Event Notification Report for April 9, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/08/2003 - 04/09/2003 ** EVENT NUMBERS ** 39226 39723 39729 39741 39742 39743 +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39226 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: PALO VERDE REGION: 4 |NOTIFICATION DATE: 09/27/2002| | UNIT: [1] [2] [3] STATE: AZ |NOTIFICATION TIME: 18:52[EDT]| | RXTYPE: [1] CE,[2] CE,[3] CE |EVENT DATE: 09/27/2002| +------------------------------------------------+EVENT TIME: 15:00[MST]| | NRC NOTIFIED BY: STROUD |LAST UPDATE DATE: 04/08/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |JOHN PELLET R4 | |10 CFR SECTION: | | |APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 99 Power Operation |99 Power Operation | |2 N Y 99 Power Operation |99 Power Operation | |3 N Y 99 Power Operation |99 Power Operation | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | OFF-SITE NOTIFICATION | | | | On September 27, 2002 at approximately 15:00 Mountain Standard Time, Palo | | Verde Nuclear Generating Station | | (PVNGS) notified the Environmental Protection Agency (EPA) that a INITIAL | | NOTIFICATION OF CONTINUOUS RELEASE was being reported. | | | | The following information was provided to the National Response Center and | | State of Arizona: | | | | "Palo Verde Nuclear Generating Station is calling to make an initial | | notification of a continuous release in accordance | | with CERCLA Section 103(f)(2). 40CFR 302.8 (d). This is not an accidental | | or episodic release. | | | | Palo Verde Nuclear Generating Station will be performing a scheduled steam | | generator cleaning activity as part of its routine refueling outage for Unit | | 1. The steam generator cleaning activity will begin on Saturday, September | | 28 at approximately 18:00. During this activity, Palo Verde Nuclear | | Generating Station will exceed the Reportable Quantities for the release of | | ammonia and hydrazine. The same activity is scheduled to occur during the | | Unit 3 refueling outage, spring of 2003. The activity occurs approximately | | once per every five to seven years on each unit. The hazardous substances | | released are ammonia (CAS #7684-41-7) and hydrazine (CAS #302-01-2). PVNGS | | expects no adverse effects to health and welfare of the general public, nor | | to the environment. | | | | The NRC Resident Inspector was notified along with the State. | | | | * * * UPDATE ON 4/8/03 FROM DAN MARKS TO HOWIE CROUCH * * * | | | | The following information was received from the Licensee via facsimile: | | | | "The following event description is a follow-up notification to ENS 39226, | | placed at 15:12 Mountain Standard Time (MST) (18:52 ET) on 09/27/2002. | | | | "ENS 39226 informed the NRC of a government notification to the National | | Response Center (EPA), the State of Arizona and Maricopa County related to a | | continuous release in accordance with CERCLA [Comprehensive Environmental | | Response, Compensation, and Liability Act] Section 103(f)(2), 40 CFR | | 302.8(d). This was not an accidental or episodic release. The planned | | release was the result of steam generator cleaning activities and would | | result in exceeding the Reportable Quantities for the release of ammonia | | (CAS #7664-41-7) and hydrazine (CAS #302-01-2). | | | | "Included in the notification was the schedule to occur in Palo Verde Unit 3 | | during its refueling outage in the spring of 2003. | | | | "Since that original notification, Palo Verde has implemented a condensation | | unit that captures a large amount of the effluent prior to release. | | Although the Reportable Quantities will still be exceeded, the notification | | to the National Response Center (EPA), [Maricopa County] and the State of | | Arizona will identify the lower levels. | | | | "The contact name for information concerning this notification is [DELETED], | | Environmental Section Leader, at telephone number [DELTED]. | | | | "As during the previous notification, PVNGS [Palo Verde Nuclear Generating | | Station] expects no adverse effects to the health and safety of the public, | | nor to the environment." | | | | The Licensee has notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39723 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 04/03/2003| |LICENSEE: TEXAS DEPT OF TRANSPORTATION |NOTIFICATION TIME: 12:21[EST]| | CITY: ABILENE REGION: 4 |EVENT DATE: 03/31/2003| | COUNTY: STATE: TX |EVENT TIME: 22:00[CST]| |LICENSE#: L00197 AGREEMENT: Y |LAST UPDATE DATE: 