been lowering one unit to | | 50% power while operating the other unit at 100% power. | | | | 3. Parker line remains faulted with fault current being supplied from the | | East bus, West bus and CPSES generation. | | 4. Approximately 30 cycles into the fault, 345 Kv offsite feeds began to | | trip via their own protective schemes. | | 5. At approximately 1.3 seconds, Unit 1 and 2 Main Generator breakers trip | | on generator backup Main transformer | | neutral ground relaying. | | 6. Unit 1 and 2 Main Generator lockout relays actuate on Load Rejection | | protection. | | 7. Unit 1 and Unit 2 Normal 6.9KV busses trip on Generator lockout signals. | | 8. Unit 1 Normal busses slow transfer to Station Transformer 1 ST at | | approximately 5 seconds. | | Unit 2 two normal bus alternate feed 2ST has been de-energized from the 8080 | | breaker blocking slow | | transfer operation. | | 9. Station Transformer 1 ST `C' phase time over current relaying operates | | generating a 1 ST lockout signal. | | 10. Unit 1 normal 6.9Kv bus alternate feeder breakers are tripped via the 1 | | ST lockout signal. | | Unit 1 and Unit 2 normal 6.9Kv busses are now de-energized. | | 11. East and West busses are inspected by ONCOR and CPSES Maintenance. | | Switchyard West bus is re- | | energized from the Wolf Hollow Line. | | 12. Station transformers 1ST and 2ST are re-energized and power restored to | | Unit 1 and 2 Normal 6.9KV busses. | | | | "Troubleshooting | | | | "Primary Fault detection relay is tested and is found failed. The Fault | | detector serves as a Supervisory relay during line faults. It serves as a | | trip permissive, placing the trip circuits of the ground detection relaying | | in service. Failure of the Fault Detector is the obvious cause of the | | Primary relay protection scheme failure to operate. Backup Fault detection | | relay is tested and is found to operate correctly. Failure of the backup | | protection scheme is likely caused by the inconsistent operation of the | | backup ground relay and failure of the CA unit of the Zone 1 relay." | | | | Notified R4DO (Johnson) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39851 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NATIONAL RESPONSE CENTER |NOTIFICATION DATE: 05/15/2003| |LICENSEE: NORTH ANNA |NOTIFICATION TIME: 13:45[EDT]| | CITY: KINGMAN REGION: 4 |EVENT DATE: 05/14/2003| | COUNTY: SUMNER STATE: KS |EVENT TIME: 18:00[CDT]| |LICENSE#: AGREEMENT: Y |LAST UPDATE DATE: 05/16/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |WILLIAM JOHNSON R4 | | |DOUG BROADDUS NMSS | +------------------------------------------------+TIM MCGINTY DIRO | | NRC NOTIFIED BY: LYNN WARRICK |JANICE KROON EPA | | HQ OPS OFFICER: ERIC THOMAS |DAVID WHITFILL STAT | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TRANSPORTATION INCIDENT | | | | The National Response Center sent a fax to the Operations Center regarding | | the following transportation incident: | | | | A tractor trailer carrying the reactor vessel head from North Anna power | | plant to EnviroCare in Clive, UT was sideswiped by a pickup truck being | | driven by a drunk driver near Kingman, KS on Route 42. The pickup truck | | passed the tractor trailer at approximately 80 mph, and proceeded down the | | road, where it was involved in a traffic accident. The incidental impact | | between the pickup and the tractor trailer caused a minor tear in the | | protective tarp and plastic container containing the vessel head, along with | | depositing some paint on the head itself. There was no apparent structural | | damage to the vessel head, and no apparent radioactive release into the | | atmosphere. | | | | The truck driver stopped his vehicle in Greensburg, Kansas to assess the | | condition of the vessel head. The shipper is sending a representative to | | inspect the packing material integrity. The state of Kansas will also be | | sending a representative out to the scene to assist. | | | | *****UPDATE ON 5/16/03 AT 13:50 EST FROM CONNELLY TO LAURA***** | | | | Three independent radiological surveys conducted by the State of Kansas and | | North Anna determined there was no spread of contamination and only minor | | damage occurred to the shipping packaging for the vessel head. The minor | | damage was repaired and the truck was released. | | | | Notified R4DO (W. Johnson), DIRO (McGinty) and NMSS (Essig). | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Fuel Cycle Facility |Event Number: 39853 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PORTSMOUTH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 