The U.S. Nuclear Regulatory Commission is in the process of rescinding or revising guidance and policies posted on this webpage in accordance with Executive Order 14151 Ending Radical and Wasteful Government DEI Programs and Preferencing, and Executive Order 14168 Defending Women From Gender Ideology Extremism and Restoring Biological Truth to the Federal Government. In the interim, any previously issued diversity, equity, inclusion, or gender-related guidance on this webpage should be considered rescinded that is inconsistent with these Executive Orders.

Event Notification Report for March 5, 2003








                    U.S. Nuclear Regulatory Commission

                              Operations Center



                              Event Reports For

                           03/04/2003 - 03/05/2003



                              ** EVENT NUMBERS **



39488  39626  39635  39636  39637  



!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED  !!!!!!!

+------------------------------------------------------------------------------+

|Power Reactor                                    |Event Number:   39488       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| FACILITY: QUAD CITIES              REGION:  3  |NOTIFICATION DATE: 01/04/2003|

|    UNIT:  [] [2] []                 STATE:  IL |NOTIFICATION TIME: 07:47[EST]|

|   RXTYPE: [1] GE-3,[2] GE-3                    |EVENT DATE:        01/04/2003|

+------------------------------------------------+EVENT TIME:        01:13[CST]|

| NRC NOTIFIED BY:  JOHN LECHMAIER               |LAST UPDATE DATE:  03/04/2003|

|  HQ OPS OFFICER:  HOWIE CROUCH                 +-----------------------------+

+------------------------------------------------+PERSON          ORGANIZATION |

|EMERGENCY CLASS:          NON EMERGENCY         |ROGER LANKSBURY      R3      |

|10 CFR SECTION:                                 |                             |

|AIND 50.72(b)(3)(v)(D)   ACCIDENT MITIGATION    |                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|                                                   |                          |

|2     N          Y       100      Power Operation  |100      Power Operation  |

|                                                   |                          |

+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| LOW PRESSURE COOLANT INJECTION DECLARED INOPERABLE                           |

