Event Notification Report for March 5, 2003
U.S. Nuclear Regulatory Commission Operations Center Event Reports For 03/04/2003 - 03/05/2003 ** EVENT NUMBERS ** 39488 39626 39635 39636 39637 !!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!! +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39488 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: QUAD CITIES REGION: 3 |NOTIFICATION DATE: 01/04/2003| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 07:47[EST]| | RXTYPE: [1] GE-3,[2] GE-3 |EVENT DATE: 01/04/2003| +------------------------------------------------+EVENT TIME: 01:13[CST]| | NRC NOTIFIED BY: JOHN LECHMAIER |LAST UPDATE DATE: 03/04/2003| | HQ OPS OFFICER: HOWIE CROUCH +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |ROGER LANKSBURY R3 | |10 CFR SECTION: | | |AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOW PRESSURE COOLANT INJECTION DECLARED INOPERABLE | | | | "At 0113 hours CST on 1/4/2003, SR 3.5.1.1 [Surveillance Requirement] | | (monthly fill and vent surveillance) was initiated on U-2 B RHR loop. When | | the high point vents were opened, no flow was observed within the | | established venting criteria required by the surveillance. Based on this, | | neither LPCI [Low Pressure Coolant Injection] subsystem could be ensured | | filled to the injection valves. Both LPCI subsystems were declared | | inoperable and TS 3.5.1 [Technical Specification] Condition D [was] entered. | | At 0204 hours CST, when full flow was observed from the 2B RHR loop, TS | | 3.5.1 Condition D was exited. At 0210 hours CST, 2A RHR loop was | | subsequently vented and full flow was observed immediately. | | | | "This notification is being made in accordance with | | 10CFR50.72(b)(3)(v)[(D)]." | | | | Licensee has informed the NRC Resident Inspector. | | | | *** EVENT RETRACTED ON 3/4/03 1157 EST BY MIKE SWEGLE TO ERIC THOMAS *** | | | | "ENS Retraction - Low Pressure Coolant Injection Declared Inoperable | | | | "The purpose of this notification is to retract the ENS report made on | | 1/04/2003 at 0747 EST (Event #39488). The initial report was made when it | | appeared the established venting criteria for Low Pressure Coolant Injection | | (LPCI) was not met during the monthly fill and vent surveillance. A | | subsequent investigation has determined that the LPCI system was properly | | filled and vented at the time. A review of plant parameters (including alarm | | data, system piping configuration, and Reactor Building Equipment Drain Tank | | flow indications) confirmed that the RHR piping was properly filled. | | | | "The original event is attributed to difficulty in interpreting the sight | | glass indications during the venting process. The sight glass indicator used | | to visually verify that flow is established during the venting surveillance | | was not properly drained. | | | | "For these reasons, Quad Cities Station has determined that the LPCI system | | was fully operable at the time of the event." | | | | The licensee has informed the NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39626 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: MA RADIATION CONTROL PROGRAM |NOTIFICATION DATE: 02/28/2003| |LICENSEE: NITON CORP |NOTIFICATION TIME: 13:46[EST]| | CITY: BILLERICA REGION: 1 |EVENT DATE: 02/05/2003| | COUNTY: STATE: MA |EVENT TIME: 15:00[EST]| |LICENSE#: 55-0238 AGREEMENT: Y |LAST UPDATE DATE: 02/28/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |JOHN KINNEMAN R1 | | |FRED BROWN NMSS | +------------------------------------------------+MARISSA BAILEY-email NMSS | | NRC NOTIFIED BY: KENATH TRAEGDE | | | HQ OPS OFFICER: GERRY WAIG | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |NAGR AGREEMENT STATE | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AGREEMENT STATE REPORT- RECEIPT OF CONTAMINATED PACKAGES | | | | The following is taken from an email received from the MA Dept. of Public | | Health, Radiation Control Program: | | | | "On Wednesday, February 5, 2003, it was discovered that a routine wipe of an | | incoming 20 millicurie (0.740 GBq) Iron-55 source ordered from AEA | | Technology QSA, Inc. was contaminated. The wipe was sent off for analysis. | | On Friday, February 14, the wipe was reported to contain 213.7 nanocuries | | (7.91kBq) of Iron-55 contamination. The distributor, AEA Technology QSA, | | Inc., was notified of the leaking source as was the Radiation Control | | Program of the Massachusetts Department of Public Health. | | | | "In the interim, on Monday, February 24, 2003, another incoming Iron-55 | | leaking source from the same lot number was discovered by Niton Corporation | | at approximately 5:00 p.m. The wipe has been sent to an authorized | | consultant for further analysis. The level of contamination of the second | | source has not been reported to the Agency at the time of this report. | | Again, the manufacturer/distributor, AEA Technology QSA, Inc., was notified | | of the leaking source as was the Radiation Control Program. | | | | "An investigation into these leaking source events has been initiated by the | | Radiation Control Program." | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39635 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: NORTH ANNA REGION: 2 |NOTIFICATION DATE: 03/04/2003| | UNIT: [1] [] [] STATE: VA |NOTIFICATION TIME: 10:33[EST]| | RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 03/04/2003| +------------------------------------------------+EVENT TIME: 08:54[EST]| | NRC NOTIFIED BY: CROSSMAN |LAST UPDATE DATE: 03/04/2003| | HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |WALTER RODGERS R2 | |10 CFR SECTION: | | |ADEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION | | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ |1 N N 0 Refueling |0 Refueling | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | THROUGH WALL LEAKAGE IDENTIFIED ON VESSEL HEAD PENETRATION | | | | A through wall leak was noted during a VT-2 inspection of reactor vessel | | head penetration "50". This condition has been assessed as a degradation of | | a principle safety barrier. Unit 1 is in a maintenance and refueling | | outage and is replacing the reactor vessel head during this outage. The old | | head was visually inspected at penetration "50" to followup on inspection | | results from a previous outage in 2001. | | | | | | The NRC Licensee was notified. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |Power Reactor |Event Number: 39636 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | FACILITY: LASALLE REGION: 3 |NOTIFICATION DATE: 03/04/2003| | UNIT: [] [2] [] STATE: IL |NOTIFICATION TIME: 12:02[EST]| | RXTYPE: [1] GE-5,[2] GE-5 |EVENT DATE: 03/04/2003| +------------------------------------------------+EVENT TIME: 03:11[CST]| | NRC NOTIFIED BY: JOHN REIMER |LAST UPDATE DATE: 03/04/2003| | HQ OPS OFFICER: GERRY WAIG +-----------------------------+ +------------------------------------------------+PERSON ORGANIZATION | |EMERGENCY CLASS: NON EMERGENCY |MONTE PHILLIPS R3 | |10 CFR SECTION: | | |AINV 50.73(a)(1) INVALID SPECIF SYSTEM A| | | | | | | | | | | +-----+----------+-------+--------+-----------------+--------+-----------------+ |UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE | +-----+----------+-------+--------+-----------------+--------+-----------------+ | | | |2 N Y 100 Power Operation |100 Power Operation | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | AUTOMATIC START OF THE DIV 1 DIESEL GENERATOR COOLING WATER PUMP | | | | "ON MARCH 3rd, 2003, AT 0311 HOURS, WITH UNIT 2 IN MODE 1 (RUN), THE | | DIVISION 1, DIESEL GENERATOR COOLING WATER PUMP (DGCWP), WHICH PROVIDES