05/16/2003| | RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 10:04[EDT]| | COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 05/15/2003| | 6903 ROCKLEDGE DRIVE |EVENT TIME: 14:00[EDT]| | BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 05/16/2003| | CITY: PIKETON REGION: 3 +-----------------------------+ | COUNTY: PIKE STATE: OH |PERSON ORGANIZATION | |LICENSE#: GDP-2 AGREEMENT: N |SONIA BURGESS R3 | | DOCKET: 0707002 |TOM ESSIG NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: MCCLEERY | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |QSAF 72.75(c)(2) SAFETY EQUIP DISABLED/F| | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SAFETY SYSTEM ACTUATION | | | | On 5/15/03 @1400 during pigtail disconnect, a small amount of particulate | | fell from the pigtail. This particulate began to smoke resulting in a see | | and flee. During the see and flee the gas release alarm was activated. The | | alarm resulted in the actuation of a "Q" Safety system while in applicable | | mode (mode III). The PSS Responded to the see and flee. The affected | | cylinder was made inoperable. No spread of contamination outside already | | posted area. Air sampling results are less than MDA. | | | | The NRC Resident Inspector was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39854 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 05/16/2003| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 12:53[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 05/16/2003| +------------------------------------------------+EVENT TIME: 04:56[EDT]| | NRC NOTIFIED BY: JOHN YADUSKY |LAST UPDATE DATE: 05/16/2003| | HQ OPS OFFICER: ERIC THOMAS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROBERT HAAG R2 | |10 CFR SECTION: | | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Hot Standby |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | SPECIFIED SYSTEM ACTUATION | | | | "On 5/16/03 with the reactor shutdown in MODE 3, an unplanned actuation of | | Auxiliary Feedwater (AFW) system occurred during testing of the 'B' Main | | Feed Pump (MFP). A trip of an uncoupled MFP generated a signal to start | | both motor-driven AFW pumps during testing following maintenance. The 'A' | | motor-driven AFW pump was already in service, so the 'B' AFW pump started on | | receipt of the signal. Feed to the steam generators was always available, | | even without the additional actuation of the AFW system. The purpose of the | | actuation of AFW following a trip of the main feed system is to ensure | | adequate flow to the steam generator. In this case, the main feed pump was | | being tested and was not being used to provide flow to the steam generator. | | Therefore the actuation was not required to provide any safety function. | | The 'B' motor-driven AFW pump was secured within approximately two minutes | | because the additional flow was not required. This condition is being | | reported as an unplanned system actuation in accordance with 10 CFR | | 50.72(b)(3)(iv)(A). | | | | "10 CFR 50.72 requires an 8-hour report for, 'Any event or condition that | | results in valid actuation of any of the systems listed in paragraph | | (b)(3)(iv)(B) of this section except when the actuation results from and is | | part of a pre-planned sequence during testing or reactor operation.' In | | this case, the AFW pump start signal due to trip of the last running MFP is | | only applicable in MODES 1 and 2, and is not required in the current MODE of | | plant operation (MODE 3). | | | | "The NRC Resident Inspector was notified." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39855 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: COOK REGION: 3 |NOTIFICATION DATE: 05/18/2003| | UNIT: [] [2] [] STATE: MI |NOTIFICATION TIME: 04:27[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 05/17/2003| +------------------------------------------------+EVENT TIME: 22:05[EDT]| | NRC NOTIFIED BY: BRIAN BATES |LAST UPDATE DATE: 05/18/2003| | HQ OPS OFFICER: ARLON COSTA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |SONIA BURGESS R3 | |10 CFR SECTION: |MICHAEL CASE NRR | |ADEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling Shutdow|0 Refueling Shutdow| | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DEGRADED CONDITION DUE TO CRACK INDICATIONS ON VESSEL HEAD | | | | "At 18:00 on 5/15/03, craze cracking indications were found on a Reactor | | Pressure Vessel Head Penetration. At 22:05 on 5/17/03, it was determined | | that this condition was reportable as a prompt eight-hour report under 10 | | CFR 50.72(b)(3)(ii)(A). | | | | "During the Unit 2 reactor head inspection, five small, shallow