Event Notification Report for May 6, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 05/05/2003 - 05/06/2003 ** EVENT NUMBERS ** 39811 39812 39814 39823 39825 39826 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39811 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 04/30/2003| |LICENSEE: ALBEMARLE CORPORATION |NOTIFICATION TIME: 13:18[EDT]| | CITY: PASADENA REGION: 4 |EVENT DATE: 04/28/2003| | COUNTY: STATE: TX |EVENT TIME: 07:00[CDT]| |LICENSE#: LO4072-000 AGREEMENT: Y |LAST UPDATE DATE: 04/30/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GREG PICK R4 | | |DOUG BROADDUS NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES OGDEN | | | HQ OPS OFFICER: RICH LAURA | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | TEXAS AGREEMENT STATE REPORT ON DISABLED GAUGE FOR OIL CRACKING PLANT | | | | "Licensee immediately suspended operations in the affected "reactor" (oil | | cracking plant) due to loss of measurement caused by loss of level/density | | measurements from an Ohmart Corporation (OC) Model SH-F2, source holder, | | containing 1 curie of Cs-137, Serial # 68526, located on the exterior | | surface of the SAS Sodium reactor, vessel # R-7202. Operators noted a loss | | of measurement at approximately 7:00 a.m. When investigating the outside of | | the reactor vessel, on-site personnel noted that the fixed gauge had broken | | free of its mounting bracket and fallen, face-down, approximately 10 feet to | | the ground. Plant personnel immediately notified Techstar, a subsidiary of | | Ohmart/Vega Corporation, for field service. A service technician arrived on | | scene, surveyed the gauge for radiation leakage, checked for contamination, | | and checked the functional operation of the gauge. The shutter was closed | | and locked by service personnel, until damage could be assessed. No damage | | was sustained by the gauge. The mechanism was fully functional and has been | | reinstalled on the reactor vessel. A set screw (a 3/4 to 1 inch bolt) had | | failed on the mounting bracket, due to suspected structural fatigue and | | vibration over 11 years since the gauge was installed (December 1992). The | | gauge was reinstalled in a bracket modified to fit on the welded beam | | (2-inch pipe), that will not allow the gauge to fall if the set screw fails | | in the future. All other gauges on site were checked by service personnel | | for security and possible deterioration on mounting hardware. This gauge was | | unique in this plant due to it's mounting which has now been upgraded to | | allow for fail-safe operation without loss of function should the bracket | | fail. Problem has been corrected by the service company. Modification to the | | mounting bracket and replacement of the set screw has rectified the cause of | | this incident and returned the reactor to operation." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39812 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 04/30/2003| | UNIT: [] [2] [] STATE: FL |NOTIFICATION TIME: 21:52[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 04/30/2003| +------------------------------------------------+EVENT TIME: 14:20[EDT]| | NRC NOTIFIED BY: CHARLES PIKE |LAST UPDATE DATE: 05/05/2003| | HQ OPS OFFICER: ARLON COSTA +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOEL MUNDAY R2 | |10 CFR SECTION: |FRANK GILLESPIE NRR | |ADEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | DEGRADED CONDITION DUE TO DEFECT IN REACTOR VESSEL HEAD PENETRATION | | | | "On April 30, 2003, at 1420 hours, with St. Lucie Unit 2 in a refueling | | outage, FPL discovered a defect in reactor vessel head penetration 72. This | | flaw was found during the ongoing reactor vessel head inspection being | | performed in accordance with the requirements of NRC Order EA-03-009. The | | defect is OD surface connected, extends into the nozzle and penetrates into | | the J-groove weld between the nozzle and reactor vessel head. The defect is | | described as an axial flaw, 0.28 inches deep X 0.96 inches long, on the | | downhill side of the penetration. Per the inspection guidance, surface flaws | | located in the attachment weld area are not acceptable. | | | | "There had been no indication of RCS leakage during the previous cycle's | | operation. This notification is being made in accordance with 10 CFR | | 50.72(b)(3)(ii)(A)." | | | | The Licensee notified the NRC Resident Inspector. | | | | *** UPDATE ON 5/2/03 AT 1337 EDT FROM R.WELLER TO A. COSTA *** | | | | "This report is a supplement to original event report #39812 dated April 30, | | 2003. On May 2, 2003 at 1240 hours, with St. Lucie Unit 2 in a refueling | | outage, FPL discovered a defect in reactor vessel head penetration #18. This | | is the second flaw found during the current ongoing reactor vessel head | | inspection being performed in accordance with the requirements of NRC Order | | EA-03-009. The defect is OD surface connected, extends into the nozzle and | | through the J-groove weld between the nozzle and reactor vessel head. The | | defect is described as an axial flaw, 0.39 inches deep X 2.98 inches long, | | on the downhill side of the penetration. Per the inspection guidance, | | surface flaws located in the attachment weld area are not acceptable. There | | had been no indication of RCS pressure boundary leakage during the previous | | cycles operation. This notification is being made in accordance with 10 CFR | | 50.72(b)(3)(ii)(A)." | | | | The Licensee notified the NRC Resident Inspector. | | | | * * * UPDATE ON 5/05/03 @ 1503 BY HESSLING TO GOULD * * * | | | | This report is a correction to the supplement to original event report | | #39812 dated April 30, 2003. On