04/03/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANTHONY GODY R4 | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES H. OGDEN, JR | | | HQ OPS OFFICER: ERIC THOMAS | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ATTEMPTED THEFT OF A TROXLER GAUGE | | | | The Texas Department of Health reported the attempted theft of a Troxler | | Model 3430, (serial # unknown), on the night of 3/31/03 from a secure | | storage trailer at a Texas Department of Transportation construction site in | | Abilene, TX. Site personnel discovered the gauge in an open case on the | | floor of a construction trailer with its lock cut. The trailer and its | | storage closet had been broken into. The sealed source contains 8 | | millicuries of Cs-137 and 40 millicuries of Am-241/Be. Gauge is currently | | secured in a different area awaiting results of leak and serviceability | | tests. An investigation is in process to determine whether other items were | | stolen, or whether this gauge was the only target of the attempted theft. | | | | This event is technically not reportable, but was entered as an attempted | | theft due to three other similar incidents that did result in stolen gauges | | in the Dallas-Fort Worth area under similar circumstances. The Texas | | Department of Transportation notified all other licensee's possessing | | portable nuclear gauges in the Abiline and Dallas-Fort Worth regions, along | | with local police and the Dallas FBI office. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39729 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 04/04/2003| | UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 09:43[EST]| | RXTYPE: [1] W-2-LP |EVENT DATE: 04/04/2003| +------------------------------------------------+EVENT TIME: 07:16[EST]| | NRC NOTIFIED BY: MCLAUGHLIN |LAST UPDATE DATE: 04/08/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |RONALD BELLAMY R1 | |10 CFR SECTION: | | |ACOM 50.72(b)(3)(xiii) LOSS COMM/ASMT/RESPONSE| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOSS OF MORE THAN 50% OF THE EMERGENCY SIRENS | | | | The plant has 59 of the 96 offsite notification system sirens out of service | | due to loss of power caused by ice storms damage to the electrical power | | supplies. They do not know how soon the sirens will be returned to | | service. | | | | The NRC Resident Inspector and local government were notified and the state | | will be informed. | | | | * * * UPDATE AT 1436 EDT ON 4/8/03 FROM DOUG PETERSON TO ERIC THOMAS * * * | | | | 82 of the 96 offsite notification system sirens are back in service. 13.5% | | of the sirens remain inoperable. | | | | The NRC Resident Inspector has been notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39741 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 04/07/2003| | UNIT: [] [2] [] STATE: MD |NOTIFICATION TIME: 22:36[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 04/07/2003| +------------------------------------------------+EVENT TIME: 22:19[EDT]| | NRC NOTIFIED BY: DAVE LYNCH |LAST UPDATE DATE: 04/08/2003| | HQ OPS OFFICER: ERIC THOMAS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |JAMES TRAPP R1 | |10 CFR SECTION: |BRUCE BOGER NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |RICHARD WESSMAN IRO | | |WILLIAM KANE ET | | |HUBERT MILLER RA | | |FEMA | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT | | | | At 2201, a fire started in the pressurizer doghouse. Welding operations | | were ongoing in the upper part of the space, and a slag catchment device | | lower in the space caught fire. The fire brigade responded to the scene. | | At 2219, the licensee declared an Unusual Event because of an ongoing fire | | in the vital area for greater than 15 minutes. At 2234, the fire was put | | out by pouring water down onto the fire from above, and a reflash watch was | | set. There was no damage noted to plant equipment, and no injuries to | | personnel. | | | | The licensee notified the NRC Resident Inspector and the surrounding | | counties. | | | | * * * UPDATE AT 2309 ON 4/7/03 FROM DAVE SEPANICH TO ERIC THOMAS * * * | | | | At 2300, the licensee secured from the Unusual Event. There was no damage | | noted to plant components, and scaffolding will be erected to conduct | | further inspections. | | | | The licensee notified the NRC Resident Inspector and the surrounding | | counties. | | | | * * * UPDATE AT 0008 ON 4/8/03 FROM MIKE KORSNICK TO ERIC THOMAS * * * | | | | The cause of the fire was slag from welding operations that fell through | | some fire blankets and ignited the herculite underneath. A fire brigade | | member will be sent back into the space this morning to conduct further | | damage assessment. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39742 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALLAWAY REGION: 4 |NOTIFICATION DATE: 04/08/2003| | UNIT: [1] [] [] STATE: MO |NOTIFICATION TIME: 15:10[EDT]| | RXTYPE: [1] W-4-LP |EVENT DATE: 04/07/2003| +------------------------------------------------+EVENT TIME: 14:10[CDT]| | NRC NOTIFIED BY: JAMES CUNNINGHAM |LAST UPDATE DATE: 04/08/2003| | HQ OPS OFFICER: ERIC THOMAS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DAVE LOVELESS R4 | |10 CFR SECTION: | | |NINF INFORMATION ONLY | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N Y 100 Power Operation |100 Power Operation | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | INFORMATION CALL | | | | "Unfounded Suspicious Call concerning demonstrations at the Callaway Nuclear | | Plant. | | | | "On 04/07/03 at approximately 1400 hours, the Assistant Superintendent of | | Security at the Callaway Plant received a call from Callaway County Sheriff. | | The sheriff stated that on 04/04/03 at 2036 hours the county dispatcher | | received an anonymous call stating that a demonstration would take place at | | the Callaway Plant on Wednesday April 9, 2003. The caller did not offer any | | additional information even when questioned other than he would get hurt if | | he stated anything else. | | | | "[Neither] Ameren Corporate Security, Callaway Plant Security, Callaway | | County Sheriff's Department nor [DELETED] with the FBI office in Jefferson | | City have received or come in contact with any information concerning any | | type of possible demonstration. | | | | "The Callaway Plant EDO, Protective Services Superintendent and Vice | | President were notified of this call. The Sheriff's Department plans on | | conducting extra patrols of the area on 04/09/03 as well as an increased | | awareness by Security." | | | | Notified IAT (J. Davidson) | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39743 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DIABLO CANYON REGION: 4 |NOTIFICATION DATE: 04/08/2003| | UNIT: [] [2] [] STATE: CA |NOTIFICATION TIME: 19:36[EDT]| | RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 04/08/2003| +------------------------------------------------+EVENT TIME: 14:53[PDT]| | NRC NOTIFIED BY: TONY CHITWOOD |LAST UPDATE DATE: 04/08/2003| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |DAVE LOVELESS R4 | |10 CFR SECTION: | | |AESF 50.72(b)(3)(iv)(A) VALID SPECIF SYS ACTUAT| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Cold Shutdown |0 Cold Shutdown | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUXILIARY FEEDWATER ACTUATION DUE TO LOW STEAM GENERATOR WATER LEVEL | | | | The following information was received from the Licensee via facsimile: | | | | "On April 8, 2003 with Unit 2 in Mode 5 (Cold Shutdown), the auxiliary | | feedwater (AFW) system automatically actuated on a valid signal when the | | solid state protection system (SSPS) was placed in service while the steam | | generator level was below the AFW actuation set point. The actuation was | | unplanned. | | | | "S/G [Steam Generator] 2-1 level had been lowered to below the feed ring for | | work on an AFW system check valve. Operations was performing testing on the | | AFW system using AFW Pump 2-2, and was going to restore S/G level to normal | | (approximately 33% narrow range level) during the test. In conjunction with | | the AFW system testing, SSPS was being placed in service in preparation for | | an expected Mode 4 transition later in the watch after the AFW system | | testing was complete. When SSPS was placed in service, the low level in S/G | | 2-1 made up the coincidence for starting the motor driven AFW pumps. AFW | | Pump 2-2 was in operation, but AFW Pump 2-3 started in response to the low | | S/G level. AFW Pump 2-3 was aligned for recirculation flow, and did not feed | | forward on the automatic start. Operations then restored S/G 2-1 level above | | the low level trip point and secured AFW Pump 2-3. | | | | "The start of AFW Pump 2-3 on a valid low level signal from S/G 2-1 is | | reportable as an 8 [hr.] non-emergency | | report." | | | | In addition to the AFW actuation, the Licensees did receive a S/G blowdown | | isolation signal but S/G blowdown was not in service at the time. | | | | The Licensee has informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021