Event Notification Report for April 8, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 04/07/2003 - 04/08/2003 ** EVENT NUMBERS ** 39723 39740 39741 +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39723 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 04/03/2003| |LICENSEE: TEXAS DEPT OF TRANSPORTATION |NOTIFICATION TIME: 12:21[EST]| | CITY: ABILENE REGION: 4 |EVENT DATE: 03/31/2003| | COUNTY: STATE: TX |EVENT TIME: 22:00[CST]| |LICENSE#: L00197 AGREEMENT: Y |LAST UPDATE DATE: 04/03/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |ANTHONY GODY R4 | | | | +------------------------------------------------+ | | NRC NOTIFIED BY: JAMES H. OGDEN, JR | | | HQ OPS OFFICER: ERIC THOMAS | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | ATTEMPTED THEFT OF A TROXLER GAUGE | | | | The Texas Department of Health reported the attempted theft of a Troxler | | Model 3430, (serial # unknown), on the night of 3/31/03 from a secure | | storage trailer at a Texas Department of Transportation construction site in | | Abilene, TX. Site personnel discovered the gauge in an open case on the | | floor of a construction trailer with its lock cut. The trailer and its | | storage closet had been broken into. The sealed source contains 8 | | millicuries of Cs-137 and 40 millicuries of Am-241/Be. Gauge is currently | | secured in a different area awaiting results of leak and serviceability | | tests. An investigation is in process to determine whether other items were | | stolen, or whether this gauge was the only target of the attempted theft. | | | | This event is technically not reportable, but was entered as an attempted | | theft due to three other similar incidents that did result in stolen gauges | | in the Dallas-Fort Worth area under similar circumstances. The Texas | | Department of Transportation notified all other licensee's possessing | | portable nuclear gauges in the Abiline and Dallas-Fort Worth regions, along | | with local police and the Dallas FBI office. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39740 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: DAVIS BESSE REGION: 3 |NOTIFICATION DATE: 04/07/2003| | UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 17:30[EDT]| | RXTYPE: [1] B&W-R-LP |EVENT DATE: 04/07/2003| +------------------------------------------------+EVENT TIME: 17:00[EDT]| | NRC NOTIFIED BY: Art Lewis |LAST UPDATE DATE: 04/07/2003| | HQ OPS OFFICER: ERIC THOMAS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MICHAEL PARKER R3 | |10 CFR SECTION: | | |AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Cold Shutdown |0 Cold Shutdown | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNANALYZED CONDITION | | | | "During the System Health Readiness Review at Davis-Besse Nuclear Power | | Plant, a potential issue was discovered concerning operability of the HPI | | Pumps. When the HPI Pumps are taking suction from the emergency sump (i.e., | | under post LOCA condition after the initial HPI injection has occurred and | | BWST has been depleted), it could receive particle size that could damage or | | render the HPI pumps inoperable due to sump debris. A review of pump design | | and rotor dynamic analysis have determined that [the] pumps are unsuitable | | to take suction from a source that contains debris in the water, such as the | | post LOCA debris (i.e., fibrous material from insulation) in the containment | | emergency sump. | | | | "The above issue is documented in Condition Report 03-01738 and is currently | | being further investigated. Davis-Besse has determined that the above | | condition will be reportable under 10 CFR 50.73(a)(b)(v), Event or Condition | | that could have prevented fulfillment of a safety function, and 10 CFR | | 50.73(a)(2)(ii), Degraded or Unanalyzed Condition. Although this condition | | was discovered during plant shutdown where HPI pumps are not required to be | | operable per TS 3.5.2, a subsequent review of immediate notification | | requirements found this condition may require an 8 hour notification via 10 | | CFR 50.72(b)(3)(ii), i.e., that is to report a historical condition where | | [a] degraded/unanalyzed condition existed within 3 years. The Statements of | | Consideration for this reporting criterion implies such conditions if it | | existed within 3 years should be reported via 10 CFR 50.72(b)(3)(ii)." | | | | The licensee notified the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39741 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: CALVERT CLIFFS REGION: 1 |NOTIFICATION DATE: 04/07/2003| | UNIT: [] [2] [] STATE: MD |NOTIFICATION TIME: 22:36[EDT]| | RXTYPE: [1] CE,[2] CE |EVENT DATE: 04/07/2003| +------------------------------------------------+EVENT TIME: 22:19[EDT]| | NRC NOTIFIED BY: DAVE LYNCH |LAST UPDATE DATE: 04/08/2003| | HQ OPS OFFICER: ERIC THOMAS +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: UNUSUAL EVENT |JAMES TRAPP R1 | |10 CFR SECTION: |BRUCE BOGER NRR | |AAEC 50.72(a) (1) (i) EMERGENCY DECLARED |RICHARD WESSMAN IRO | | |WILLIAM KANE ET | | |HUBERT MILLER RI | | |FEMA | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N N 0 Refueling |0 Refueling | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | UNUSUAL EVENT | | | | At 2201, a fire started in the pressurizer doghouse. Welding operations | | were ongoing in the upper part of the space, and a slag catchment device | | lower in the space caught fire. The fire brigade responded to the scene. | | At 2219, the licensee declared an Unusual Event because of an ongoing fire | | in the vital area for greater than 15 minutes. At 2234, the fire was put | | out by pouring water down onto the fire from above, and a reflash watch was | | set. There was no damage noted to plant equipment, and no injuries to | | personnel. | | | | The licensee notified the NRC Resident Inspector and the surrounding | | counties. | | | | * * * UPDATE AT 2309 ON 4/7/03 FROM DAVE SEPANICH TO ERIC THOMAS * * * | | | | At 2300, the licensee secured from the Unusual Event. There was no damage | | noted to plant components, and scaffolding will be erected to conduct | | further inspections. | | | | The licensee notified the NRC Resident Inspector and the surrounding | | counties. | | | | * * * UPDATE AT 0008 ON 4/8/03 FROM MIKE KORSNICK TO ERIC THOMAS * * * | | | | The cause of the fire was slag from welding operations that fell through | | some fire blankets and ignited the herculite underneath. A fire brigade | | member will be sent back into the space this morning to conduct further | | damage assessment. | +------------------------------------------------------------------------------+
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Page Last Reviewed/Updated Thursday, March 25, 2021