THE | | EMERGENCY SERVICE WATER TO THE RESIDUAL HEAT REMOVAL (RHR) ROOM COOLERS | | (VY), AUTOMATICALLY STARTED DURING THE PERFORMANCE OF A MAINTENANCE ACTIVITY | | ASSOCIATED WITH THE UNIT 2 RESIDUAL HEAT REMOVAL (RHR) CORNER ROOM FAN (VY) | | BREAKER INSPECTION. THE APPARENT CAUSE OF THE AUTO START WAS THE ACTUATION | | OF THE AUXILIARY CONTACTS IN THE FAN BREAKER CUBICLE BY THE TECHNICIAN AS | | PART OF THE MAINTENANCE ACTIVITY. THE APPARENT CAUSE WAS THE RESULT OF AN | | INADEQUATE REVIEW OF THE ELECTRICAL RELAY LOGIC DURING DEVELOPMENT OF THE | | INSTRUCTION FOR THE MAINTENANCE ACTIVITY. THIS ACTUATION OF THE AUXILIARY | | CONTACTS PROVIDED AN INVALID SIGNAL THAT CAUSED THE DIVISION 1 DIESEL | | GENERATOR COOLING WATER PUMP TO LOGICALLY BELIEVE THE 2A RHR PUMP ROOM | | COOLING FAN WAS RUNNING, THEREBY GENERATING AN AUTO START SIGNAL. THIS | | INVALID BREAKER CONTACT CLOSURE RESULTED IN THE AUTOMATIC ACTUATION OF THE | | DIVISION 1 DGCWP. THIS SYSTEM ACTUATION IS REPORTABLE UNDER 10CFR50.73 (a) | | (2) (iv) (A). | | | | "THE DIVISION 1 DIESEL GENERATOR COOLING WATER PUMP RESPONDED | | SATISFACTORILY. | | | | "THIS REPORT IS BEING MADE IN ACCORDANCE WITH 10CFR50.73 (a) (1), WHICH | | STATES THAT IN THE CASE OF AN INVALID ACTUATION REPORTED UNDER 10CFR50 .73 | | (a) (2) (iv), OTHER THAN AN ACTUATION OF THE REACTOR PROTECTION SYSTEM (RPS) | | WHEN THE REACTOR IS CRITICAL, THE LICENSEE MAY PROVIDE A TELEPHONE | | NOTIFICATION TO THE NRC OPERATIONS CENTER WITHIN 60 DAYS AFTER DISCOVERY OF | | THE EVENT INSTEAD OF SUBMITTING A WRITTEN LICENSEE EVENT REPORT (LER)." | | | | The licensee has notified NRC Resident Inspector. | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ |General Information or Other |Event Number: 39637 | +------------------------------------------------------------------------------+ +------------------------------------------------------------------------------+ | REP ORG: 3M CORPORATION |NOTIFICATION DATE: 03/04/2003| |LICENSEE: 3M CORPORATION |NOTIFICATION TIME: 14:50[EST]| | CITY: ST PAUL REGION: 3 |EVENT DATE: 03/04/2003| | COUNTY: STATE: MN |EVENT TIME: [CST]| |LICENSE#: 22-00057-03 AGREEMENT: N |LAST UPDATE DATE: 03/04/2003| | DOCKET: |+----------------------------+ | |PERSON ORGANIZATION | | |MONTE PHILLIPS R3 | | |DON COOL NMSS | +------------------------------------------------+MOHAMED SHANBAKY R1 | | NRC NOTIFIED BY: FRED ENTWISTLE |JOHN DAVIDSON TAT | | HQ OPS OFFICER: GERRY WAIG | | +------------------------------------------------+ | |EMERGENCY CLASS: NON EMERGENCY | | |10 CFR SECTION: | | |BLO1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | | | | | | | | | | | | | | +------------------------------------------------------------------------------+ EVENT TEXT +------------------------------------------------------------------------------+ | LOST OR STOLEN, ANTI-STATIC, POLONIUM 210 SOURCE | | | | A 0.3 millicurie, Polonium 210 source, nuclear static eliminator, model | | P2001, serial number A2BG425 was reported as not received being by the | | recipient. The source is used in a laboratory balance application to | | eliminate static charge and is about 2 inches long. The original source | | strength was 4.5 millicuries (8/2002) and 0.3 millicuries as of 3/2003. The | | shipment was made on January 6, 2003 from 3M Corporation, St Paul, MN to the | | manufacturer of the static eliminator, NRD, Grand Island, NY. This shipment | | consisted of 42 sources, in a common box, of which the recipient reported | | receipt of only 41 sources. A extensive search has been conducted for the | | missing source by the sender and recipient with negative results. | +------------------------------------------------------------------------------+
Page Last Reviewed/Updated Thursday, March 25, 2021
Page Last Reviewed/Updated Thursday, March 25, 2021