indications | | were found on the inside diameter of penetration #74. The indications are | | closely spaced and are approximately 3/8 inch below the J-groove weld | | region. Initial calculations showed a crack depth of 0.117 inches. All of | | the indications are bounded within an area that is one inch wide by 2.6 | | inches high. There was no through-wall leakage and the reactor coolant | | pressure boundary remains intact. | | | | "These indications were previously identified during the last refueling | | outage in February 2002. They were evaluated as acceptable to leave in | | service for a full cycle at that time, and they have not shown any | | significant growth since then. | | | | "The industry guidance on projected flaw growth rates has been revised since | | these indications were discovered in 2002. As a result, the new projections | | for these indications result in less than a full fuel cycle before reaching | | the limit for remaining in service. Therefore, repairs will be needed. | | Current plans are to perform an excavation of the affected area, under | | existing code guidance." | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39856 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 05/18/2003| | UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 21:58[EDT]| | RXTYPE: [1] W-3-LP |EVENT DATE: 05/18/2003| +------------------------------------------------+EVENT TIME: 18:07[EDT]| | NRC NOTIFIED BY: RANDY WILSON |LAST UPDATE DATE: 05/18/2003| | HQ OPS OFFICER: ERIC THOMAS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROBERT HAAG R2 | |10 CFR SECTION: | | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA| | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 28 Power Operation |0 Hot Standby | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | RPS ACTUATION WHILE CRITICAL | | | | "On 5/18/03 with the reactor at 28 percent power in MODE 1, an unplanned | | actuation of the reactor protection system occurred. At 1807 the reactor | | was automatically tripped from a turbine trip - reactor trip signal. All | | systems functioned as required and no other safety systems were actuated. | | The operations staff responded to the event in accordance with applicable | | plant procedures. The plant stabilized at normal operating no-load Reactor | | Coolant System temperature and pressure following the reactor trip. The | | cause of the turbine trip is under investigation. | | | | "This condition is being reported as an unplanned reactor protection system | | actuation in accordance with 10 CFR 50.72(b)(2)(IV)(B) and 10 CFR | | 50.72(b)(3)(iv)(A)." | | | | All rods fully inserted and decay heat is being removed via the PORV's. | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39857 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PILGRIM REGION: 1 |NOTIFICATION DATE: 05/19/2003| | UNIT: [1] [] [] STATE: MA |NOTIFICATION TIME: 05:57[EDT]| | RXTYPE: [1] GE-3 |EVENT DATE: 05/19/2003| +------------------------------------------------+EVENT TIME: 04:24[EDT]| | NRC NOTIFIED BY: MARTIN MANPENFEL |LAST UPDATE DATE: 05/19/2003| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |BRIAN MCDERMOTT R1 | |10 CFR SECTION: |TERRY REIS NRR | |ARPS 50.72(b)(2)(iv)(B) RPS ACTUATION - CRITICA|RICHARD WESSMAN IRO | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 A/R Y 3 Startup |0 Startup | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC REACTOR SCRAM RESULTING IN PRIMARY CONTAINMENT AND REACTOR | | BUILDING ISOLATIONS | | | | At 0424 EDT, during startup operations, the Main Turbine Bypass valves | | unexpectedly opened and depressurized the reactor vessel. After | | depressurization, the reactor level increased due to swell and caused an | | automatic reactor scram. Additionally, there was a Reactor Building | | Isolation Signal and Group I, II, and VI Primary Containment Isolation | | Signal generated. Immediately after the automatic scram, five control rods | | failed to insert into the core. Plant operations personnel performed | | actions in accordance with their Emergency Operating Procedures to drive the | | control rods into the core. According to the licensee, adequate shutdown | | margin was always maintained. | | | | The plant electrical system is stable with plant equipment being powered | | from offsite and the startup transformer. Reactor pressure and level are | | being maintained via steam line drains to the main condenser. | | | | Troubleshooting of the Main Turbine Bypass valves/control system is in | | progress. | | | | The licensee will be notifying the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021