|                                                                              |

| "At 0113 hours CST on 1/4/2003, SR 3.5.1.1 [Surveillance Requirement]        |

| (monthly fill and vent surveillance) was initiated on U-2 B RHR loop.  When  |

| the high point vents were opened, no flow was observed within the            |

| established venting criteria required by the surveillance.  Based on this,   |

| neither LPCI [Low Pressure Coolant Injection] subsystem could be ensured     |

| filled to the injection valves.  Both LPCI subsystems were declared          |

| inoperable and TS 3.5.1 [Technical Specification] Condition D [was] entered. |

| At 0204 hours CST, when full flow was observed from the 2B RHR loop, TS      |

| 3.5.1 Condition D was exited.  At 0210 hours CST, 2A RHR loop was            |

| subsequently vented and full flow was observed immediately.                  |

|                                                                              |

| "This notification is being made in accordance with                          |

| 10CFR50.72(b)(3)(v)[(D)]."                                                   |

|                                                                              |

| Licensee has informed the NRC Resident Inspector.                            |

|                                                                              |

| *** EVENT RETRACTED ON 3/4/03 1157 EST BY MIKE SWEGLE TO ERIC THOMAS ***     |

|                                                                              |

| "ENS Retraction - Low Pressure Coolant Injection Declared Inoperable         |

|                                                                              |

| "The purpose of this notification is to retract the ENS report made on       |

| 1/04/2003 at 0747 EST (Event #39488). The initial report was made when it    |

| appeared the established venting criteria for Low Pressure Coolant Injection |

| (LPCI) was not met during the monthly fill and vent surveillance. A          |

| subsequent investigation has determined that the LPCI system was properly    |

| filled and vented at the time. A review of plant parameters (including alarm |

| data, system piping configuration, and Reactor Building Equipment Drain Tank |

| flow indications) confirmed that the RHR piping was properly filled.         |

|                                                                              |

| "The original event is attributed to difficulty in interpreting the sight    |

| glass indications during the venting process. The sight glass indicator used |

| to visually verify that flow is established during the venting surveillance  |

| was not properly drained.                                                    |

|                                                                              |

| "For these reasons, Quad Cities Station has determined that the LPCI system  |

| was fully operable at the time of the event."                                |

|                                                                              |

| The licensee has informed the NRC Resident Inspector.                        |

+------------------------------------------------------------------------------+



+------------------------------------------------------------------------------+

|General Information or Other                     |Event Number:   39626       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| REP ORG:  MA RADIATION CONTROL PROGRAM         |NOTIFICATION DATE: 02/28/2003|

|LICENSEE:  NITON CORP                           |NOTIFICATION TIME: 13:46[EST]|

|    CITY:  BILLERICA                REGION:  1  |EVENT DATE:        02/05/2003|

|  COUNTY:                            STATE:  MA |EVENT TIME:        15:00[EST]|

|LICENSE#:  55-0238               AGREEMENT:  Y  |LAST UPDATE DATE:  02/28/2003|

|  DOCKET:                                       |+----------------------------+

|                                                |PERSON          ORGANIZATION |

|                                                |JOHN KINNEMAN        R1      |

|                                                |FRED BROWN           NMSS    |

+------------------------------------------------+MARISSA BAILEY-email NMSS    |

| NRC NOTIFIED BY:  KENATH TRAEGDE               |                             |

|  HQ OPS OFFICER:  GERRY WAIG                   |                             |

+------------------------------------------------+                             |

|EMERGENCY CLASS:          NON EMERGENCY         |                             |

|10 CFR SECTION:                                 |                             |

|NAGR                     AGREEMENT STATE        |                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

+------------------------------------------------------------------------------+



                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| AGREEMENT STATE REPORT- RECEIPT OF CONTAMINATED PACKAGES                     |

|                                                                              |

| The following is taken from an email received from the MA Dept. of Public    |

| Health, Radiation Control Program:                                           |

|                                                                              |

| "On Wednesday, February 5, 2003, it was discovered that a routine wipe of an |

| incoming 20 millicurie (0.740 GBq) Iron-55 source ordered from AEA           |

| Technology QSA, Inc. was contaminated.  The wipe was sent off for analysis.  |

| On Friday, February 14, the wipe was reported to contain 213.7 nanocuries    |

| (7.91kBq) of Iron-55 contamination.  The distributor, AEA Technology QSA,    |

| Inc., was notified of the leaking source as was the Radiation Control        |

| Program of the Massachusetts Department of Public Health.                    |

|                                                                              |

| "In the interim, on Monday, February 24, 2003, another incoming Iron-55      |

| leaking source from the same lot number was discovered by Niton Corporation  |

| at approximately 5:00 p.m.  The wipe has been sent to an authorized          |

| consultant for further analysis.  The level of contamination of the second   |

| source has not been reported to the Agency at the time of this report.       |

| Again, the manufacturer/distributor, AEA Technology QSA, Inc., was notified  |

| of the leaking source as was the Radiation Control Program.                  |

|                                                                              |

| "An investigation into these leaking source events has been initiated by the |

| Radiation Control Program."                                                  |

+------------------------------------------------------------------------------+



+------------------------------------------------------------------------------+

|Power Reactor                                    |Event Number:   39635       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| FACILITY: NORTH ANNA               REGION:  2  |NOTIFICATION DATE: 03/04/2003|

|    UNIT:  [1] [] []                 STATE:  VA |NOTIFICATION TIME: 10:33[EST]|

|   RXTYPE: [1] W-3-LP,[2] W-3-LP                |EVENT DATE:        03/04/2003|

+------------------------------------------------+EVENT TIME:        08:54[EST]|

| NRC NOTIFIED BY:  CROSSMAN                     |LAST UPDATE DATE:  03/04/2003|

|  HQ OPS OFFICER:  CHAUNCEY GOULD               +-----------------------------+

+------------------------------------------------+PERSON          ORGANIZATION |

|EMERGENCY CLASS:          NON EMERGENCY         |WALTER RODGERS       R2      |

|10 CFR SECTION:                                 |                             |

|ADEG 50.72(b)(3)(ii)(A)  DEGRADED CONDITION     |                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|1     N          N       0        Refueling        |0        Refueling        |