May 2, 2003 at 1240 hours, with St. Lucie | | Unit 2 in a refueling outage, FPL discovered a defect in reactor vessel head | | penetration #18. The second flaw was incorrectly identified to be 0.39 | | inches in depth, and 2.98 inches in length, located on the down-hill side of | | the penetration. The correct depth was 0.26 inches in depth, length was 2.98 | | inches. The location of this flaw was on the side of the penetration, vice | | on the down-hill side. This flaw was found during the current ongoing | | reactor vessel head inspection being performed in accordance with the | | requirements of NRC Order RA-03-009. The defect is OD surface connected, | | extends into the nozzle and through the J-groove weld between the nozzle and | | reactor vessel head. The defect is described as an axial flaw. Per the | | inspection guidance, surface flaws located in the attachment weld area are | | not acceptable. There had been no indication of RCS pressure boundary | | leakage during the previous cycle's operation. | | | | | | The NRC Resident Inspector was notified. | | | | The Reg 2 RDO (Munday) was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39814 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: NE DIV OF RADIOACTIVE MATERIALS |NOTIFICATION DATE: 05/01/2003| |LICENSEE: BECTON DICKSON CONSUMER PRODUCTS |NOTIFICATION TIME: 09:54[EDT]| | CITY: HOLDREGE REGION: 4 |EVENT DATE: 04/27/2003| | COUNTY: STATE: NE |EVENT TIME: 12:00[CDT]| |LICENSE#: 37--3-01 AGREEMENT: Y |LAST UPDATE DATE: 05/01/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |GREG PICK R4 | | |TOM ESSIG NMSS | +------------------------------------------------+ | | NRC NOTIFIED BY: H. SHUMAN | | | HQ OPS OFFICER: JOHN MacKINNON | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | STUCK IRRADIATOR SOURCE | | | | The State of Nebraska was notified by Becton Dickson Consumer Products | | located in Holdrege, Nebraska, that on 04/27/03 a source got stuck in the | | Becton Dickson Pool Irradiator. The stuck source was moved to a shielded | | position. Nordion repaired the stuck source on 04/27/03. Nobody was exposed | | to the stuck source. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Other Nuclear Material |Event Number: 39823 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: FOX CHASE CANCER CENTER |NOTIFICATION DATE: 05/05/2003| |LICENSEE: FOX CHASE CANCER CENTER |NOTIFICATION TIME: 12:50[EDT]| | CITY: PHILADELPHIA REGION: 1 |EVENT DATE: 05/02/2003| | COUNTY: STATE: PA |EVENT TIME: 10:48[EDT]| |LICENSE#: 37-02766-01 AGREEMENT: N |LAST UPDATE DATE: 05/05/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |EUGENE COBEY R1 | | |DOUG BROADDUS NMSS | +------------------------------------------------+ROGER LANKSBURY R3 | | NRC NOTIFIED BY: SHEEHAN | | | HQ OPS OFFICER: CHAUNCEY GOULD | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BLO2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | MISSING FEDEX SHIPMENT OF PHOSPHORUS-32 | | | | The licensee, Fox Chase Cancer Center reported not receiving a shipment of | | 351 micro curies of liquid P-32 from Amersham's Arlington, Illinois | | facility. The material, which is used in the licensee's research lab, was | | shipped via FEDEX on 4/11/03 and was to be received on 4/14/03. The | | material was scanned when loaded on the FEDEX truck, but not scanned when | | the delivery was made at the licensee's facilities. The licensee has no | | record of receiving the package and has filed a claim with FEDEX. FEDEX is | | still investigating. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39825 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 05/05/2003| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 17:44[EDT]| | RXTYPE: [1] GE-4 |EVENT DATE: 05/05/2003| +------------------------------------------------+EVENT TIME: 14:45[EDT]| | NRC NOTIFIED BY: HALLIDAY |LAST UPDATE DATE: 05/05/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |EUGENE COBEY R1 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFF SITE NOTIFICATION DUE TO LOSS OF 35 POUNDS OF FREON R-22. | | | | The licensee discovered that approximately 35 lbs of freon R-22 was missing | | from a plant refrigeration system. The State of New York requires the | | licensee to notify the National Response Center, New York State Department | | of Environmental Conservation and Oswego County Emergency Management Office | | of R-22 leaks to air >1 lb in any 24 hour period. The system currently | | tested tight, however an investigation is showing there was probably an | | acute release >1 lb during recent maintenance activities. | | | | The licensee notified the NRC Resident Inspector, the State, local agencies | | and other Government Agencies. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39826 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: TURKEY POINT REGION: 2 |NOTIFICATION DATE: 05/05/2003| | UNIT: [3] [4] [] STATE: FL |NOTIFICATION TIME: 23:48[EDT]| | RXTYPE: [3] W-3-LP,[4] W-3-LP |EVENT DATE: 05/05/2003| +------------------------------------------------+EVENT TIME: 20:41[EDT]| | NRC NOTIFIED BY: HARRISON |LAST UPDATE DATE: 05/05/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOEL MUNDAY R2 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |3 N Y 100 Power Operation |100 Power Operation | |4 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST ERDS DUE TO COMPUTER MALFUNCTION | | | | "Loss of ERDS communication Link from 20:41 [EDT] until 22:26 [EDT] 5/5/03. | | Computer displayed hard disk error. Rebooted machine; error corrected. | | Re-established ERDS Link." | | | | The NRC Resident Inspector will be notified by the licensee. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021