|                                                   |                          |

|                                                   |                          |

+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| THROUGH WALL LEAKAGE IDENTIFIED ON VESSEL HEAD PENETRATION                   |

|                                                                              |

| A through wall leak was noted during a VT-2 inspection of reactor vessel     |

| head penetration "50".  This condition has been assessed as a degradation of |

| a principle safety barrier.   Unit 1 is in a maintenance and refueling       |

| outage and is replacing the reactor vessel head during this outage.  The old |

| head was visually inspected at penetration "50" to followup on inspection    |

| results from a previous outage in 2001.                                      |

|                                                                              |

|                                                                              |

| The NRC Licensee was notified.                                               |

+------------------------------------------------------------------------------+



+------------------------------------------------------------------------------+

|Power Reactor                                    |Event Number:   39636       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| FACILITY: LASALLE                  REGION:  3  |NOTIFICATION DATE: 03/04/2003|

|    UNIT:  [] [2] []                 STATE:  IL |NOTIFICATION TIME: 12:02[EST]|

|   RXTYPE: [1] GE-5,[2] GE-5                    |EVENT DATE:        03/04/2003|

+------------------------------------------------+EVENT TIME:        03:11[CST]|

| NRC NOTIFIED BY:  JOHN REIMER                  |LAST UPDATE DATE:  03/04/2003|

|  HQ OPS OFFICER:  GERRY WAIG                   +-----------------------------+

+------------------------------------------------+PERSON          ORGANIZATION |

|EMERGENCY CLASS:          NON EMERGENCY         |MONTE PHILLIPS       R3      |

|10 CFR SECTION:                                 |                             |

|AINV 50.73(a)(1)         INVALID SPECIF SYSTEM A|                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |

+-----+----------+-------+--------+-----------------+--------+-----------------+

|                                                   |                          |

|2     N          Y       100      Power Operation  |100      Power Operation  |

|                                                   |                          |

+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| AUTOMATIC START OF THE DIV 1 DIESEL GENERATOR COOLING WATER PUMP             |

|                                                                              |

| "ON MARCH 3rd, 2003, AT 0311 HOURS, WITH UNIT 2 IN MODE 1 (RUN), THE         |

| DIVISION 1, DIESEL GENERATOR COOLING WATER PUMP (DGCWP), WHICH PROVIDES THE  |

| EMERGENCY SERVICE WATER TO THE RESIDUAL HEAT REMOVAL (RHR) ROOM COOLERS      |

| (VY), AUTOMATICALLY STARTED DURING THE PERFORMANCE OF A MAINTENANCE ACTIVITY |

| ASSOCIATED WITH THE UNIT 2 RESIDUAL HEAT REMOVAL (RHR) CORNER ROOM FAN (VY)  |

| BREAKER INSPECTION. THE APPARENT CAUSE OF THE AUTO START WAS THE ACTUATION   |

| OF THE AUXILIARY CONTACTS IN THE FAN BREAKER CUBICLE BY THE TECHNICIAN AS    |

| PART OF THE MAINTENANCE ACTIVITY. THE APPARENT CAUSE WAS THE RESULT OF AN    |

| INADEQUATE REVIEW OF THE ELECTRICAL RELAY LOGIC DURING DEVELOPMENT OF THE    |

| INSTRUCTION FOR THE MAINTENANCE ACTIVITY. THIS ACTUATION OF THE AUXILIARY    |

| CONTACTS PROVIDED AN INVALID SIGNAL THAT CAUSED THE DIVISION 1 DIESEL        |

| GENERATOR COOLING WATER PUMP TO LOGICALLY BELIEVE THE 2A RHR PUMP ROOM       |

| COOLING FAN WAS RUNNING, THEREBY GENERATING AN AUTO START SIGNAL. THIS       |

| INVALID BREAKER CONTACT CLOSURE RESULTED IN THE AUTOMATIC ACTUATION OF THE   |

| DIVISION 1 DGCWP. THIS SYSTEM ACTUATION IS REPORTABLE UNDER 10CFR50.73 (a)   |

| (2) (iv) (A).                                                                |

|                                                                              |

| "THE DIVISION 1 DIESEL GENERATOR COOLING WATER PUMP RESPONDED                |

| SATISFACTORILY.                                                              |

|                                                                              |

| "THIS REPORT IS BEING MADE IN ACCORDANCE WITH 10CFR50.73 (a) (1), WHICH      |

| STATES THAT IN THE CASE OF AN INVALID ACTUATION REPORTED UNDER 10CFR50 .73   |

| (a) (2) (iv), OTHER THAN AN ACTUATION OF THE REACTOR PROTECTION SYSTEM (RPS) |

| WHEN THE REACTOR IS CRITICAL, THE LICENSEE MAY PROVIDE A TELEPHONE           |

| NOTIFICATION TO THE NRC OPERATIONS CENTER WITHIN 60 DAYS AFTER DISCOVERY OF  |

| THE EVENT INSTEAD OF SUBMITTING A WRITTEN LICENSEE EVENT REPORT (LER)."      |

|                                                                              |

| The licensee has notified NRC Resident Inspector.                            |

+------------------------------------------------------------------------------+



+------------------------------------------------------------------------------+

|General Information or Other                     |Event Number:   39637       |

+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+

| REP ORG:  3M CORPORATION                       |NOTIFICATION DATE: 03/04/2003|

|LICENSEE:  3M CORPORATION                       |NOTIFICATION TIME: 14:50[EST]|

|    CITY:  ST PAUL                  REGION:  3  |EVENT DATE:        03/04/2003|

|  COUNTY:                            STATE:  MN |EVENT TIME:             [CST]|

|LICENSE#:  22-00057-03           AGREEMENT:  N  |LAST UPDATE DATE:  03/04/2003|

|  DOCKET:                                       |+----------------------------+

|                                                |PERSON          ORGANIZATION |

|                                                |MONTE PHILLIPS       R3      |

|                                                |DON COOL             NMSS    |

+------------------------------------------------+MOHAMED SHANBAKY     R1      |

| NRC NOTIFIED BY:  FRED ENTWISTLE               |JOHN DAVIDSON        TAT     |

|  HQ OPS OFFICER:  GERRY WAIG                   |                             |

+------------------------------------------------+                             |

|EMERGENCY CLASS:          NON EMERGENCY         |                             |

|10 CFR SECTION:                                 |                             |

|BLO1 20.2201(a)(1)(i)    LOST/STOLEN LNM>1000X  |                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

|                                                |                             |

+------------------------------------------------------------------------------+



                                   EVENT TEXT                                   

+------------------------------------------------------------------------------+

| LOST OR STOLEN, ANTI-STATIC, POLONIUM 210 SOURCE                             |

|                                                                              |

| A 0.3 millicurie, Polonium 210 source, nuclear static eliminator, model      |

| P2001, serial number A2BG425 was reported as not received being by the       |

| recipient. The source is used in a laboratory balance application to         |

| eliminate static charge and is about 2 inches long. The original source      |

| strength was 4.5 millicuries (8/2002) and 0.3 millicuries as of 3/2003. The  |

| shipment was made on January 6, 2003 from 3M Corporation, St Paul, MN to the |

| manufacturer of the static eliminator, NRD, Grand Island, NY. This shipment  |

| consisted of 42 sources, in a common box, of which the recipient reported    |

| receipt of only 41 sources.  A extensive search has been conducted for the   |

| missing source by the sender and recipient with negative results.            |

+------------------------------------------------------------------------------+





                    

Page Last Reviewed/Updated Thursday, March 25, 2021